(page 88 of 166)

Scupper 216

Thursday

The cherry trim piece I built to accommodate the owner’s selection of two small flush-mount lights was complete now, and I turned to the final installation.  Each of the two lights fit in the holes I’d prepared in the trim, and I secured them with screws before installing the trim rings.

I’d routed a wire channel on the back side of the trim, and I spent some time at the bench wiring up the two lights and conjoining the wire leads to a single wire pair that would exit the trim and eventually connect to the circuit I’d run into the engine room for these lights.  To accommodate the larger butt connectors needed to connect both lights together, I had to ream out a portion of the existing wiring channel to make it deep enough for the connectors to remain flush.  I used dabs of hot glue to hold the wiring and connectors in place within the channel so they wouldn’t move during installation.

After some layout, I installed the trim with the lights above the galley, securing it to the overhead with screws.  I planned to lead the wiring directly aft to the bulkhead, as I knew there was an open space between the bulkhead and the after bridgedeck molding through which I could lead the wires.  I chose this because it was the most direct and (irony to follow) easiest route for the wires given all the other complications in the mounting location.  I laid out a line perpendicular to the light trim and leading aft to the bulkhead to show where I needed to drill a hole for the wiring (not shown here).

This is where the job got fun.  To drill my hole, I first removed the trim along the upper aft edge of the bulkhead, then drilled a hole through at my mark.  What I’d not counted on was the fact that the actual bulkhead didn’t extend quite all the way up, so there was a small gap hidden behind the beadboard.  This meant that the hole, drilled at the extreme edge/corner of the bulkhead to hide it behind my wiring trim, didn’t come out cleanly or even in the proper orientation, and I had a bear of a time snaking the wires through.  There was no direct, or even indirect, access to the back side, and after various failed attempts I had to open up the hole more than I wanted in order to have a chance at accessing the space for my wires.  At great length I eventually managed to get a tiny, relatively stiff solid copper wire I had on hand through the hole and far enough down into the narrow, tall gap behind so I could finally grab it with a long grabby tool.  Once I had the messenger through, pulling through the wire pair from the lights was straightforward enough, but this had taken inordinately long.

This left me with a larger and uglier hole than I had planned on–a bit too large for the trim to cover properly, so I’d have to patch the hole and repaint the area.  But what mattered for right now  was that the wires were in place.

I temporarily installed the new wiring trim after cutting it to length, and reinstalled the aft bulkhead trim that I cut to accommodate the wires and trim.  So this would be ready to quickly install later, but for now I removed the trim and, after masking and other preparations, filled the excess hole in the bulkhead with an epoxy mixture.

Working from the port cockpit locker, I finished up the wiring connection for the galley lights, securing the new hard-won wires to the end of the circuit I’d run in for the purpose.

With only an hour or so left in the day, I decided to get ready for the final panel wiring and installation.   To accommodate a couple higher-draw appliances on board, namely the electric toilet and the potable water pump, I needed to replace a couple of the stock 15-amp circuit breakers in the panel with larger ones:  25-amp and 20-amp, respectively.  I decided to put these larger breakers at the bottom of each panel, so I disassembled the panels as needed to remove the old breakers and install the new.

In the electrical locker, I chose a location for and installed a large negative distribution buss, so which I’d install all negative wires.  To begin the process, I cut to length and terminated the yellow wire leading to the panel from the house battery location and negative buss there.

To secure the locker cover and electrical panels while working on the final wiring, I made up a couple supports from spare wire, which let the panel hang in an open position with good access for wiring now, and maintenance later.  I looked forward to making order from the wiring mess starting next time.

Total time billed on this job today:  8 hours

0600 Weather Observation:  12°, clear. Forecast for the day:  Sunny, 22°

Scupper 215

Wednesday

I began the day in the varnish room, where I lightly sanded the table parts and applied a coat of gloss varnish to the base and the visible side of the table leaves, locker lid, and support brackets.  This brought all sides of all pieces up to at least 4 base coats.

A few weeks back, after finding that the LED diffusers I’d bought for the underdeck lighting in the forward cabin and main saloon weren’t suitable for my application, I ordered different materials for the purpose–aluminum channels and diffuser covers–and now I could finally return my attention to these lights, starting in the forward cabin.  The channels were longer than I needed for the space available in the forward cabin, so I cut two channels to length.  These came with two kinds of end caps:  solid caps for the blank end, and caps with a hole for wiring at the other end.  In order to secure the channels in place, I drilled pilot holes and countersunk for flat head screws.

