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Dharma Rose 15

Thursday

Starting once more in the old waste tank, I lightly sanded the new fiberglass over the raised floor at the aft end.  This completed the main structural work in this area.

Using the little templates I’d made earlier, I cut the end pieces for the engine drip pan, using some 3/8″ thick fiberglass.  After test-fitting as needed, I glued the ends to the bottom board with epoxy.

I was looking forward to putting the cabin sole back together and moving forward with other jobs on the boat, so my next step was to prepare 1/4″ fiberglass cleats to re-secure the sole section I’d cut out in order to access the old waste tank.  After cutting the cleats to length as required, I epoxied them to the underside around the edges of the cutout, clamping them in place while the epoxy cured.

Meanwhile, I laid out an additional access hatch in the forward section of the sole.  I chose to locate the opening to take advantage of the cleats I’d just installed in the sole, so that the same cleats would in part support the lid to the new hatch, and sized and located the hatch to allow reasonable access to the space below.  Sometime later, there’d be a teak overlay over the sole and new hatches.

The original fuel tank, located in the starboard cockpit locker, looked reasonably good from above, but regardless of condition we wanted to remove the old fuel for a fresh start, and to better assess the condition of the tank and whether replacement was desired or required.  To gain access to the fuel, I removed the fill hose assembly from the tank,  and set up a siphon rig to drain the fuel into a pair of plastic diesel jugs, and while I baby sat the process I tried to take care of a few other tasks, and made a few steps towards installing the new Cutless bearing, but as the tank drained further I found I had to pay more attention and actually hand-pump a lot since the siphon action faltered.

With all but a few ounces of fuel removed successfully, I removed the remaining fuel fittings, and, reaching up in the tight space behind the tank, the top end of the fuel fill hose.  I removed the strap and a screw securing the tank to the platform, and tipped the tank in order to try and get rid of the last of the fuel inside, as well as start to get a sense of the tank’s condition.  Externally and where visible, the tank was in good condition, and though I couldn’t see the bottom (more on this shortly) I could move the tank enough to feel beneath it and determine there was no sign of rust there.

The tank was slightly larger than the opening above it, which I’d expected since I’d run into it on a similar project 10 years ago, and therefore I couldn’t remove it easily from the space without certain modifications.  For the moment, I held off on further attempts to remove the tank and concentrated on the inside, shining a light through the old vent hole and viewing the inside through the larger fill hole.  The inside of the tank looked quite clean, with just a bit of rust visible where it appeared the original internal tank coating had worn away, but my field of view was limited.

For the moment, the day was nearly done, and before I left for the day I wanted to send the owner the current info so we could start deciding the best course of action.  I thought the first thing I’d do next time was remove the fuel gauge from the tank to give me another small portal inside and help better assess the tank’s condition.

Total time billed on this job today:  7.5 hours

0600 Weather Observation:  0°, clear.  Forecast for the day:  Sunny, 20s

Dharma Rose 14

Wednesday

I got started by lightly sanding the new fiberglass in the repurposed waste tank/bilge area.

To raise the after end of the compartment and allow drainage through the dictated-by-circumstances drain location, I chose to install a flat platform at the proper height and extending forward till it died out against the angle of the ballast pig, which was higher at the forward end and angled aft naturally.  Because the prefab fiberglass panel I planned to use to construct the platform was 24″ in length, I chose this as my arbitrary distance forward, which worked out well in any event.  Starting with a piece of cardboard, then graduating to some 1/4″ pattern plywood, I made a reasonable pattern of the space, which featured lots of bumps and burbles along the sides to keep things interesting.  After various modifications, I achieved a satisfactory fit that was level side to side, and properly angled downwards towards the drain at the aft end.

I transferred the pattern to my 1/4″ laminate panel and massaged the fit as required.  At the aft end, I created a little dip in the panel right in front of the drain to allow the panel to slip just beneath the protruding drain pipe and promote drainage.  I tapered the base of the forward end to bring the panel face closer to the adjacent bilge and ease the transition there.

After final preparations to the bilge and the new panel, I installed the panel in thickened epoxy, using a mass of the epoxy at the aft end to seal and secure the panel there and around the drain tube, and forming lavish fillets along the panel edges where it met the hull at all sides.  At the forward end, I used a trowel to create a broad fillet that properly faired the main bilge surface in with the plane of the new floor.

