(page 64 of 165)

Lyra 25

Wednesday

After being away from the shop all morning to finish up a small job offsite, I got back to work in the afternoon on the forward hatch, ready now for the final installation after some final masking to the hatch frame itself.

I installed the hatch frame in a bed of thickened epoxy adhesive, securing the frame with clamps as needed to press it into the epoxy and to keep it level from side to side.  I cleaned up the excess epoxy and shaped it as needed inside and out, then removed all the masking tape leaving clean lines everywhere.  I left the frames in the clamps to cure overnight.

Next, I prepared and installed the plywood platform in the generator compartment, now that the support cleat at the forward end was in place.  After surface preparations, I epoxied the bottom (hidden) side of the platform, then installed it in a bed of thickened epoxy adhesive at both sides, forming fillets as needed to smooth the transition to the hull and at the cockpit end.  I used a couple small lead weights to hold the platform securely against the hull, as it tended to rock slightly.

Afterwards, having already masked off around the hatch coaming again, I cleaned up the original fillets with some more epoxy, just to improve appearance and make the fillets consistent all around.  I removed the tape afterwards to leave a clean line.

Total time billed on this job today:  2.5 hours

0600 Weather Observation:  32°, mostly clear.  Forecast for the day:   Increasing clouds, 46°

Lyra 24

Tuesday

I’d planned to spend the day on the second coat of interior paint, but after careful inspection of all areas, and as critically as possible, I couldn’t find any reason why it would be necessary or even beneficial:  The finish on the first coat was so good as to obviate it, and I couldn’t find a notable fault.  Happy, if a bit surprised, to save the effort, I removed the masking tape and left the paint alone to continue curing before getting into any more interior work.  I planned to paint the cabin sole late in the week, which would give it the weekend to cure.

After some unrelated nits and nats during the morning, I got back to work on the generator storage area.  To test-fit the bottom platform in its final position, I used hot glue to mount a pair of temporary support blocks on the aft side of the cockpit well inside the locker, on which I could rest the plywood platform to check its angle properly against the “natural” angle of the generator in repose.  I ended up using a couple extra scraps of wood to raise the platform just a bit further, which worked pretty well and appeared to support the generator when installed.

After removing the temporary blocks and cleaning the bonding area, I installed with epoxy adhesive a 24″ hardwood cleat at the proper location; this would eventually support the inner edge of the new shelf.

For protection, I masked off the deck around the hatch opening, then installed the fiberglass hatch coaming permanently with thickened epoxy, forming a fillet around the outer edge and removing the tape when complete.  During an earlier work session, I’d already sanded away the paint from this narrow border to give the epoxy something real to bond to.

In a similar vein, I made final preparations towards the forward hatch installation.  Using the now-varnished hatch frame as a guide, I masked along its perimeter on the deck.  This gave me a line inside of which I needed to sand away the various paints to expose gelcoat for bonding.  With a sander, I could brush up against and slightly over the tape without causing damage to the adjacent areas, and remove the coatings within.  Inside the cabin, I used delicate surface tape and plastic to cover the opening and prevent sanding dust from going inside on the new paint.

Now I temporarily reinstalled the frame once more, and masked around it again, this time as protection against the epoxy I’d use to secure the frame to the deck in the near future.

Total time billed on this job today:  4 hours

0600 Weather Observation:  30°, partly clear, a crusty inch or two of snow from overnight.  Forecast for the day:   Partly sunny, 41°

Lively Heels Phase 3-25

Monday

After some shipping delays, the straps I’d ordered for the holding tank arrived, and with an afternoon available I looked forward to finishing the installation.

I began by reinstalling the modified port divider in the holding tank compartment.

After determining how to position the new angled base platform to allow room for the stainless eye straps that would hold the ratchet straps to secure the tank, I installed the platform with eight screws, four to a side, through predrilled holes in the platform, and with slight recesses to accept the screw head and a washer.  I secured the eye straps to the sole substrate with screws and pre-attached both ends of the ratchet straps, which featured stainless steel buckles and carabiners at the ends.

Now I could put the tank in place.  The tank fit easily through the overhead hatch, as planned, and soon it was in position.  However, I immediately ran into a problem.  Because of the various tank fittings, the hold-down straps only worked in two obvious areas where the way was clear–no problem there.  I’d used these positions to locate the eye straps and ratchet straps in the compartment.  What I’d not foreseen was a twofold problem:  First the starboard strap and ratchet buckle ended up interfering with the saltwater washdown pump and its filter housing, which were located on the bulkhead just ahead.  This meant there wasn’t clearance to operate the ratchet, and it also posed an ongoing clearance issue for the filter assembly.

