(page 90 of 166)

Scupper 196

Thursday

After some minor surface preparation and fiberglass cutting, I installed 10 layers of biaxial fiberglass to fill the space I’d opened up in the overhead liner beneath the mast step.  This brought the surface close to flush with the old liner.

While I let the fiberglass cure for a while, I installed the AC shore power plug with my newly-arrived 10/3 cable, securing the wires to the receptacle as needed and fastening the strain relief in place after leading the wires out what would be the aft side of the housing.  Then, I installed the receptacle in the coaming, this time with its supplied gasket in place.

From below, I left some excess wire looped up inside the coaming to allow removal of the plug from outside if needed, then secured the cable along the inside of the coaming and around the aft side of the cockpit and then up the starboard side to the aft bulkhead, where I left the excess for now, pending the final run up to the electrical panel in the near future.

By now, the new fiberglass at the mast step had cured sufficiently to allow me to apply some epoxy compound thickened with high-density filler over the plug, bringing the whole area flush with the adjacent liner.  This would provide the necessary firm support for the compression post, and also allow me fresh, flat material into which I could recess the mast step nuts and washers.

While I had mast step on the mind, I marked and drilled the new stainless steel organizer plate for the mast step bolts.

With fittings and hoses now on hand, I chose to install the cockpit scuppers.  I’d long ago removed the old plastic fittings from the cockpit, and the remaining holes needed just some minor cleanup and, on the port side, slight enlargement to fit the new bronze drain fittings, which I then installed in a heavy bed of sealant.

In the engine room, I installed new hoses and clamps to complete the scupper drains.

While I was working in the engine room, I slightly changed how I’d led the positive battery cable to the engine to clean up the appearance of the two cables just forward of the engine room.  With new parts now on hand, I could also install a couple more line clamps for the yellow negative cable, and fully secure the engine battery switch with four screws through the external housing.

Looking for a loose end to fill the last part of the afternoon, I decided to install the bobstay tang on the stem, now that I had the new fasteners I needed on hand.  After reaming out the bolt holes to remove debris, and removing the bottom paint in way of the bonding surface, installation was a fairly straightforward affair, using copious amounts of sealant to bed the fitting and fasteners.  Sticking with what had been there originally, I chose extra heavy nuts to secure the bolts from the small space below the chain locker, using locking pliers to hold the nuts while I tightened the bolts from outside.  Afterwards, I cleaned up the excess sealant.

Total time billed on this job today:  8.25 hours

0600 Weather Observation:  18°, clear.  Forecast for the day:  Partly sunny, 38°

Scupper 195

Wednesday

Now that the interior companionway hatch paint was complete, I was ready to move on with its final installation.  First, however, I wanted to install a solar vent that the owner requested.  To my dismay, however, when I opened the package I found the vent was absolutely massive, which was one thing, but even worse, it was incredibly tall/deep, and I knew at a glance that the housing was far too deep to work in the companionway, which was only roughly 3/4″ thick.  It had been quite a while since I’d put one of these in, and apparently these vents have changed significantly from what I recalled.

I didn’t think there was much clearance below the hatch where it passed over its rails on the boat, but to be sure I brought the hatch up on deck and placed it in position, and checked the clearance beneath:  essentially none.  This meant that any vent in the hatch would require a flush fit from beneath.  To an extent, I could install a minor riser beneath the vent to reduce its depth a little, but not as much as would be required by the huge vent I’d ordered.  I packaged up the large vent for return, and sourced and ordered another, smaller version that I thought had a better chance of working.

Putting that temporary failure behind me, I moved on to the AC shore power inlet.  The owner had got in touch to let me know that he thought the inlet should be on the port side, which matched his slip configuration better than the starboard, so to confirm the possibility I used my little wooden stick to check the clearance inside the port coaming just aft of the winch island, where the plug would be out of the way of sailing gear.  With the top of the stick wedged in place within the coaming, I measured beneath it (about 3.5″ to where I estimated the top of the deck to be), which was enough space to install the receptacle there.