I had to leave the shop for a while on an appointment, but when I returned I prepared and installed two layers of fiberglass over the new floor and extending up the sides of the bilge accordingly.  Not only would the new floor take care of the drainage issue, but in fact made the whole space better and more useful going forward, as it improved the character of the space and eliminated the worst of the undulations left over from the original construction of the ill-fated tank.

In the engine room, I lightly sanded up the tops of the new support cleats, then patterned and cut a 1/4″ fiberglass platform to form the base of the new drip pan.  At the ends, I made patterns for 2″ tall vertical pieces (no pictures) that would close off the pan once complete.  I’d cut and install the new ends next time.

Total time billed on this job today:  6.25 hours

0600 Weather Observation:  18°, clouds, spitting snow.  Forecast for the day:  Clearing, becoming windy and growing colder, 20s

Dharma Rose 13

Tuesday

The newly-opened waste tank, now becoming part of the bilge for future storage use, occupied most of my time during the day, starting with the usual round of water washing and light sanding to prepare the new fiberglass bulkheads fore and aft, as well as the new fillets and filler I’d applied in the rest of the space, for new work.  The owner and I discussed a plan to bring the after section of the new space up even with the drain pipe to ensure water flow out of the new space as needed, and I’d install that “false floor” a little later, but first I still needed to fiberglass the inside of the space.

After cleaning up, I measured and patterned new fiberglass to glass over the ballast keel cavity and completely close off and secure the space.  To allow continued access to the area so I could work, I broke the space into three sections, each just over 18″ long, and laid out and cut three layers of material, offsetting the seams by 6″ on each layer.  The first layers extended up past the level of the old tank top, stopping just short of the cabin sole, with each subsequent layer stepped back a couple inches.

I disassembled the stack of new fiberglass in reverse order of application, stacking it nearby so I could quickly access the next pieces I needed during installation.

Starting at the forward end and working my way aft, I spent the first part of the afternoon installing the three new layers of fiberglass in the bilge.  As needed, particularly in the forward section, I started with a spot application of thickened epoxy to fill some leftover low spots from the first round of filleting, just to make the surface as smooth as possible and encourage good bonding of the fiberglass to the substrate.  The nature of the space required that I work my way aft sequentially to remain clear of the fresh fiberglass, and the staggered layers I’d set up kept this workable and logical along the way, which kept me moving but otherwise posed no issues along the way.  Before installing the first layer in the aftermost of the three sections, I applied thickened epoxy over a few rougher spots, particularly to help smooth out and cover over some protruding cutoff steel studs leftover from the original construction and installation of the lead ballast pig.  The new fiberglass overlapped the tabbing securing the small bulkheads I’d installed earlier at the ends of the compartment.

I had a few tasks remaining in the engine room before I could finish up the space and think about painting it out, and now, with work in the forward bilge starting to wind down a bit, I could turn my attention back to the engine room, starting with the construction of a drip pan beneath the engine.  To maintain future access possibilities to the bilge beneath, I chose to make a semi-permanent, removable-if-necessary pan, which also happened to keep construction details simple.

To begin, I laid out the location for a pair of cleats along the hull to support the non-load bearing drip pan.  I used 1-1/2″ fiberglass angles to create the cleats, choosing the location more or less randomly an appropriate distance beneath the engine foundations (somewhere between 10″ and 12″).  I angled the cleats down at the forward end to promote ease of runoff collection and cleanup.  With the substrate prepared ahead of time, and layout lines in place, I secured the cleats to the hull with epoxy adhesive, using two dabs of hot glue to hold each cleat in place while the epoxy cured.

Total time billed on this job today:  7.5 hours

0600 Weather Observation:  4°, clear.  Forecast for the day:  Sunny, 20s

Dharma Rose 12

Monday

I removed the glue blocks from the scupper through hull pads, then, after a light sanding, applied a little more epoxy to clean up the fillets as needed, only for visual reasons.

I spent the rest of the day working on the abandoned waste tank, starting with making cardboard patterns of the forward and after ends, so I could close off the openings to the short remaining (and hidden) sections of the old tank fore and aft.  Once I had fine-tuned the patterns as needed, I cut out the shapes from 1/4″ fiberglass prefab sheeting, which I first sanded to remove the smooth factory finish.  (While I was at it, I also pre-sanded a number of other prefab sheets I planned to use soon on other parts of the project.)