In addition, the two ratchet buckles ended up closer to the top corner of the tank than I’d wanted, by virtue of the 12″ dead end measurement of these (and most similar) straps.  The starboard buckle, notwithstanding the filter issue, was more or less OK because the tank was higher on this side because of the angled platform.  But the port buckle (not shown here) ended up awkwardly and unacceptably at and just above the corner of the tank, and tensioning it in that position would likely tend to put undue pressure on the tank itself.

In a vacuum, as it happened, I could have made the starboard problem work, since the filter assembly and hose from the pump were actually easy to remove at a whim thanks to the design of the pump housing (a little plastic clip holds things in place).  So by removing the filter and hose assembly, I had enough room to operate the ratchet, and then reinstall the filter.  But this still wasn’t ideal, and in the end the fix for the port side worked a treat for the starboard as well.

The fix was to take the carabiners on the buckle side of the ratchet out of the picture.  Fortunately, I could remove easily enough the eye straps and slip the sewn loop of the ratchet strap over the eye, then re-secure the eyes.  Because the carabiners were permanantly attached, with the webbing sewn though a closed eye in the hooks, I couldn’t remove them, so I taped them above the webbing loop and out of the way to keep them from flopping around loosely.

This had the net effect of lowering the buckles by close to three inches at each location, which solved both issues nicely:  On the starboard side, the buckle was now below and clear of the pump housing (check); and on the port side, the buckle was now nicely below the tank corner where it could be safely tensioned (check).  This was a relief.  Now I could strap down the tank properly and finally, using some strips of 1/4″ thick rubber (left over from the first attempt at the new anchor pad on the stem) as chafe gear beneath the straps.

Continuing, I moved on to the hose connections, which were straightforward and didn’t take long, and went according to plan.  I secured the loop from the tank discharge to the nearby  pump with a pair of clamps to hold it securely and avoid any undue tension on the fittings at either end.  Afterwards, I reinstalled the water lines to the head shower setup, which I’d removed for access early in the project, cut off the excess strap length from the tank hold-downs, and wrapped up other details in the space to call this installation complete.

Total time billed on this job today:  3 hours

0600 Weather Observation:  12°, partly clear.  Forecast for the day:   Mostly cloudy, snow and rain in the afternoon and evening, 35 °

Lyra 23

Monday

Everything was ready to go, so I got right to work applying the first coat of semi-gloss white enamel to all interior surfaces, starting in the forward cabin.

Onwards to the head!

And finally, the main cabin, and then the loose hatches I’d removed to the bench.  This paint would cure to a soft satin finish.

Total time billed on this job today:  4.25 hours

0600 Weather Observation:  12°, partly clear.  Forecast for the day:   Mostly cloudy, snow and rain in the afternoon and evening, 35 °

Lively Heels Phase 3-24

Saturday

After a brief round of sanding to the first coat of fairing filler on the cockpit box, I set it aside, planning to add the second coat of fairing later in the day, but I didn’t end up getting around to it after all.

I’d hoped to use the day to finish up the holding tank installation, but alas, hub-related weather delays at FedEx had tied up the straps I’d ordered for the task, which were now days late but supposedly in my state at least, so I hoped they’d be delivered soon.  Instead, I turned to a wholly different project:  Some additional shelving in the large locker forward of the galley, across from the head.  Here, I’d originally, during the main project years before, installed just two shelves, mainly because of time constraints:  a low shelf, which had originally been intended and sized to hold an ice chest; and a large shelf about halfway up.  Now the owner was more than ready to have this space better available and more useful for the large amount of storage it could hold.

Earlier, the owner had mocked up some plastic storage bins he hoped to use in the space, and these would dictate the relative placement of two new shelves.  Using these bins as a guide, and allowing for room to pass the bins over fiddles at the inboard ends of the shelves (to be installed later), I determined the location for new shelf support cleats and made various measurements for the cleats themselves.  Most crucial was allowing room for the two bins in the lower space–the large bin (shown here) on the lower shelf, and a shorter bin to fit in an upper shelf.  There was enough room for both, but not a lot of room for leeway.

The new uppermost shelf would fit just at the space in the closet where the cabin trunk began, and would be much shallower than the other shelves below it, which extended all the way to the hull below deck level.  With the measurements complete, I milled four new shelf supports from scrap hardwood, along with some new shelf fiddles to help secure the storage bins, and prepared and sanded these all smooth before installing the cleats on the bulkheads for each new shelf.