With the position confirmed, there was no time like the present to do the installation, so using the backing gasket as a guide, and confirming the cutout’s location against the required maximum height from within, I cut a hole for the receptacle and dry fit it with some screws.  The housing fit inside the coaming with a little room to spare.  Of course I’d have to do the wiring from outside before installing the receptacle, but this posed not problem.  The receptacle ended up fairly close to deck level by necessity, but this still allowed easy finger access to lift the cover, and as an added yet unplanned benefit, the cover, when opened completely, remained just below coaming height.

I was prepared to go ahead and pre-install the wiring and complete the receptacle installation, but after giving it some thought I realized that I should use 10/3 wiring from the plug to the panel, partly because it was some distance to the panel, wiring-wise, and partly because of the anticipated loads the boat’s pair of battery chargers (one for the 48-volt engine bank, one for the separate 12-volt house bank).  I had 12 gauge wire in stock, but had to order the 10 gauge since I rarely use that size.

With another job temporarily stymied by the impossible desire to have everything I could possibly need for any situation on hand the instant I needed it, I moved on to the electric motor, looking to wrap up its installation as much as possible.  By design, I chose not to have the new 6-volt batteries for the engine and house banks on hand till later in the project, when the wiring and charging system was complete and I could maintain the batteries, so I knew I couldn’t completely wrap up the battery cabling, but I could take care of the basics now, starting with the raw runs of positive and negative cabling from the engine to the eventual battery bank.

To begin, I used one of the battery boxes I had on hand to make some temporary marks in the engine room, largely for overall height so I’d not install any cabling below that level, but also to mark out a cable run in the center of the forward battery shelf, where I planned to run the cables between the two boxes that would sit on the shelf.  There would be four battery boxes in the engine room, each holding a par of 6-volt batteries:  two on the forward shelf, and one each on the shelves flanking the engine room on each side.

The engine wiring plan, shown below, was straightforward overall, and all the engine-based cabling and wiring (to and from the motor and motor controller box) was pre-installed at the factory, so my job now boiled down to installing positive and negative cables to the required terminals on the motor itself:  that is, terminal “A1+” on the side-mounted solenoid (positive) and the B- terminal on the motor controller (negative).

For no particular reason other than best access, I decided the positive side of the bank would start on the starboard side, where the access door from the head was located, and to begin I installed the 250-amp fuse holder a few inches above the battery box, staying close enough that the final cable length between the battery  terminal and the fuse would be as minimal as possible.  I’d wait to install that short length of cable till I had the batteries on hand.

Next in the circuit was an on-off switch, a basic battery switch, which I installed a bit above the fuse and easily accessible from the engine room access door, connecting it to the fuse with a short length of 2/0 cable.  Then, I led another length of the cable from the switch, above the doorway, and down the bulkhead and across the battery shelf through the open area in the center that I’d laid out.  (Note that the photos might jump a bit ahead of the text from here on since, because of poor access, I only photographed the setup when I’d completed the day’s wiring.)

I protected the cable with some flexible conduit where it crossed the battery shelf and engine space, and connected the other end to the proper terminal on the solenoid.

The negative battery cable needed to lead from the B- terminal on the controller box over to the port side of the eventual battery bank, so leaving ample cable for later termination, I led the cable from the engine and across the battery shelf, secured in closely with its positive compatriot.  I ran out of line clamps of the right size, so for now I left most of the yellow cable unsecured, but I’d take care of that once my replacement clamps arrived.  The 2/0 cable is heavy and stiff to work with, and I had to leave clearance for the sheet metal control box cover as I planned these cable runs.  Upon review, I realized I could redirect slightly the red cable run from the battery shelf to the solenoid connection, and made plans to do so.

With the bulk connections complete, and after double-checking the connections and tightening the bolts securely, I decided to install the cover to protect the wiring and because it was unlikely I’d need to get back in there.

Since the designers saw fit to place the main bulkhead only 12″ forward of the mast step, the mast step required a compression post beneath to transfer its loads to the keel below.  Looking to complete and install this post in the near future (and also to finalize how it was going to work with the new cosmetic plywood overhead panels), and also as I prepared to install the mast step on deck at the earliest convenience, I turned to the underside of the deck now to figure out how to proceed.  In the original fiberglass liner/overhead, holes had allowed access to the nuts and washers that had originally secured the mast step, but now I thought it would be easier if I simply cut out a portion of the old liner to open up access to the whole space.