At the aft end, I wanted to incorporate a drain into the new compartment.  This meant running a tube through the old section of the tank beneath the battery compartment and out into the deep bilge beyond, and this would require a hole at the aft end of the compartment.  At the moment, there was no access to the back side of this area given the existing hatches and openings, but the owner had expressed an interest in creating a new access hatch directly below the companionway, just forward of the engine room, to get into the forwardmost portion of the bilge there, which space was otherwise basically inaccessible.  As it happened, a hatch in this area was just what I needed to create the thru-drain, so I marked out a square opening of appropriate and about maximum dimensions and cut out the cabin sole with a thin blade.

With some measurements, I could determine roughly where the drain had to exit the bulkhead, so, using my new access hatch, I transferred the measurements and drilled a hole large enough for the 1″ diameter fiberglass tubing I planned to use for the drain. Running the pipe through the space and the new hole at the aft end, I found that I couldn’t get the pipe down to the very bottom of the newly-created space, as the inaccessible small area below the battery shelf still contained the original bottom of the old tank (other than what I’d removed from the forward end), and I saw no reason to take heroic efforts for this little drain, so I compromised by running the pipe  through the new little bulkhead as low as I could get it, which was slightly off to one side and an inch or so above the bottom.  There was no particular reason the new bilge space should collect water anyway, but at least the drain would prevent any serious water build-up.

Before lunch break, I installed epoxy fillets around the two new fiberglass bulkheads, to glue them in place, seal the edges, and provide a good clean basis for tabbing that would permanently secure them later.  I spread some of the epoxy around on the nearby hull to prepare it for the tabbing and smooth any inconsistencies in the old laminate.

First thing in the afternoon, I prepared two layers of tabbing for all the sides of each bulkhead, then wet out and installed the new tabbing in epoxy resin.  I added some light cloth around the mouth of the drain tube to help secure it and close off the opening, not worrying much about any material that protruded as I could sand it smooth later.

Grateful to have the ends of the new compartment closed off, I used the remaining part of the day to prepare the rest of the space for new glasswork by applying fillets and smoothing in new epoxy compound over the sides and bottom of the compartment as needed, sealing up the remaining concrete around the lead ballast keel and easing transitions between the various surfaces.  While I might need to clean up a few areas a second time, this application gave me the basis needed so I could hopefully get the glasswork done next time.

Finally, at the very end of the day, I prepared two fiberglass cleats that I epoxied below the cabin sole inside the new hatch opening, which would allow me to reinstall the hatch  over the opening.

Total time billed on this job today:  7.5 hours

0600 Weather Observation:  10°, clear.  Forecast for the day:  Sunny, 27°

Dharma Rose 11

Friday

I spent the first part of the day working once more on the space formerly known as the waste tank.  After the major dismantling, there remained a need to further clean up the space with solvent wash and additional sanding, mainly to prepare the surfaces for new work.  In the process, I found I could scrape and chip out more of the remaining concrete, and probably could have spent the rest of my days chipping here and there and making progress, but I chose a happy medium, leaving the material that resisted my immediate efforts and seeking mainly to achieve a reasonable clean and sound substrate.

While I was at it, I lightly sanded the interior patches over the abandoned waste system through hulls on the starboard side, and prepared the site leftover from the old waste tank inlet opening (located beneath the v-berth sole on centerline) for eventual patching.

After sanding the surfaces to the extent necessary for now, leaving them relatively clean and smooth, I thoroughly cleaned up the newly-opened space as well as the entire interior of the boat to remove the final residues of dust and debris from the work and allow me to reclaim the space as a habitable area conducive to continued work.

With lingering dampness around the remaining concrete at the edges and aft end of the space, I felt it prudent to leave things for now and let it continue to dry out for a couple days before proceeding with rebuilding and epoxy work.

Meanwhile, back outside I sanded the exterior patchwork over the waste tank through hulls, smoothing and bringing it flush with the adjacent surfaces, then, after cleaning, applied a coat of fairing compound over the patches.

I installed two layers of fiberglass over the abandoned waste tank inlet hole beneath the forward cabin sole.

Now I prepared to install the backing pads for the cockpit scupper through hulls.  The hull was already prepared inside and out, so I solvent-washed the areas as needed and dry-fit the pads to check their fit and alignment with the existing through hull holes.  Since the hull here was nearly vertical, and the pads were heavy, I worried that they would slip while the adhesive was curing, so I carefully aligned each pad the way I wanted it, and aligned with the holes as needed, and hot-glued little support blocks beneath the pads to hold them in place.