Beginning on the starboard side, I installed the channel beneath the sidedeck with 1/2″ screws.  I kept the channel near the outboard side of the space, and started them just forward of the reading lamps I’d installed earlier.  Once the channel was in place, I installed the waterproof LED light strip, which I cut to length as needed to fit within the channel.  This strip was self-adhesive.  I led the wires out the aft end of the channel, through the end cap, and then through a hole I drilled in the liner to accept the wiring and a short length of flexible conduit.

To finish off the first of four installations, I installed the diffuser cover over the channel–a simple snap-in installation–and made up the wire ends to a wire pair I’d already led forward into the space.

I repeated the process on the port side.

Moving aft, I repeated the installation on the starboard side aft of the electrical locker.  Here, I could butt the end of the channel up to the small bulkhead, through which I drilled a hole for the LED wiring.

On the port side of the main cabin, there was room for a full length of the aluminum channel.  Here, to avoid interference at the aft end with possible deck hardware, I let the channel run out towards the inboard side of the space beneath the deck as it ran aft, keeping the outer aft section clear in case I needed to cut access through the liner for the jib track or stanchion base when the time came.  I extended the wiring and led it through the locker and up to the lighting terminal block I’d installed earlier, finishing up the connections there.

To round out the day, I finished up the bulk wiring runs. leading four circuits and a VHF cable from the panel area, through the forward part of the boat, and back into the bilge in way of the mast compression post, through which these wires would ultimately lead.  These circuits would service mast lighting as well as a couple additional interior fixtures based off the compression post.  For now, I left ample length at the bilge end for final connection later, and, after securing the wires through the starboard lockers alongside the existing wire runs,  at the panel end left sufficient length for final connections there, which could start happening soon now that all the basic wires for known circuits were finally in place.

Total time billed on this job today:  8 hours

0600 Weather Observation:  25°, light snow. Forecast for the day:  Light snow, maybe an inch forecast, 32°

Scupper 214

Tuesday

I finished up work on the electric bilge pumps’ installation, beginning with where I left off in the engine room at the new diaphragm pump.  I installed a bronze suction screen on the end of the hose leading to the bilge, then secured the hose as needed from the bilge, through a small intake filter, and to the pump itself, through the new holes I’d prepared in the small divider bulkhead.  Then, I led the discharge hose from the pump and aft through the engine room as needed, securing it with rubber-lined clamps along the way.

At the transom, where I’d recently installed the outlet through hull, I finished off both hose runs from both electric pumps, starting with the larger hose from the forward pump.  I led this hose in an arc to the underside of the deck to minimize backflow potential through the hull fitting, and then secured the smaller hose from the everyday diaphragm pump to the larger hose to keep it out of the way as well.

Armed now with new fasteners, I turned to the mast reassembly, and spent the remainder of the day reinstalling most of the hardware, except for the masthead casting, which I left off for now till I could run in the wires needed.  For all the fasteners, I treated the threads with Tef-Gel to reduce future corrosion problems.

I reassembled the boom ends, and installed a bail at the aft end for the main sheet.

Finally, I re-led messenger lines for the halyards, leaving things ready for the riggers when they returned later in the week.

Total time billed on this job today:  7 hours

0600 Weather Observation:  11°, mostly clear. Forecast for the day:  Mostly sunny, 32°

Scupper 213

Monday

Over the weekend, I finished up the base coats of varnish on the various cherry trim pieces, and to start the day now I applied a final coat using satin varnish.

In the main bilge near the galley, I finished up the installation of the new centrifugal “emergency” pump and automatic switch.  Now that the pump bracket was secured to the boat, I snapped the pump back in place and, working from the engine room, led in a length of 1-1/8″ hose, which I connected to the pump.  For now, I left the other end of the hose wild in the engine room pending final connection to a new through hull.

I ran the wires up through into the locker beneath the galley, where I eventually secured them to a terminal block held up out of the way on the inboard side of the locker, and connected the wire leading back to the panel to the other side of the terminal.  This provided a straightforward way to make up the connections between the pump and switch to allow manual or automatic operation; I’d finish up the wiring at the panel end a little later.