Of course one thing led to another, and my initial cuts showed that there was a mass of (what turned out to be) unthickened polyester resin filling the space immediately beneath the mast step, with little hollows where the mast step bolts had been.  This had been to create a solid transfer between the deck and the liner, and thus with the original compression post, and this had worked fine for the boat’s life up till now.

Since I had the area open now, I decided to remove the old resin and start fresh with a solid laminate of fiberglass instead; because the whole area would be covered with my already-completed plywood panels, the appearance of this area didn’t matter.  So at some length I cut, chipped, and sanded away the old material till I reached the bottom of the deck laminate.  This left a somewhat uneven surface, so once I’d cleaned up and just before quitting time, I applied a skim coat of thickened epoxy that would give me a better base for the solid fiberglass once it cured.

Total time billed on this job today:  8 hours

0600 Weather Observation:  12°, clear, 8″ snow from yesterday.  Forecast for the day:  Mostly sunny, 35°

Scupper 194

Tuesday

The companionway hatch required a third and final coat of the semi-gloss white enamel, which I took care of first thing.

Preparing ahead for the reinstallation of various hardware, as well as the four bronze opening ports and the six elliptical deadlights, I determined what fasteners I’d need and ordered them, and also ordered a scraping attachment that I could use to remove some of the stubborn old silicone sealant from inside the deadlight openings in the cabin, in the little space between the liner and the cabin trunk itself.

With yet another fairly extensive administration and ordering session completed, I continued work on the cables from the electric motor control and battery monitor.  Now that the new wire mounts were ready to use, I could clean up and secure the cables permanently.  I ended up routing the two cables away from the engine in a different way than I thought I might, leading them down and then aft along the engine foundation to avoid any conflict with the motor cover, which wasn’t in place now but would later cover all the wiring connections to the electric motor itself.    I led the two cables through some flexible conduit in the engine room.  At the back of the battery monitor, I bundled and secured the excess cable; there was only just a little extra cable at the throttle control, and for the moment I left it unsecured pending final installation of the control and any wiring changes I might need to make there.

I’d soon continue work on some of the electric motor cabling, but was awaiting newly-ordered materials, namely the 2/0 battery cable required for the job, so instead I got to work cleaning up the chainplates, bobstay tank, and mast step to prepare them all for installation in the near future.  The external bronze chainplates were in good condition and nicely weathered, and I concentrated on removing any remnants of old sealant and stuck paint on the back sides, but otherwise left the surfaces as is.

The backstay chainplate and bobstay tang were stainless steel, and in good condition other than some surface corrosion that I removed easily.

The aluminum mast step was covered in old gunk and silicone, and at length I scraped and wire-brushed it away, also removing most of an old coating of (tough) paint and back to bare aluminum, which later I sprayed with primer to prepare it for new paint.

I planned to install the step above a new stainless steel mast organizer plate that would allow easy attachment of turning blocks to lead various control lines aft as desired.

One of the things I’d been discussing with the owner was potential locations for the shore power inlet, which would power battery chargers and a basic AC electrical system on board.  The owner preferred not to have the plug somewhere in the cockpit well, as the cable can be a nuisance, but this did limit the other possibilities.  At issue was whether the plug could be installed on the outside of the molded coaming, which was hollow and accessible from within but fairly narrow.  With the inlet plug now on hand, I made a little wooden template of the maximum depth required within the coaming (disallowing the thickness of the coaming laminate itself,  which in this case would only increase interior clearance) and used it in a few places from beneath the coaming to check clearance.  This particular plug would be wired from the sides of the housing, so as long as the entire housing and its wiring cover backing could fit as is, the installation would be workable.

At the aft side of the cockpit coaming, my little template fit to a point, but the tapered shape of the coaming limited the potential height, which, based on the deck height outside, would be too low to allow the plug to be installed properly.

Further forward on the starboard side, there was good clearance on either side of the winch island, and the required depth within the coaming would be high enough to allow installation of the receptacle in either location, with ample room for the plug housing within at a height that would work given the overall size of the plug itself.

