(page 160 of 167)

Nomad 7

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Sunday

Before beginning any other work, I took advantage of the cleanliness of the hull, and of the air in the shop, to mask off the waterline, the only area not yet masked to prepare for the primer later.  Sometime later, once I’d completed the sanding and repair work, I’d protect the bottom and trailer with additional masking against overspray, but that could wait for now.

Continuing work on the transom repair, I water-washed the new fiberglass, then lightly sanded the area as needed to remove rough edges and scuff the surface to prepare for the next steps.  After cleaning up, I applied a first coat of epoxy fairing compound, concentrating on smoothing in the repair with the adjacent surfaces and filling the texture of the fiberglass as required.

Meanwhile, I used some of the leftover epoxy to spot-fill a few minor dings and gouges here and there on the hull.

Total time billed on this job today:    .75 hours

0600 Weather Report:
20°, clear.  Forecast for the day:  Sunny, breezy, 31°

Nomad 6

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Saturday

The original gelcoat on the hull was badly oxidized and faded, but essentially in great condition otherwise, meaning my painting prepwork would be straightforward.  With the decks all masked off from the last work session, it didn’t take me long to get set up and ready to start sanding.

I sanded the hull twice–80 and 120 grits–with a 6″ finishing sander, scuffing the gelcoat and bringing it to the level of sanding required for high-build primer.  It didn’t take long, as gelcoat sands easily and the heavily-weathered surface made the process that much easier.  I sanded everywhere the tool would fit, which was most everywhere, but there were some areas that would require detail and hand-sanding.

Next,  I took care of some heavier-duty sanding at the transom, where the deck/hull joint had separated right in the motor well–a nearly universal condition on production outboards, it seemed.  Someone in the past had sort of caulked this joint, but with the outboard gone it was the perfect time to effect a more lasting repair.   To begin, I sanded away any loose material and old sealant, and ground the gelcoat on the deck edge and transom to prepare for fiberglass, while also rounding over the edge a bit to allow for fiberglass to lay cleanly.

After cleaning the area, I applied some epoxy thickened with silica to the seam, filling any voids and smoothing over the edge as needed.   While the fill was still pliable, I installed a 6″ and 4″ layer of biaxial fiberglass over the seam, forming a smooth and strong reinforcement to the joint.

While the transom began to cure, I went around the boat and hand-sanded as needed to take care of all the areas the sander couldn’t reach.  Afterwards, I cleaned up and solvent-washed the hull to prepare for the next steps, including some minor gouge filling and the continuing transom repair.

 

Total time billed on this job  today:  4.25 hours

0600 Weather Report:
22°, mostly clear.  Forecast for the day:  Partly sunny, 39°, chance of snow showers

Danusia 4

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Friday

Bright-eyed and bushy-tailed, I was back at the windlass capstan first thing.  Nothing had changed overnight, but I continued slowly making progress, though the drum wasn’t going to simply give up till the last inch of shaft was free.  It took another hour or so to finally release the capstan, during which time I bottomed out the puller once again and had to adjust it once more in order to continue.  Not long after this, I found that it was getting harder–not easier–to move the wrench attached to the puller’s screw, and I eventually determined that the screw threads were damaged and galling from the efforts of the past hours.  This was not a high-quality puller.  Fortunately, I had another, larger, one on hand, and with this one I managed to complete the job in relatively short order.  This was a battle won, but the war raged on.

The level of corrosion at the steel shaft housing–which extended from the bronze deck plate through the deck to the gearbox beneath, and through which the bronze shaft turned–was horrific.  It was pieces of this housing that I’d pulled out earlier, when I’d started to move the capstan upwards.  The tragically rusted remains seen here are supposed to be a nice, clean, whole steel  pipe, essentially.

The photos below, stolen blatantly from two separate Ebay listings that I found, show similar windlasses in more or less whole and usable condition, and helped give me–and you, perchance–a better idea of how the components fit together.

Anti-plagiarism and intellectual property compliance note:  if any of these are your photos and you’re unhappy that I’ve reused them here, please let me know and I’ll remove them at once.

I chipped and cleaned away what I could of the corroded mess, leaving behind a sort of cove-shaped remnant that looked a little better, but was no closer to allowing the windlass to come apart into its component pieces.  That little drive pin, seen in the first photo, is what allows the shaft to drive the capstan and it, too, was irrevocably stuck in the shaft at this time.  I didn’t waste much time trying to get it out since I didn’t think it needed to be removed at this point.