I permanently installed the backing pads in heavy epoxy adhesive, which not only secured the pads but also made up the space between the tops of the pads and the hull to account for the curvature.  I cleaned up the excess adhesive and left the blocks to cure fully.

Not wanting to jiggle the boat unnecessarily  and possibly upset the positioning of the backing pads, I chose to spend the remaining afternoon working off the boat, preparing the engine and related parts for installation later.  There are several changes I liked to make to the basic engine to make it not only easier to install for me, but easier to work on going forward.

The cover plate for the raw water impeller was conveniently located on the front of the engine, a vast improvement over the designs of many other engines, but was secured with six tiny screws, making accessing the impeller in an emergency less convenient.  I did notice on this engine that the screws were a little different than in the past, now incorporating a hex head as well as screwdriver slot, which was definitely an improvement over the plain panhead screws that I’d seen on these covers in the past, but still I preferred fasteners that one could undo quickly by hand.  I replaced the original fasteners with knurled stainless steel ones.  These particular fasteners also had a 2.5mm Allen socket, so I included a T-handle wrench that could be used if needed to loosen the screws.  I’d secure that by the impeller once the engine was in the boat.

The fussy little clamps for the throttle and gear control cables frustrate me to no end regardless of what I do, but replacing the slotted fasteners with something a bit more positive always helped with installation.  I like socket-head fasteners (5/32″ in this case) instead of other kinds of screws, and replaced the four screws accordingly.  I also marked the wrench sizes nearby.

I loosened the fasteners where I’d later install the positive and negative battery cables, and marked wrench sizes on the engine nearby.  On this boat, where access to the side of the engine was tight and unnecessarily difficult once the engine was in place, I’d go so far as to pre-install the batter cables before dropping the engine into the boat, but that would come soon enough.

It sure would be nice if these two fasteners were the same size.

On previous installations, I’d found that the way the engine wiring harness plug came secured from the factory got in the way of clear access to that corner of the engine, so now I removed the cable clamp holding it below the throttle control cable bracket, releasing the harness so I could align it as I pleased and, more importantly, clearing access to the engine mount beneath.

A happy installer makes for an efficient installation and a happy owner.

I received the narrow 11-1/2″ mounting center mounts for the aft side of the engine from my engine supplier, who had sent them at my request earlier in the week.  All I had to do was send back the 14″ original mounts from the engine.  Lifting the engine from its shipping crate with my crane, I unbolted the original mounts and installed the replacements in their stead.  These mounts would allow the engine to sit properly on the new foundations in the narrow hull.

During the layout of the foundations, and the adjustment of the after mounts to the narrower width, I noticed on the engine drawings that the narrow mount centers were slightly closer to the aft end of the engine (the reference point being the face of the transmission coupling), about 1/4″ further aft than the 14″ mounts.  This wasn’t a big change, but it was enough for me to note pending arrival of the actual mounts, and also enough that I didn’t want to rely on the template alone in order to physically mark and mount the flexible mounts before engine installation.  I’d marked and drilled the new holes in my template for the narrower aft mounts using the same transverse layout line that I’d originally used for the 14″ mounts, and only afterwards had I noticed the discrepancy on the drawing.  For shame.

Now, I could hold the old (14″) mount directly against the newly-installed 11-1/2″ mount and determine that indeed the new mounting center was just slightly aft of the original (on top here).  It’s always good to confirm measurements physically.

This wouldn’t affect anything I’d done, but I’d either wait to mark the bolting locations till I put the engine in the boat itself, or make another basic template with the correct centers first.

I specified my usual Racor fuel filter for this installation, and, as is my habit, I replaced the drain plug on the bottom of the metal bowl with a valve to make draining more convenient.  In this case, with tight space, I had to use a 90° elbow first to allow the valve to be oriented horizontally, since there wasn’t enough clearance otherwise.  To avoid leaks if the valve handle was operated inadvertently, I installed a plug at the end.

The ball valves I specified for the new scuppers arrived with an add-on zerk fitting to allow lubrication of the ball and help avoid unwanted stiffness over time–a good addition, I thought, particularly on little-operated valves like scupper drains since even good ball valves can become stuck if not well-used.  As directed, I replaced the bronze drain plugs on the two valves with the zerk fittings, which would allow the user to install waterproof grease at will.