In the engine room, I continued work on the second, main pump:  a diaphragm pump designed for routine and complete dewatering of the bilge.  I’d already installed the bracket and automatic switch in the bilge, and now I led the switch wires through flexible conduit and along the path of some other wires already in place in the engine room and over to the starboard side, where I chose to install the diaphragm pump on a shelf at the outboard side of the engine room.  I wired up the pump and switch to the cable leading to the panel through another terminal block.

To lead in the suction and discharge hoses for the pump, I drilled a pair of holes through the divider at the side of the pump, in line with the two ports on the pump itself.  I found a plywood void in one of the holes, and while the divider was non-structural, I chose to fill the void with thickened epoxy, and treated the exposed plywood in the second hole as well.  I left the new epoxy to cure overnight.

To accept the discharge ends of the two electric pump hoses, as well as a forthcoming manual bilge pump, earlier the owner and I had decided to install a pair of through hulls, one on each side of the counter:  one on the starboard side for the two electric pumps; and a second on the port side for the manual pump.  Using the location left over from the old discharge through hull (which I’d removed and patched much earlier) on the starboard side as a guide for the new locations, I drilled a pilot hole from inside the boat on each side in the desired location, then, from outside, drilled the larger holes required to accept each through hull.

After cleaning up the drill spoils and around the holes themselves, I installed new bronze fittings at each location.

On the port side, I chose a barbed through hull that would later accept the 1-1/2″ discharge hose from the manual bilge pump.  For the starboard fitting, I needed a normal threaded through hull so I could install a bronze tee fitting for the two discharges from the electric pumps:  1-1/8″ from the centrifugal pump, and 3/4″ from the diaphragm pump.

Total time billed on this job today:  7.5 hours

0600 Weather Observation:  5°, mostly cloudy. Forecast for the day:  Mostly cloudy, 28°

Scupper 212

Friday

It was a quiet day, with important yet largely non-visual progress at the shop, aimed mostly at setting things up for the work to come in the next weeks.

To begin, I cleaned up as needed from the mast painting operation,putting away the painting supplies and equipment so I could get that side of the shop back to normal.  I left the freshly-painted spars alone for now for some additional cure time, but soon planned to move them to the side so I could reclaim the bay for a vehicle that I stored there, but had moved out for the painting operation.

Completing the mast painting was a significant milestone, and I wanted to finish its reassembly as soon as possible so the riggers and sailmakers could get back to work on their respective jobs, so to that end I went through all the mast hardware, noting the fasteners required so I could order replacements as needed, which I did once I’d checked existing stock against my scribbled notes.

Next, I turned to the new bowsprit, which I’d glued up some time before.  Now I removed the clamps, scraped off the excess epoxy, and milled the blank to the final dimensions, using the original as a guide:  10-1/4″ wide and 84-1/2″ long.

I finished up the blank by rounding the corners as appropriate, and sanding the whole thing smooth.  Since the bowsprit would remain bare, this completed the initial construction, and I could soon prepare to install it.

Afterwards, I lightly sanded, cleaned, then revarnished the new cherry trim pieces and the cabin table.  I’d recently moved an unrelated finishing project out of my little finishing room, and now I spread the table pieces out there to allow the refinishing process to go on over the coming days, as the numerous two-sided pieces would require extra time to varnish completely.  I planned to finish up the cherry trim over the weekend, so I left them in the main shop for the duration.

Total time billed on this job today:  7 hours

0600 Weather Observation:  30°, cloudy. Forecast for the day:  Cloudy, 42°

Scupper 211

Thursday

The mast painting remained my main focus, but since there was little prep required before I could apply the gloss topcoat, I decided to use the morning to take care of some smaller jobs before continuing on the mast.

I wanted to keep the varnish work going on the cabin table and various trim parts that I’d started before the holidays, so to get going I lightly sanded everything and, after cleanup, applied a second coat of gloss varnish to all surfaces.

On my new bracket, I installed one of the automatic switches, along with the base for the centrifugal bilge pump, using short screws tapped into the fiberglass to avoid penetration through the bracket itself.  I aligned the bilge pump base so that the outlet of the pump would face the desired direction once the bracket was installed.