Total time billed on this job today:  7.25 hours

0600 Weather Observation:  26°, snow and sleet just started.  Forecast for the day:  Snow, 4-8″ forecast, 30°

Scupper 193

Monday

To finish up the deck trim, I pared away the bungs on the coaming caps that I’d installed last time.

The companionway hatch required a light sanding and then a second coat of the semi-gloss white enamel.

A while back, after completing the shaft and propeller installation, I’d ordered a shaft zinc, and now, to get it out of the way and checked off the list, I took two minutes to install it on the shaft.

With those small chores complete, I planned to shift gears and start getting into the electrical and plumbing systems in the cabin, and to that end I spent some time preparing orders for some of the materials I’d need to continue work in those directions.  Then, I set to work in the cockpit, where I planned to install the electric motor controls and a cockpit shower housing, all of which were on hand now.

The motor controller (throttle) was a simple panel with a rheostat control and key switch, and the owner had asked that I install it in the cockpit well aft of the starboard cockpit locker.  After some quick layout, I prepared the opening for the controller, drilling a pair of 2″ holes and then connecting them through the center.  Afterwards, I aligned the control panel and drilled for the six screw holes.  I installed the panel dry and only temporarily for now with two screws, since I might need to change some of the wiring leads on the back depending on whether the control knob was properly set up from the factory.

To eventually lead the control wire forward and down to the electric motor, I needed some additional wire tie mounts, so from the starboard locker I installed what I thought I needed, sanding away any locker paint in way of the mount locations before securing them in place with the mount adhesive.  I ran additional mounts aft towards the transom, planning ahead for sternlight wiring later.

The electric motor system also required a battery monitor, which I planned to install in the raised portion of the cockpit well beneath the bridgedeck.  I’d built in access to the back side of this area from the head, and to begin I removed my access panel, then made various measurements so I could roughly transfer the location of the open access area to the exterior so I’d know where to install the panel, along with some sailing instruments later on.  After the initial layout, I decided to open up the access panel a bit more along the top edge, which I did with a multi-tool.  This increased access at the top side and allowed me to install the panel where I wanted it to go.

After additional layout, and double-checking, I drilled the holes needed to install the battery monitor, which had a rather fussy means of securing it with two screws from the back side only.  There was a mounting template supplied with the panel, but I discovered–fortunately before I relied on it to do the cutting–that the template was not accurate and didn’t exactly match the actual panel and its pre-marked screw locations.

Securing the panel in place from behind, when there was no direct communication between the spaces and no helpers to be found in my one-man shop, was an exercise in patience, frustration, and fortitude, and required numerous trips back and forth between inside and outside before I could properly align, hold in place, and then tighten, the small screws to secure the panel.  I applied butyl tape sealant to the panel and around the central wiring port before installing it (the photo shows an early version of the sealant that I ultimately replaced after the first panel installation attempt failed).

At length–far greater length than such an inherently simple installation ought to require–I secured the panel successfully.

The final cockpit installation for the moment was the shower housing, which the owner had supplied and asked me to install at the forward port corner of the well.  This covered housing would ultimately hold a small shower head and hose leading from within, but for now I worked with the bare housing.  Installation was straightforward with a single large hole, butyl sealant, and three screws.

With some personal business to attend to in the afternoon, I had to call it quits for now, but next time I could lead and connect the wiring from the engine panel and battery monitor and continue with various other aspects of the systems installations.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:  24°, cloudy, a snow shower.  Forecast for the day:  Cloudy, snow showers, and snow beginning late in the evening, 31°

Scupper 192

Wednesday

To start the day, I continued work on the underside of the companionway hatch, which needed a light sanding and then the first of a couple coats of the same semi-gloss white enamel I used throughout the the interior.

Next, I turned to the starboard coaming, where during the course of the morning I repeated the templating and milling process I’d done to port.  Not really expecting it to work, but figuring it was worth a try regardless, I checked to see if the templates from the port side would work if flipped over for the starboard side, but while the forwardmost piece almost worked, the others clearly wouldn’t, owing to slight differences in the original molding, so I made fresh templates for the starboard side.

