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    | 3 June 2003
 With a new arsenal of
      industrial reciprocating saw blades from McMaster-Carr, I took advantage
      of a couple free hours in the afternoon to cut out more of the remaining
      interior structure.  With the salon basically empty, I concentrated
      on the head and forward cabin.  A few select cuts with the saw
      enabled me to quickly remove the bulk of the old plywood, which I tossed
      unceremoniously on the foredeck through the hatch, or out into the
      cockpit.  Most of the plywood came out easily, but the incredibly
      thick tabbing on both top and bottom of the horizontal pieces against the
      hull proved to be too tough to deal with at this juncture, so, as in the
      salon, I cut the plywood inside the tabbing.  I even tried my small
      angle grinder, which worked fairly well--if dustily--at cutting through
      the top layers of tabbing.  Unfortunately, the tabbing beneath the
      bunks was simply too tough to pry or beat off the hull, so I abandoned
      this grinding tactic after doing one side.  Later, I'll tackle the
      inevitable and cut out whatever remains.  For the moment, it can
      wait.  I removed the old fiberglass water tank; the only thing
      holding it in place was the surrounding cabinetry.  I also removed
      the remaining portion of the cabin sole; as with the other sections, the
      weak tabbing ripped out fairly easily. |  
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    | I left the forwardmost
      bulkhead--into the chainlocker--in place.  It's in good condition,
      and will probably remain in place even as I begin new construction
      later.  I cut through the tabbing at the top edge, however.  I
      also removed the mast step; the nuts on the two through bolts holding it
      on came right off, but the bolts were of course frozen firmly in place in
      the aluminum step, so I pried it up from the top. As expected, the
      underside looked like wet concrete in consistency--falling apart.  I
      removed the mast beam; its condition was as expected. |  
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    |  The
      cheesy shelves and "chainplate knees" (ha!) for the forward
      lowers in the forward cabin came out with a minimum of fuss; the
      chainplate supports were a complete joke and came out with a light tap
      from my hammer.
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    | Next, I tackled the large
      head discharge seacock.  Earlier, I had determined that there was no
      threaded through hull fitting externally; instead, there was simply one of
      the ubiquitous Pearson fiberglass tubes installed.  Inside the boat,
      the seacock was secured to a fiberglass and wooden fairing block with four
      square-head lag screws (I had also previously determined that these had to
      be screws, not bolts, as no bolt heads were apparent on the
      outside).  Before climbing onto the boat earlier, I had grabbed a
      selection of box end wrenches from the shop in order to tackle these lags,
      since earlier attempts to use some of the lame demolition-quality tools I
      kept in a plastic toolbox on board had ended in dismal failure. 
      Imagining the size of the square bolt heads in my mind, I chose several
      wrenches beginning with 5/8", thinking the heads were at least that
      large.  Of course, they ended up being 9/16", so I had to climb
      down for the proper size.  The four lags came out easily once I
      chipped away some fiberglass and paint that was in the way. However, it turned out that
      the seacock was not free!  Further investigation revealed that the
      fitting must have been set into a bed of wet fiberglass before bolting,
      meaning that it was firmly ensconced in position.  Using a variety of
      chisels, screwdrivers, and other tools, I made an attempt to break it
      free--no dice. |  
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    | Since
      I had my small hand maul nearby, I beat a hole into the head platform to
      get an idea what was going on inside.  I was expecting wet, rotten
      plywood, but what I didn't expect was to find that the cavity inside the
      platform was 2/3 filled with standing water! |  
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    | With that, I called
      it  quits for the day.  With the interior at this stage, it
      didn't make much sense to keep slaving away under the cover of the
      deck.  Most subsequent interior demolition and preparation will occur
      once the deck is removed. |  
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