Inside the boat, in the bilge opening near the galley, I chose the location for the bracket and removed paint from the bottom of the bilge so I could epoxy the bracket in place.  This location allowed relatively easy access for wiring and servicing the pump and switch in the future, and the bracket design intended for the wiring to be easily led up and away from the bilge water, where I could make all connections in a dry location.There was room on each side of the bracket to allow free passage of water towards the aftermost part of the bilge in the engine room, which was the deepest part and where I planned to install the switch and suction for the everyday “nuisance water” pump.

To that end, I installed the second switch on the bracket I’d made for the engine room space, then installed the bracket to the aft edge of the engine platform with a screw.  I’d hoped to use two screws, but the shaft above prevented accessing the second screw location.  The screw only holds the bracket upright, and there’d be no pressure on the installation, so the single screw was ample in any event.  I noted earlier that I’d mistakenly built the bracket backwards from my intention, but this actually worked out well since now the switch was well-protected on the forward side of the bracket, leaving plenty of room behind for the manual and nuisance pump suction hoses.  Final wiring runs and plumbing connections would happen in the near future.

After an early lunch break, I turned to the mast painting for the afternoon.  The anti-corrosive metal primer I chose for the spars didn’t require any further primers before topcoat, nor did it require sanding for adhesive purposes (within the specified time frame, which was six months after application).  The surface as applied was smooth and without obvious flaws, but I went over the spars briefly with a Scotch-Brite pad just to knock down any minor surface  texture.  After solvent-washing and other final preparations, I spray-applied three coats of the Alexseal snow white gloss topcoat I used elsewhere on the boat, leaving the new coating to cure overnight.

Total time billed on this job today:  6.5 hours

0600 Weather Observation:  20°, mostly clear.  Forecast for the day:  Partly sunny, 37°

Scupper 210

Monday

Before continuing work on the spars, I wanted to come up with a way to suspend the spars between the sawhorses so they would be free and clear for primer and paint.  The boom was no issue:  it was small and light enough that I figured I would just hang it from small line led through some screw holes at each end, and to the saw horses.  This would allow the boom to swing, which I wouldn’t want for sanding, but for spray painting it would work fine.  For now, I left the boom as is pending final sanding.

The mast was tougher, as it was too heavy to hold with small line, and in any event there weren’t enough holes at the ends to secure the line even if I’d wanted to do it that way.  I could have built wooden inserts that fit inside the mast, and then used those to secure it to the sawhorses, but that was frankly more work than I felt was necessary or desirable.

After a failed attempt to build a simple internal support with a stick protruding to the sawhorse–this failed because the wedge inside the mast didn’t hold as I’d hoped, and the stick ended up looser than intended–I came up with a plan to secure a square piece of hardwood (actually a leftover stair baluster) inside the mast, with screws through the inside of the mast track.  There were already holes in place at the bottom of the mast that I could use, but I drilled two holes as needed inside the track at the top of the mast.

When suspended between the two sawhorses and clamped at both ends, this held the mast solidly with the track facing down, which is how I wanted it for ease of painting.  I arranged the mast kitty-corner in the shop as needed to accommodate its length and the sawhorses, while still leaving just enough room for me to maneuver around at the masthead end (where the sawhorse was almost at the doorway to the woodshop) as needed so I could work on all sides of the mast.

I sanded the epoxy filler in the screw holes left over from the spinnaker pole track; this came out well and didn’t require any further work.

Everything was set up as I needed it, so next I sanded the mast and boom a final time, this time with 120 grit paper.  Although there was no visual indication that the previously-sanded spars had oxidized over the couple days since their last sanding, this final round of sanding would ensure clean, bright metal to encourage the best possible adhesion of the anti-corrosion metal primer.  The finer grit also brought the prepared surface to the desired level of roughness (or smoothness) for the primer.

With metal, one can’t use rags for solvent-washing after sanding, as tiny fibers might catch in the rough metal and create a tiny wick that could exacerbate primer failure and corrosion later, so all I could do at this stage was vacuum the surfaces thoroughly to remove dust.

Afterwards, I strung up the boom to hang it, bottom side up, from the two sawhorses.  I added vertical pieces to raise the boom’s height and make it easier for me to paint.

After final preparations and getting the paint ready, I spray-applied two coats of the protective anti-corrosion metal primer to the spars.  As always, spraying rendered the shop otherwise uninhabitable, so I called it quits for the day.