As before, I traced the templates onto the coaming stock and cut out and milled the pieces, taking some extra time now to completely finish the edges before dry-fitting the starboard pieces into place with screws.

Now I removed all the pieces from both sides, and did all the final prep to the screw holes in the coaming, after which I vacuumed and solvent-washed the surface.

Down on the bench, I finished as necessary the boards from the port side, which still needed a bit of final cleanup at the rounded edges.  I discovered a method of dealing with cut,milled, or sanded edges and surfaces on the plastic material that helped return it to its more or less original color:  light treatment with heat from a torch.  In this photo, the portion to the right has just been lightly heated with the torch, returning the color and texture back to more of an original state.

With all eight pieces fully prepared, I installed them for real in a bed of sealant.

To wrap things up, I tapped bungs into the screw holes, but held off removing the excess for now to avoid getting any chips into the fresh sealant.

Total time billed on this job today:  6.5 hours

0600 Weather Observation:  26°, clear. Forecast for the day:  Mostly sunny, 44°, then a chance of rain in the evening

Scupper 191

Tuesday

The four loose hatches (cockpit locker lids, lazarette hatch, and companionway hatch) were a bit of a loose end, as their undersides required painting.  This had been on my list for a few days, but I’d not been able to get to it, but now I masked off each hatch as needed and did any final surface preparations, then applied a coat of gray Bilgekote to the storage area hatches, and a white primer coat to the underside of the companionway.

The larger screws I’d used to secure the handrails required 1/2″ plugs, which I’d not ordered along with the plastic material as I’d not thought of it.  However, I found there was no problem using a piece of scrap and a normal plug cutter to mill the plugs I needed, and afterwards I installed them in the handrails to complete the installation.

In the finished overhead in forward cabin, and also in the head, I installed some cover caps over the holes I’d drilled when I installed the handrails.

The last bit of exterior  trim was the coaming caps, which would cover the top edge of the molded cockpit coaming. The shape and curvature of the coamings meant that the trim would need to be installed in a number of pieces, and I chose to make basic plywood patterns first.  I milled strips of 1/4″ plywood to the same width as the trim stock I planned to use, then set about patterning at the forward end of the port coaming, where I needed to scribe the piece to fit against the cabin trunk.  Once I’d achieved a decent fit there, I marked the underside of the pattern a set distance from the coaming on each side.  For this, I found a little stub of a pencil, held flat against the coaming, provided the right distance for my marks; I had to use a short stub at least at this stage because of the interference of the bridgedeck on one side, and the winch island on the other.

With the pattern thusly marked, I removed it to the bench and cut out the shape for a final test-fit.

In this manner I worked my way down the coaming, butting the templates together and allowing the width of the pattern stock to dictate how long each piece could be.  I marked and trimmed four sections of coaming cap template in order to reach the centerline of the cockpit at the stern.

With the patterns complete, I transferred their shapes to the final stock and cut out the pieces, which one by one I fine-tuned, edge-milled, and fit in place temporarily, securing them with machine screws to the fiberglass coaming.  This brought me to the end of the day, but next time I’d repeat the process on the starboard coaming.

Total time billed on this job today:  8 hours

0600 Weather Observation:  25°, clear. Forecast for the day:  Mostly sunny, 50°

Scupper 190

Monday

After some administration and a planning session early in the morning, I had to leave the shop on other business  for part of the  day, but in the afternoon I got back to work on the deck trim, starting with the handrails.  With the sealant cured, it was a relatively simple process now to remove the excess and the masking tape.  I had hoped to bung the screw holes, but ran out of time later in the day.

I removed the dry-fit eyebrow and finalized preparations, including milling my usual little countersinks at each fastener location, then cleaning up the bonding surfaces.  I cut the two after pieces of eyebrow trim to the proper length where I’d marked them, and prepared all three pieces for final installation.