Dutifully following along with the old removal instruction from Ideal Windlass’s website, my next chore was to attempt to release the deck plate from the deck, and, dreamily, from the steel housing itself.  I proceeded with as much delicacy as I could given the fairly brutal tasks at hand, all this to try and salvage not just the windlass–still hoping, at this point–but, perhaps more importantly, the deck parts on which it sat.  Releasing the deck plate wasn’t too difficult, with an eventual combination of stiff putty knives, screw drivers, pry bars, and, finally, a long blade on a reciprocating saw to clean out sealant from beneath the slim slot.  None of this had the least effect on the grip between shaft housing and deck plate.  But at least now I knew that the deck plate was free, and that the space beneath might give me the avenue needed should I eventually need to resort to the most destructive means of removal.

windlass6-121815

I turned once more to “The Google” to seek the help of collective wisdom of the Interwebs.    There was little there to help.  I found one other tale of woe with a similar or identical windlass, in which the writer resorted to cutting through the pipe and shaft after jumping through similar (and apparently ineffective) hoops to release the corroded components after consulting the same documentation that I’d been.  I think Danusia’s winch looks far worse, frankly.  Attribution for these photos listed below.

http://themarineinstallersrant.blogspot.com/2014/05/winch-removal-made-easy.html

After a morning’s work, I decided to simply keep soaking the area in question with penetrating solvent over the weekend, and see what happened from there.  I had little hope, but one never knows.

windlass9-121815

in between some other goings-on at the shop, I spent the rest of the day’s time going over several of the upcoming jobs on the work list and assessing the projects in a preliminary way.

Total time billed on this job today:   4.75 hours

0600 Weather Report:
Clouds, fog, 40°.  Forecast for the day:  Clouds, fog, trending toward some sun, highs in the 40s to near 50.

Danusia 3

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Thursday

Danusia was equipped with a bronze (the on-deck portion, that is…mostly) Ideal vertical windlass.  Various measurements and online investigation suggested it was a model A or 3VA, which appeared to be the same thing.  Equipped with a capstan only, the owner reported that the windlass had not worked since he purchased the boat.  It didn’t take much to figure out why:  the belowdecks components, including the electric motor and gearbox, were terrible nightmares of heavy rust, as they were constructed of plain steel that belied the rugged marine-specific appearance of the nice weathered bronze capstan and deck plate above.  Moisture and the leakage that seems inevitable with vertical windlasses, along with the typical neglect that so often afflicts ugly components stuck in out-of-sight-out-of-mind places, had taken their toll on the mechanical side of the windlass.

We hoped to remove the windlass and send it off to the factory to be rebuilt, and to be converted to include a chain wildcat.  No matter what else, however, the windlass had to come off, whether for rebuilding or replacement with something else, as it was useless in its current state, though that green bronze sure looked nice.  So I decided that the windlass removal had to be at the top of the work list, to give time either for it to be rebuilt, or to decide on how else to proceed.

My first order of business was to remove the anchors and rodes and open up the chainlocker as much as possible.  Once I’d removed the rodes, I removed a plywood divider that someone had put in to allow two rodes to fit, and which completely impeded access to the windlass above.  In yet another example of why polyester resin makes such a poor choice for any repair or new work added to a boat after the initial construction at the factory, I pulled the divider–and its tabbing–out with only the smallest hand effort.  In this case I was certainly grateful that it was so easy to remove, though.

With as much room as I was going to get–which wasn’t really enough but would have to do–I inspected the windlass and documented its condition, as well as its wiring.  To improve access and avoid damage, I removed the door to the chainlocker for the time being, and looked around for the windlass solenoid switch, normally installed near the windlass motor and typically an integral part of the required wiring.  None was to be found, and, wondering if it might be hidden beneath a wiring access panel running alongside the v-berth at the overhead. I removed some trim for access, which exposed more of the heavy 2/0 cabling but no solenoid.  Weird.

Armed with some information from the Ideal website, I went about the steps that might eventually lead to removal, starting with removing the cables attached to the windlass motor and one of the deck bolts.  These came off easily, and I marked the wires for future reference and later assessment.

windlassremove11-121715

The removal instructions called for me to remove the capstan drum, which in theory would release the gearbox and motor below.  So I removed the small screw and washer from the top, and sprayed in some penetrating oil, as the instructions kindly suggested that the drum might just be kind of hard to remove.  Indeed this proved to be, and with no immediate movement of the drum possible, I returned to the chainlocker below to work on the four bolts that secured the windlass deck plate to the housing below.