Total time billed on this job today:  7.25 hours

0600 Weather Observation:  25°, snow shower.  Forecast for the day:  Clearing, around 30° but dropping in the afternoon

Dharma Rose 10

Thursday

After solvent-washing inside and out the two forward through hull openings awaiting patching, I masked over the holes from outside and installed a thickened epoxy mix flush from the inside, which I allowed to partially cure before applying two layers of fiberglass over the whole area.

Later, once the epoxy had cured enough to continue work from outside, I removed the masking tape and applied three layers of fiberglass to each hole.

While this was going on, and in between steps, I worked on the through hull pads for the cockpit scuppers.  In this case, the owner requested that I not bolt the through hull assemblies all the way through the hull, my normal and preferred method of installation, but that I consider instead blind-bolting the flanges to the pads before installation.  I agreed because I felt this was an acceptable alternative when the backing pad is permanently glued to the hull, as I always did and planned to do in this case as well.

Using the appropriate drill bit, I drilled through the fiberglass pads at each of the three bolt locations on the flange bases.  Then, from beneath, I tapped threads into each hole to accept the 5/16″ bronze machine screws.  I used a hand tap because my drill wouldn’t hold the tap securely enough to mill through the dense, hard G10.  Once the holes were tapped, I milled countersinks in the bottom to accept the screw heads, then dry-fit everything to ensure that I could install the flange over the protruding threads after the fact, since I didn’t want the bronze in place till after I’d glued the pad to the hull later.  I repeated the process with the second fitting, ensuring throughout the process that the flange was properly centered over the hole in the backing pad to later accept the threaded through hull.

Finally, I backed out the screws a bit, then applied some thickened epoxy adhesive to the threads and in the counterbore before re-tightening the bolts securely, all to help hold the bolts from spinning now or later (even though they probably wouldn’t spin with the bolts tightened securely through the tapped holes).  After removing excess epoxy, I left the pads to cure.

Now I turned to the waste tank removal–or repurposing, as it were, since the tank was just a built-in (and poorly at that) void in the bilge above the keel.  After determining roughly what was going on beneath the cabin sole, and how much clearance there was, I marked out a cut line in the sole that would allow me to remove it and access the tank, which was located a few inches beneath with its own fiberglass cover.  The only access at the moment was through a 12″ hatch in the sole.

Using a cutting wheel on my grinder, and finishing the corners with a saw, I removed the cabin sole in one piece.  I’d reuse this later once the work beneath was completed.

With the tank top now fully exposed (at least as much exposed as it ever could be), I used the grinder again to cut away the top close to the hull on each side, after which I could remove the top to expose the tank beneath.  This revealed a mess of brittle, damaged, and loose fiberglass that apparently had once covered the ballast cavity directly below, but had clearly failed long before.  The old tabbing was completely breached along one side, and the disaster of concrete and whatever else the builders used around and above the lead ballast pig was partially visible through breaks in the fiberglass.

I used a comfy supplied air mask whenever I sand, grind, or cut fiberglass in a major way, and I kept the gear on throughout the entire round of work on this tank, so fortunately I was spared whatever biohazard fumes might arise from the tank and the sludgy contents I discovered and now had to remove.  It’s glamorous work, this.  I pulled out loose fiberglass, some sort of maybe-fibrous material from beneath the tabbing (unidentifiable and intermashed with concrete and other contents) and so forth till I’d gotten down to the crumbly loose concrete mess above the lead pig.  I had to bail out the aft part of the tank, which for unknown and clearly ignorant reasons extended aft beneath the battery storage area, through a small screw-in deck plate located in the battery floor.  I’d seal off this ridiculous void later, during reconstruction.

Continuing, I worked to remove the loose concrete, using whatever means worked, including putty knife, chisel, hands (mostly), and hammer.  Most of the material was like wet gravel in consistency, and there was plenty of it.  As I went, I used the grinder and cutoff wheel to further cut back the fiberglass edges where needed, once it had become exposed as I removed the concrete.  In this way, I eventually worked my way down to the top of the lead ballast and/or sound, solid concrete and whatever surrounding it.

After wiping out some final detritus, I used an aggressive sanding disc to remove most of the remaining fiberglass edges where I’d cut, and to clean up most of the area in at least an initial way.  There’d be more prep work ahead, but the worst was done.  There are ways to build tankage safely and successfully into bilges and hulls, but this wasn’t one of those ways.