Total time billed on this job today:  6 hours

0600 Weather Observation:  26°, cloudy.  Forecast for the day:  Cloudy, chance of snow late, 27°

Scupper 209

Friday

I spent the day preparing the mast and boom for primer and paint, beginning by stripping the old paint off the spars.  To do this, I sanded with 40 grit discs, removing the old paint and primer and abrading the aluminum beneath.  With the mast resting on saw horses, I worked my way down one side from masthead to base in this manner.

Once I’d reached the bottom part of the mast, I was faced with a decision.  Despite repeatedly soaking for a couple weeks the six remaining bolts holding the spinnaker pole track to the mast, I had come no closer to removing them cleanly.  In fact, they were so stuck in place, even with half a can’s worth of penetrating oil, that each time I tried to remove the screws, I simply shattered my driver bit in my impact gun.  It was clear those bolts were not going to budge.

I seriously considered leaving the track in place and working around it for the paint, and almost certainly would have done so if I’d not been able to remove all but six of the screws.  But it seemed so close to removal, and it would be better for the mast prep and paint if I could remove the track entirely–even though at this point it meant destroying the track–so eventually I decided to remove the track through whatever means.

Almost immediately, I rued this decision, as I found the track was extremely difficult to cut through, even though it was aluminum.  It was a heavy, 1-1/4″ T-track that dated to the spar’s original construction. I tried grinding through the heads of the screws, but they were stainless steel and extraordinarily tough, and in any event the threads were still well welded in place through the aluminum track itself.  I tried using the grinding wheel to cut through the track and screw studs, but this was difficult and dangerous, and I didn’t want to risk damaging the spar.  I tried using a reciprocating saw, but again, the track was too difficult to cut through, and too time-consuming.  Ultimately, I employed some combination of these techniques, along with a pry bar to bend and break away the track in sections, finally exposing each screw so I could then grind them flush.  The track was tough enough that it broke the end off my flat pry bar that I was using to help bend and break the track at the cuts I’d made.

With the track successfully–finally–and cleanly removed, I turned the mast over and sanded off the paint from the other side.  The spar was in good condition beneath the old paint, with some minor surface etching here and there where the old coating had failed long before.

Next, I turned to the boom, beginning by removing the end caps and remaining hardware.   This was easy and quick since the riggers had already had these off in order to remove the bits of the old outhaul arrangement and plan for the replacement.  Once the hardware was gone, I set to work sanding away the old paint and primer.  Once I’d reached bare, white (silver) metal and finished the sanding with the 40 grit paper, I switched to 80 grit and sanded the entire boom again, to get closer to the final surface I’d need before applying the corrosion-resistant primer I planned to use.  The bare aluminum would oxidize rather quickly, so I planned to finish the sanding with 120 grit on the day of the primer application, which would finish the spars’ preparation and clean the metal one last time just before the primer.

With the boom complete through 80 grit for now, I returned to the mast and sanded it with the 80 grit as well.

To round out the day, I decided to fill the old screw holes left from the spinnaker pole track, so I used a countersink to bore them out a bit, then, after cleaning with solvent, filled the holes with an epoxy mixture, choosing to leave the fill high in the hopes that I could do the job in one round only.  The old bolt studs at the bottom of the track had ended up flush with the mast, but I applied some fairing compound over them as well, just because.

Total time billed on this job today:  6.25 hours

0600 Weather Observation:  28°, light freezing rain.  Forecast for the day:  Freezing rain and sleet, then rain, 37°

Scupper 208

Monday

As a sort of break and change of pace, I chose to focus for a day on some ancillary, yet still critical, portions of the project that could otherwise tend to be pushed aside in favor of some of the larger ongoing jobs.

To begin, I checked the fit of the after bilge switch platform I’d glued up last time, and found that indeed it would still work fine even though I’d mistakenly glued the top piece on backwards, so I went ahead and sanded the two platforms as needed to clean them up for paint and final fitting.  I added wire tie mounts near the top of each platform to help guide the switch wires, then painted the platforms with bilge paint.

I surface-planed some rough teak 8/4 stock as needed to smooth the sawmill marks, and dimension the wood as needed for the bowsprit.  Afterwards, I straightened one edge with a simple plywood straightedge and a circular saw, then trimmed the opposite edges of the two boards on the table saw to prepare for gluing up into a blank wide enough for the new bowsprit.

Afterwards, I glued the two board together and clamped them securely.