One of these bolts had also been the mounting point for the negative battery cable, and I’d already removed that nut, so I was 25% there.  First inspection of the rest revealed the depressing news that the whole underpinnings were so heavily corroded as to virtually eliminate any hope for finding–never mind removing–some of the nuts, but after flaking off a few pounds of iron oxide and ruined steel, I visually located the second of four bolts–it looked like I might be able to get a wrench on it after all–and, with difficulty and by feel only (as well as the magic view provided by a digital camera held into an otherwise inaccessible space) I eventually chipped away enough heavy corrosion to expose the final two nuts, which were in a tight space between the deck and the housing.

I did manage to get a socket, extension, and ratchet on the second visible nut, and made some progress unwinding it before it became apparent that the carriage bolt at the deck plate was simply spinning, having rounded off the soft bronze edges, so for the moment that was all I was going to get on that second bolt.  At this point still fairly early in the day, I’d barely even considered how or if I’d ever get to the two invisible nuts forward, but even the second bolt was taking substantial amounts of time.  I eventually determined that the nut was galled on the threads, and would never release, but fortunately I’d loosened it enough so I could pull the head of the carriage bolt up and cut it off with a saw from above.  Two down, two to go.

Meanwhile, I returned to the deck side to work again on the capstan.  By now it was obvious that the drum was very stuck on the shaft, and prying it up wasn’t going to work, so I turned to a gear puller, as suggested in the removal instructions.  These usually work pretty well, but I cranked it as tight as I could, well past what I could do by hand (I hammered the end of the wrench–not the little ratcheting one shown in the photo, but a heavier box end wrench that I switched to by this point– in order to turn the puller’s screw), but this seemed to make no difference to the position of the drum.  So I added more penetrating oil, cranked a little more on the screw for good measure, and returned belowdecks to keep working on what I could there.

In this way passed the remainder of the day.  Against all odds–I never would have taken that bet–I found that the two hidden nuts at the forward side of the windlass gear housing were accessible (with great difficulty and by feel only) with a wrench, and actually turned.  The bolts were bronze, which was their saving grace, and I felt an indescribable pleasure at having succeeded at their removal.  I’d already been working through various means of simply getting this windlass off the boat, whatever it took.  The instructions joked about C4, and I wondered if it might actually take something almost that destructive just so we could move forward with another plan.  Getting the bolts removed was a victory, but I was still far from having the windlass off.

In between fighting the tight and miserable access below, I went on deck periodically to beat on the wrench and  keep tightening the puller.  It seemed to be doing nothing for hours, but then suddenly I happened to notice that there appeared to have been some movement.  I’d not seen the drum move, mind you–it wasn’t like it just released and popped off–but the top of the shaft, which had been flush with the inside of the washer recess at the start, was now slightly more recessed, meaning the drum had moved upwards.  This was a positive development, but even so I spent the rest of the day slowly hammering the wrench–and therefore the puller screw–tighter. with great effort.  But at least now the progress was visible, with the drum slowly lifting from the deck.  Once I could get some fingers in there I found one likely cause of the extreme level of stuck-ness:  I pulled out ferrous chunks of junk that were clearly coming off the shaft or housing–from where exactly was not clear, but it was there.  It was very disappointing to see so much plain steel in this windlass.  This work was the unfortunately inevitable result of that sort of construction.

In the event, I kept at it till the end of the day, resetting the puller once after I’d exhausted the travel of the screw.  The tightening of the puller–and removal of the drum–didn’t get any easier as the day wound down, and while I’d made about an inch of progress it was obvious that I probably wasn’t going to get the drum off in the next 15 minutes, so I resoaked the shaft with penetrating oil and left it overnight, hoping perhaps it would get a little easier next time–in any case my arms  would be in better shape for more hammering.

To take the edge off the exhausting day, I took care of one of the easy (and it actually was) tasks from my list.  Someone had overtightened the bolt securing the roller on the main anchor roller, which pinned it tightly and didn’t allow it to roll.  Loosening the nylon locknut on the pin a bit allowed the roller to spin, and also allowed the whole arrangement to slide up and down in the intended slot.

 

Total time billed on this job today:  7 hours

0600 Weather Report:
32°, cloudy with light snow and mixed freezing showers.  Forecast for the day:  Showers, clouds, and more rain later in the day, high near 44.

Aventura 54

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Wednesday

With some #4 battery cable now on hand, I finished up the electrical system, running the cables from the battery storage area to the panel and making up the connections.  I’d wait on purchasing and installing the battery till later, closer to the season.