Total time billed on this job today:  8 Hours

0600 Weather Observation:  16°, clouds.  Forecast for the day:  Sunny, 34°

Dharma Rose 9

Wednesday

To begin, I lightly sanded the new fiberglass on the engine  foundations, smoothing any rough edges and preparing the area for the next steps, including another alignment test for the engine template, but for the moment I continued with some other tasks.

Back to the port chainplates.  To open the tight access panel, I screwed a small handle temporarily to the top and pulled it out without issue, exposing the two chainplate knees and chainplates beyond.  While I could see and reach the chainplates as is, I couldn’t get into the narrow locker opening with both arms and shoulders at once, which I needed to do in order to manipulate the wrenches, so I removed the outer panel from the locker to improve access.

Once more, I was happy to find that, although tight and only just barely possible, it was indeed possible to remove the after (i.e. center) chainplate without removing the main bulkhead, breaking the two-for-two streak from past Contessa 26 jobs.  Reinstallation later would be challenging, but still possible (I thought…I hoped).  It didn’t take long to remove the six bolts from the two chainplates, after which I pulled them up from above decks.

Fortunately, these two remaining chainplates were in similar (good) condition, and with all six now out and exposed I spent some time cleaning them up to remove the old sealant and prepare them for reinstallation, which I’d do a little later once I got the fasteners I needed.

With the new engine foundations in and available for me to stand or kneel on in the engine room, it was the best and most convenient time to remove the old Cutless bearing from the stern tube.  With just a little scraping on the outside of the tube, I exposed the two little setscrews that were securing the existing bearing, and removed them without issue.

From inside, I used a length of steel pipe that just fit within the stern tube to hammer out the old bearing.  After a few tentative taps on the pipe–not wanting to overdo it–I checked outside and was happy to find that the bearing had moved a little, so I proceeded with more vigor as required till I pushed the old bearing completely out.  Afterwards, I measured up the stern tube and bearing and ordered a replacement bearing, along with the new packing box to replace the old grease-filled one.

The next task to take care of while engine room access was as good as it would get was to install the two new  through hulls for the cockpit scuppers.  I’d already ordered and received the new bronze hardware.  I discovered I’d mistakenly ordered through hulls with a hose barb instead of the plain threaded versions, so that would delay final installation slightly while I waited for the replacement order, but in the meantime there was plenty I could do to prepare, starting with the fiberglass backing pads for the flange bases.  I cut and shaped these from 3/4″ G10 leftover from the engine foundations.

I’d already prepared the hull at the scupper openings inside the boat, but outside I sanded away the paint and old sealant from around the holes, and, since the old holes were a little undersized, used a drum sander to open up the holes as needed to fit the new through hulls.

While I was at it, I prepared the two old holding tank through hull openings on the starboard bow for patching, grinding out circular dish-shaped areas around each hole so I could patch with fiberglass.

Total time billed on this job today:  6.75 hours

0600 Weather Observation:  15°, clear.  Forecast for the day:  Sunny, 30°

Dharma Rose 8

Tuesday

The epoxy work on the newly installed foundation platforms required light sanding to clean it up and prepare for the next steps.

Next, I made basic paper patterns of the tabbing needed to secure the foundations to the hull–top and bottom on both sides.

After finalizing the patterns’ shapes and trimming the excess paper, I used the patterns to cut three layers of 1708 fiberglass for each set of tabbing.  I slightly stepped back the tabbing size on the areas on the hull, mainly for a nicer appearance when all was said and done, but let all the tabbing run to the edge of the patterns where it would rest on or beneath the foundation platforms themselves.

After final preparations and cleanup, I installed all the tabbing in epoxy resin, starting with the bottom sections, with their more difficult access, and continuing to the top sections.

Leaving the new fiberglass to cure, I changed directions and started work on accessing and removing the chainplates for inspection and to determine whether replacement or other work would be required.  From past experiences, I knew that I’d probably have to remove the galley bulkheads on each side in order to gain access to the center (main or upper) set of chainplates, which knees tended to be uncomfortably close to the plywood bulkheads.  This would require various dismantling and disconnecting of things, including wiring bundles, miscellaneous and sub-cover panels within the lockers (particularly on the port side opposite the head), and more, so I set about the task.