I’d thought about using tape to mark the top edge of the eyebrow position before I’d removed it, but decided against it, thinking it wasn’t necessary.  This was a decision I quickly regretted, as installing the eyebrow in a good bed of sealant turned out to be fussier than I’d anticipated, mainly because it was challenging to find the screw holes in the boat beneath the sealant bead, particularly the first few.  I got it done, but it was messier and more frustrating than I’d anticipated, particularly with the first piece that rounded the forward part of the cabin trunk, but even the shorter side pieces, which I could install at eye level from the staging, proved to be more time-consuming than I’d expected.

Because I wanted to ensure a solid and consistent bead of sealant at the top edge of the trim once installed, I’d used a fairly heavy amount beneath, which required substantial cleanup but ultimately achieved the goal.

With the eyebrow complete, I moved on to the winch islands, each of which required six screws (placed to avoid the anticipated winch base bolt pattern) that I drilled and tapped into the fiberglass beneath before installing the trim in a bead of sealant and bunging the screw holes.

Total time billed on this job today:  5.25 hours

0600 Weather Observation:  32°, clear.  Forecast for the day:  Mostly sunny, 45°

Scupper 189

Friday

Sticking with the idea of replicating most of the original wood trim that had been on the boat, I got to work on the winch islands, which had originally featured wooden tops.  To create new faux wood accents, I started with cardboard templates of the winch islands’ shape, which I transferred to some 1/2″ thick plastic lumber stock and cut out and shaped accordingly.

For the moment, I left these at the dry-fit stage, planning to permanently install them later once I had sealant going for some of the other trim on deck.

I’d cut the winch islands now because I wanted to use the same stock to mill pieces for the eyebrow trim, but wanted to ensure enough of the material for the winch islands first.  Now that those were all set, I milled 3/4″ wide pieces of the 1/2″ stock (in 12′ long pieces) to use for the eyebrow.  With one factory edge, I needed only to round over the cut, second edge to complete the trim before I could set about for the layout and dry fit.

The owner and I had discussed the eyebrow but we agreed that this was an important visual feature of the boat that made it worth installing the numerous screws required to hold it in place, though I planned to use no more fasteners than necessary.

The eyebrow needed to follow the shape of the edge of the cabin trunk forward to roughly the forward set of elliptical ports, after which point it took a different line as it curved forward and around the front of the cabin trunk.  My first layout involved the trim rings for the forward ports, which I held in place and marked at the top edge just to be sure the eyebrow wouldn’t interfere with the trim rings at all.

Afterwards, I used 1/2″ masking tape to mark a line following the edge of the cabin trunk as far forward as the forward ports.

Here again, the flexibility of the plastic material made life easier here, as it would easily make the bend around the curved forward edge of the cabin trunk.  Starting with a point on centerline, I clamped a piece of the eyebrow trim in place, bending it round the sides and adjusting it till it looked right and would blend into the line of the after pieces of the trim.  One twelve-foot section was long enough to span the entire forward part of the cabin and past the forward set of ports and the tape line running aft.

After various adjustments and when I was satisfied with the position of the trim, I used masking tape to mark its top edge around the front of the cabin trunk for later reference.

Removing the clamped-on trim, I cut 45° angles on each end, much as I’d done with the toerail, to connect and incorporate the after trims, then dry-fit the forward trim with screws places 12″ apart.

With the forward piece in place, I could continue with a second piece on each side, running aft towards the cockpit.  I let these run long past the edge of the cabin trunk for now, but planned to end the eyebrow just forward of where the coaming caps would later conjoin the cabin trunk, and duly marked these with tape for trimming once I removed the trim before final installation with sealant.

With the eyebrow dry-fit, I cleaned up the boat and shop and called it a day.

Total time billed on this job today:  6.5 hours

0600 Weather Observation:  38°, mostly clear. Forecast for the day:  Mostly cloudy, showers, 46°

Scupper 188

Thursday

Next on the agenda was the cabin top handrails.  I’d had these made to my specifications when I ordered the plastic wood material.  To prepare the deck for installation, I masked off wide areas on both sides to accommodate the rails.

Starting with the location of the old handrails as a general guideline, I settled on 11″ from the edge of the cabin top to the outside face of the handrails, or roughly 12″ on center from the edge of the cabin, and began the rail 6″ forward of the cockpit.  Working my way forward, I secured the rail temporarily with 1/4″ machine screws in tapped holes, using only a few screw locations as needed to align and bend the rail into a fair curve as it went forward, and keeping it a consistent distance from the edge of the cabin top.  With the rail thusly secured, I went back and prepared the remaining screw locations.