On deck, a few final tasks remained.  I deemed the varnish work on the coamings complete and removed the masking tape, then installed the genoa sheet winches and the plain teak backing board at the engine well, which I’d held off for now so it wouldn’t interfere with the varnishing.

With that, the work list was essentially complete, and I’d be moving on to other jobs.  I had a small punch list to take care of before the season, including installing and testing a new battery, and supplying and installing the new name (still pending) and registration numbers, and I’d take care of those in due course.

 

Total time billed on this job today:  3 hours

0600 Weather Report:
26°, clear.  Forecast for the day:  Sunny, 40.

Aventura 53

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Tuesday

I spent the morning installing most of the electrical system., running new wiring as needed to the depthsounder (including rereouting the existing transducer cable) , outlet, and bilge pump and making up the final connections at the panel.

I’d hoped to finish up the wiring with the battery cables, materials for which I’d ordered earlier,  but although I waited as long as I could, the shipment arrived late in the afternoon, late enough that I’d already moved on to the varnish work again, so I’d wrap up the cabling next time.

 

Total time billed on this job today:  4.5 hours

0600 Weather Report:
Rain and showers, 40°.  Forecast for the day:  showers ending later and warm, near 50.

Aventura 52

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Monday

With most of the other work now complete, I turned my attention to the interior.  The work list here was minor, as most of the interior–consisting largely of molded interior structures and liners–was in generally good condition, and the owners had no particular plans for truly using the interior.  Earlier, I’d painted the overhead in the main cabin, but we deemed the forward cabin OK as is, other than requiring some cleaning and sprucing up.

Someone in the past had applied some blue plastic tape as a sort of molding or trim beneath the full-length shelves along the sides of the cabin.  The tape was in poor condition and had to go. so I removed it with a heat gun and solvent to get rid of the substantial adhesive residue.

Afterwards I vacuumed everything, then washed the exposed hull and overhead to remove dirt and mildew, which improved the appearance above the shelves and liner. and lightly buffed the gelcoated liners and interior structures to clean them up.    Finally, I reinstalled the newly-varnished teak fiddles  on the long shelves.  The net result was a completely presentable interior.

Getting started on a basic electrical system–required for a bilge pump, 12-volt outlet, and depthsounder–I increased the size of an existing cutout in the step area beneath the companionway, making room for a new electrical panel, which I temporarily installed for now, along with a new outlet in an existing hole to replace an old one that I’d removed before.

electrical5-121415

I installed a new automatic bilge pump to replace the one that was in the boat originally, along with a new hose.  Later, I’d complete the wiring.

In the port cockpit bulkhead, I reinstalled the depthsounder that I’d removed early in the project.

 

I’d wrap up the wiring for these items soon, but for now I had to transition to varnish mode, and apply another coat to the coamings.

Total time billed on this job today:  6.75 hours

0600 Weather Report:
35°, cloudy.  Forecast for the day:  Clouds and showers, around 40.

Danusia 2

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Sunday

Preparing for the work ahead, I set up staging around the boat to make it efficient and comfortable to work on the toerails and other brightwork, which would be one of the main focuses of the project.  With deep draft and fairly tall topsides, I had to cut blocking to raise the planks  a foot or so above the 5′ maximum height of my existing staging supports.   I completed the staging around most of the boat, except for the last sections at the bow since I needed to move some stuff in the shop to make room.

staging1-121315

Total time billed on this job today: 2.5 hours

0600 Weather Report:
30°, mostly clear.  Forecast for the day:  Sun and clouds, 40

 

Aventura 51

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Saturday

I wanted to keep the varnish work going, so with prep already done from the day before it was a quick matter to apply another coat to the coamings.

Total time billed on this job today:   .75 hours

0600 Weather Report:
35°, mainly cloudy.  Forecast for the day:  Mostly sunny, 50

Danusia 1

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Friday

After rearranging the boats already in the shop earlier in the week, I’d opened up one of the bays and now, taking advantage of continuing–yet surely finite–unseasonably warm weather I moved Danusia into the shop so she’d be ready to go as soon as I was available to begin the project within the next couple weeks.  It was a relief to have her inside, as I’d no longer need to worry about the first snowstorm making her repositioning more difficult, or affecting the boat herself.

 

Total time billed on this job today:  1.5 hours

0600 Weather Report:
Foggy, 39°.   Forecast for the day:  fog, clouds, low 50s

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