Starting on the “easier” starboard side, I began by removing the water fill line, and then removed the longitudinal cover panel behind, exposing the two forward sets of chainplates on that side.  The aftermost set was accessible separately through a small locker above the galley and posed no particular access problems.  I found a big rodent’s nest behind the panel.  The chainplates looked good where visible, but since problems can occur where the chainplate runs through the deck slot, I proceeded with removal.

Removing the forwardmost chainplate, with the ground wire attached, posed no problem, though one of the nuts was galled and eventually broke the bolt during removal (which was a preferred outcome to having to cut or otherwise remove the bolt).

At the after location (i.e. the middle, or upper, chainplate) in this case I found that I could just slip a wrench into the narrow space between the bulkhead and upper chainplate in order to remove the nuts, so for the moment at least I didn’t have to remove the bulkhead.  I hoped I’d be able to reinstall the nut similarly through the narrow space, and would by all means try rather than go through the effort of removing the bulkhead.

I removed the aftermost chainplate from the galley locker without issue, and from on deck removed all three plates, which came forth reluctantly thanks to whatever sort of bedding compound was around the slots.

Down on the bench, I scraped off the excess sealant, and was pleased to see that all three chainplates were in apparently excellent condition with no corrosion observed.  With some minor cleanup they could go right back in, I thought.

Turning to the port side, I removed the screws securing the longitudinal cover panel over the two forward sets of chainplates, but the panel was so tight in its place that I couldn’t budge it to pull it out, with no room even to pry it from an edge.  It was growing late, and I decided that continued efforts to remove the panel would be best handled fresh in the morning, so instead I removed the more easily accessible aftermost chainplate above the galley sink, which was also in good condition like its counterparts to starboard.

Total time billed on this job today:  7.5 hours

0600 Weather Observation:  32°, clouds, spitting snow.  Forecast for the day:  Sun, 29°

Dharma Rose 7

Monday

Now that the rough templates for the new engine foundations were in place, and the basic positions of the four flex mounts marked accordingly, I removed the engine template, and used one of the mounts to mark outlines at all four locations, using the rough marks I’d made to align the mounts.   This gave me what I needed to I could plan the final shape and size of the foundation platforms, leaving ample room around the mount bases to allow for position adjustments, while eliminating excess material where possible.  Then, I removed the rough pine templates from the boat and down to the bench so I could prepare the actual pieces.

I sanded off the smooth, shiny factory surface from the sheet of 3/4″ G10 I’d purchased for the foundations, then cut out the pine patterns along the marks I’d made earlier, and used these to mark and ultimately cut the fiberglass.  Then, I marked the rough shapes of the bevels on the outboard edges of the foundations, where they met the hull, and shaped these areas as needed.

After a test-fit, I cleaned up the cut edges and rounded the edges and corners of the new foundations.

I wanted to be sure that the final foundations didn’t end up any higher than needed; if anything, I preferred they ended up low, since it was easier to add height than deal with an overage.  I also had to leave room for the fiberglass tabbing that would ultimately secure the foundations, so I made new reference marks about 1/4″ vertically below the originals, and I’d align the fiberglass foundations with these new marks.

Using a level to ensure side-to-side alignment, I tacked the foundations in place along my reference lines, adding a little support beneath to help support the weight.  I started with the starboard piece, then, once it was set, prepared level braces across to the other side so I could install the port piece properly according to the first piece.

Once all the glue set up the arrangement was quite rigid, and I removed the top cross braces and levels to clear the way for the next step, which was to replace the engine template and shaft string to check, once more, that the new foundations were where they needed to be.  Keeping in mind that the platforms were about 1/4″ lower than their final designed height, I confirmed that the position and basic alignment was in keeping with expectations.

Finally, I applied epoxy fillets to the top edges to secure the foundations permanently and fill small gaps at the edge.  I chose to leave the underside of the platforms for later, once I could clear the braces beneath and improve access all around  I used more of the epoxy to smooth out the slots leftover from the original foundations and otherwise prepare the overall area for fiberglass, which would be the next step.

Total time billed on this job today:  5 hours

0600 Weather Observation:  32°, clear overhead with fog.  Forecast for the day:  Clouds and sun, low 40s

Dharma Rose 6

Friday

I had a short day planned, but wanted to make good progress in the engine room first.  I planned to build the new engine foundations from 3/4″ G10 composite sheeting, an almost foolishly strong and hard fiberglass and epoxy product that’s overkill for almost every proposed situation, but provides the durability and piece of mind one might consider useful in something like an engine bed. G10 is also heavy and difficult to work, and therefore machining tasks are best kept to a minimum.