Before removing the rail, I used a sharp knife to cut the masking tape around each base location and, after removing the rail, removed the tape in these areas.  Then I milled the usual countersink at each fastener location.

Belowdecks, I had additional work to prepare for the final installation.  Since the overhead in all areas was covered with the molded interior liner, I needed to remove the liner so I could secure the rail directly to the underside of the deck.  In the main cabin, where the original overhead was in such poor condition that I’d built a new plywood cosmetic overhead to cover it, these additional holes posed no issues for the final appearance of the cabin, so here I used a 2″ hole saw to remove the liner in way of each handrail bolt.  In the forward cabin, where the molded liner was still the finished surface, I used a 1-1/4″ hole saw to drill the holes–the same size as the fender washers I planned to use to secure the rails.

I installed the first handrail in a heavy bed of sealant using 1/4-20 machine screws, nuts, and washers.  The bolts I used were a little long, so later I cut off the excess (seen in photos later in this post).  I also ordered some cosmetic caps to use in the forward cabin and hide (or at least improve) the 1-1/4″ holes.

On the starboard side, I repeated the process of layout and installation.  Handrails are always a fussy and time-consuming proposition, but in this case the installation seemed to take an extraordinarily long time for whatever reason (perhaps only perception), but certainly drilling the holes through the interior liner added significantly to the overall process and made a huge mess in the cabin.   I left the excess sealant that squeezed out around the handrails for removal at another time, once it had cured, since I knew it wouldn’t stick to the plastic rails themselves, and in this instance I preferred to give it time to cure before removal.

To finish up the day, I installed bungs in all the toerail fastener holes.  I’d ordered 3/8″ bungs along with the trim material, and these were straightforward to install, though getting them started in the holes was often a little difficult since the bungs were a friction fit only, since no glue would work with this material.  I found them to be a good snug fit, and it was easy enough to remove the excess with a chisel.

Total time billed on this job today:  8.25 hours

0600 Weather Observation:  32°, clear. Forecast for the day:  Sunny, 43°

Scupper 187

Wednesday

With everything ready to go, it was a relatively simple matter to permanently install the port toerail.  For each section, I applied a heavy bead of sealant to the deck, then installed the toerail with the screws I’d used during the dry fit.  Once each section was secured, I cleaned up the excess sealant, then moved on to the next section.

I moved my operation to the starboard side, and, starting at the stem, repeated the dry-fit process with the starboard toerail, working aft to the transom.  As before, I dry-fit the final section at the transom and let it run wild so I could mark and then trim the final length and shape at the end.  Before removing the rails, I measured and marked for the three drains in the rail, using the measurements I’d determined from the port side to do so.

After removing the starboard rail sections, I milled countersinks at each fastener location, then cleaned and prepared the deck surface for the final installation.  Down on the bench, I marked and cut out the drain openings, and cleaned all the rail sections.

Now I repeated the final installation process with the starboard toerail.

Normally (i.e. using wood), the compound curvature at the transom would have been too extreme to bend a single piece of toerail into place, but in this instance, the flexible plastic wood material was up to the challenge, which streamlined the construction of the taffrail.  I cut a length of the previously-prepared toerail stock to rough length to fit between the ends of the toerails, then, starting at centerline, bent and secured the taffrail blank in place, following my layout line and working towards the transom corners in each direction.  Once the taffrail was secured, I determined the width of the scupper opening at each corner, between the toerails and the new taffrail, and marked layout lines for the taffrail cuts; these lines also dictated the position of the final screws on the taffrail, which I placed the same distance from the eventual cutline as those on the adjacent toerails.

Removing the taffrail to the bench, I trimmed the ends according to my lines, cutting a similar angled profile as on the toerail ends, then installed the taffrail permanently in a bed of sealant.

Total time billed on this job today:  8.25 hours

0600 Weather Observation:  34°, cloudy. Forecast for the day:  Cloudy, slight chance of rain or snow, 38°

Older posts Newer posts