After setting the assembly aside to cure, I got back to work on the original cabin table, which I’d stripped and mostly sanded during the end of Phase 2 earlier in the year.  Now, I went over the table base, leaves, and top and sanded everything with 220 grit to prepare for finishing.  Then, after vacuuming and solvent-washing to remove dust, I applied a sealer coat of varnish to all sides of all pieces.

To finish up some of the lighting and wiring in the cabin, I required a few additional trim pieces, including the following:

During the rest of the day, I milled, sanded, and otherwise prepared these trim pieces as required, so that by the end of the day I had everything ready for primer or sealer coats of varnish as needed.

Total time billed on this job today:  6.5 hours

0600 Weather Observation:  18°, partly clear.  Forecast for the day:  Mostly sunny, 42°

Scupper 207

Friday

I got started by installing the replacement vent I’d ordered for the water tank.  This one was long enough to still work after passing through the thickness of the hull.

Sticking with the plumbing theme for now, I finished up the water hose run leading from the water pump aft, first through a tee fitting on the port side to accommodate the cockpit shower, then across beneath the cockpit and eventually through the bulkhead into the head area, where the water hose would eventually supply the fresh water flush toilet.  Near the end, I reduced the supply line from 5/8″ to 1/2″ to accommodate the nipple on the toilet intake.

I had expected to install a few more wires from the toilet control box to the head, but found that the wires needed were pre-installed inside the back of the toilet itself, so running them to the control box would happen later on, when I installed the toilet permanently.  For now, I didn’t want to do that as I wanted to be sure I finished up as much related (and other) work in and near the head before filling the space with the throne.  For now, I put the cover on the control box in the engine room and left it be.

Next on the agenda was the two electric bilge pumps.  I planned a diaphragm pump for routine dewatering.  This pump, which would be mounted high and dry away from the depths of the bilge, had a smaller flow capacity, but with its diaphragm pumping action and hose to the deepest part of the bilge sump in shaft alley, it would work well to keep the bilge as dry as possible, and wouldn’t allow backflow when the pump stopped.

In order to mount an automatic float switch, I needed to build a little platform to secure the switch and be able to lower it into the bilge sump, since this area was mostly inaccessible and there was no way to secure the switch directly to the boat in any event.  After measuring the depth required, and allowing for a means of securing the little platform to the engine beds, I built the simple arrangement from prefab fiberglass panels.  The switch I chose was a cylindrical fully-enclosed type that hopefully would work consistently without clogging, and was designed to be held in place with a u-shaped bracket; the width of this bracket determined the width of the support I built, but I also included a little base platform on which the pump could rest so it couldn’t slide out of its bracket.  I glued up the new bracket with epoxy and left it to cure.  I realized later, as I reviewed the photos, that I’d glued the top piece–the smaller chunky piece–on the wrong side.  I’d meant the L-shaped bracket to face aft, and for the chunky top to fit over the aft side of the engine platform to accept screws.  That said, I thought the bracket would work even turned around, but I’d soon find out.

As a backup, and for more potentially significant electric dewatering, I also planned a 2000GPH (0′ head) centrifugal bilge pump to be mounted further forward, in this case in the space accessible through the bilge hatch in the galley.  To secure this pump, along with its automatic switch, I built another simple platform, which here I planned to adhere directly to the flat base of the bilge through this locker opening, providing a place to screw in the pump strainer/base and the float switch’s bracket.  I made the vertical part of the bracket tall enough to provide a mounting point for the wires, to keep them elevated out of the bilge, and glued up the simple bracket with epoxy.  There’d also be, of course, a manual bilge pump to come.

Speaking of bilge access, in order to install the final wiring runs for the mast and some related wiring that would lead from the compression post, I needed to regain access to the forward part of the bilge, which access hatch had been covered for much of the construction with protective paper.  In addition, the paper had seen better days, and I’d been patching numerous rips and tears as they occurred.  Now, though, I removed the old paper and installed new protective plastic (same as on deck) to the sole, keeping the covering separate over both bilge access hatches so I could come and go as I pleased in the coming days and weeks.

I eased out of the day and the week by looking in some detail at potential anchor windlasses for the boat.

Total time billed on this job today:  6.5  hours

0600 Weather Observation:  4°, clear. Forecast for the day:  Sunny, 26°

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