To template the position and shape, of the new foundation pieces, as well as continue to check the overall engine alignment and proposed placement accurately, I chose to build basic mockups of the foundations from some scrap pine lumber that was light as a feather after more than 12 years aging in my shop, and easy to work to boot.

With the engine template suspended in the engine room over the taut shaft alignment string, I fine-tuned the position as needed, getting it as level and accurate as possible.  Because of the suspension’s propensity to sway the whole template a bit aft, I used a handy bitter end of  string to pull the template forward to my desired position, and checked and adjusted again till the template, still level, allowed the string to pass through the centers of the forward and aft template holes.

To help with basic positioning throughout the process, I used a metal straightedge to transfer and make reference marks from the centers of the mounting studs to the sides of the engine compartment.   Then, with a small steel rule held tightly to the bottoms of the forward mounts, I transferred their heights to the hull side, making tick marks on each side.   I re-checked the level each time, since the whole template was easily knocked out of position in its dangling lines.

The tight confines of the compartment and the way the engine template hung over the curvature of the hull prohibited clear access to the after mounts, so to help mark their position I first removed the two forward mounts, re-checked level and position, then managed to get some rough marks aft where the mounts contacted the hull.  I couldn’t manipulate the little ruler and pencil like I did forward, but in this case the after mounting bases just touched the hull at their outboard sides, which was enough for me to get reference marks that would serve the required purpose.

Once I had all four mounts’ locations marked, I removed the template and string for now to open up access to the space, and darkened the four tick marks with a pen before connecting them on each side with a flexible steel rule; the lines turned out more or less straight since the hull curvature here was transverse more than longitudinal.  These lines gave me the reference for where the flat engine foundations needed to be.  To help with overall dimensioning, I made rough marks to correspond with the flex mounts’ positions and lengths on each side.  I didn’t want the new foundations to be any longer than strictly necessary, to aid all future access to the engine and the space, but also needed to account for some necessary wiggle room to allow the engine to be properly positioned fore and aft as dictated by the vagaries of the installation when the time came.

From scrap pine board, I made two pieces 24″ long and whatever its width was (about 6″).  The width at this stage was unimportant, and the length was just a starting point; similarly, the inelegant ends would eventually be massaged into something more situationally- and aesthetically appropriate.  I cut as steep a bevel on the outboard side of each piece as possible, and knocked off the after corners of each board so that the two sides together wouldn’t interfere with one another.  After a couple brief test fits and some minor reshaping with a sander to allow the templates to fit more or less closely against the hull on each side, I tacked them in place with some hot glue along the lines I’d marked earlier, striving to force them level in the process.

The starboard forward end ended up a bit higher than I’d planned, accounting for the slight off-ness [sic] of the level, but that didn’t matter for these purposes, as my goal, other than checking the basic positioning for later, was just to provide simple templates from which I could more easily and efficiently shape the granite-like G10 material later, and the minor discrepancy didn’t affect the shape of the mockups (nor of the final fiberglass) at all.  The time for ultimate accuracy would be during the final and permanent installation later.

With the rough cutting complete, and the boards tacked in place, I glued the little triangular offcuts from the aft end beneath each side to help support the boards from beneath, again holding the inboard edges of the board level while I did so.  Afterwards, I restrung the alignment string from the shaft, this time working just a little harder to ensure its accuracy.

Test-fitting the engine template again, I immediately saw that I needed to provide clearance at the aft end for the down-hanging plywood board that provided the shaft centerline mark (and also happened to correspond to the transmission width and depth for this engine), so I carefully cut out some extra material with a handsaw to allow a proper fit.  Then, I installed the template and made whatever adjustments were necessary to properly position it.

I was pleased to see that the engine fit well on the mockup foundation, particularly at the difficult and tight after end.  I was running out of time in my self-shortened day, but before knocking off I made reference marks as much as possible to show the positions of the four flex mounts; again, reaching the after mounts was virtually impossible given the shape of the template–which, we must not forget, represents the overall size of the largest dimensions of the engine and transmission together, and is not necessarily representative of the actual shape thereof–but I managed to get some scribble marks in there that would be enough to allow me to determine where to mark and cut the foundation mockups to their final desired shape next time.

Total time billed on this job today:  3 hours

0600 Weather Observation:  25°, mostly clear.  Forecast for the day:  Mainly sunny, 40°

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