After some basic measurements, I cut cardboard roughly to size to fit each new shelf location loosely, and scribed the actual shape and dimensions of the two shelves directly on the cardboard mockups, which I would then use to cut the actual plywood shelving to fit accurately.  With the cardboard “shelves” in place, I mocked up the storage bins in the lower shelves to illustrate their fit.

That was all I had time for at the moment, but one more good work session ought to see the shelf project to completion.

Total time billed on this job today:  2.5 hours

0600 Weather Observation:  23°, cloudy.  Forecast for the day:   Cloudy, chance of show showers, 30°

Lively Heels Phase 3-23

Friday

In a short work session, I lightly sanded the new fiberglass on the cockpit box and, after cleanup, applied the first of a few rounds of epoxy fairing compound over the sides.

Total time billed on this job today:  .5 hours

0600 Weather Observation:  21°, cloudy.  Forecast for the day:   Another anemic excuse for a snow event, cloudy with a chance of light snow and little accumulation, 29°

Lyra 22

Friday

In the cabin, I lightly sanded all the fresh primer to prepare for finish coats.  This was a light scuffing by hand to remove the “grain” that the primer raised and to provide a generally smooth surface free from burrs and fiberglass texture.  After sanding everything, I vacuumed and solvent-washed the entire area, leaving it ready for the next coat of paint.

This took all morning, and there wasn’t enough time  to think about starting the paint after lunch, so instead I turned to the generator storage locker once more, starting by removing the fiberglass tab that had been in the way at the base of the existing compartment.

Next, I marked a new cut line on the aft side of the opening 3/8″ aft of the existing cut to provide ample room for the new hatch coaming, then cut the new line with a jig saw.  Then, I cut the pieces of pre-made hatch coaming to length to fit tightly within the opening, overlapping the edges as planned.  This was all fine, but the deck here actually had more camber than I expected–it looked and seemed flat or even sagging in the middle–which meant that the rabbetted area of the coamings didn’t work quite as intended, but nonetheless the pieces would still work fine, and where the rabbet ended up exposed at the sides of the opening I could make up with a fillet during final installation.

I’d originally planned to install the coaming pieces piece-by-piece in the opening, but as I dry fit it seemed to make more sense to temporarily glue the four sections together in the right orientation with some scrap wood hot-glued across each corner, after which I removed the whole assembly to the bench and finalized the connections with epoxy fillets at the corners.

The leftover bit of the original glassed-over plywood stiffeners exposed in the new opening on deck needed a little attention now also, as these had long ago debonded from their skins, so I filled the voids as necessary with some of the epoxy leftover from gluing the frame, clamped as needed, and coated the exposed plywood with more epoxy to seal it and prepare the opening for the coaming’s final installation soon.

In final works for the day, I carefully sanded the eight filled bolt holes in the transom to prepare them for the next steps.  Also, new bronze flat bar stock I’d ordered for the chainplates arrived; the owner and I had decided it made sense to replace the original chainplates after I found a reasonably-priced source for the raw silicon bronze.   The new stock was 3/16″ thick compared to the 1/8″ thick originals.

I’d still have to cut to size and shape and drill the holes in each chainplate, but because these were bronze it was something I could do easily enough at the shop.

Total time billed on this job today:  5 hours

0600 Weather Observation:  21°, cloudy.  Forecast for the day:   Another anemic excuse for a snow event, cloudy with a chance of light snow with little accumulation, 29°

Lively Heels Phase 3-22

Thursday

With a new supply of fiberglass cloth on hand, I cut and installed new fiberglass to sheathe the field areas of the box inside of the tabbed corners.

Total time billed on this job today:  1 hours

0600 Weather Observation:  12°, clear.  Forecast for the day:   Partly sunny, 28°

Lyra 21

Thursday

Before starting the primer in the cabin, I had to mask off several areas for protection, including some naturally-finished beams in the forward cabin and head, and the main bulkhead in the saloon.

With that complete, I got started on the primer, beginning in the forward cabin.  I found that the cleats within the locker openings were still filthy with dust and debris in the corners, so for now I left those unpainted.

Continuing my way aft, I painted the head.  This space, already small, became that much tighter with every brush and roller stroke as I willed myself not to bump into any of the freshly-coated surfaces.

During the afternoon, I finished up in the main cabin, painting every surface except the cabin sole, which would get more of the light gray Bilgekote sometime later in the process. In painting all areas of the empty main cabin now, it was understood that there would later be cause to remove some of the paint to allow for new interior installation and tabbing, but given the nature of the project, with limited time and an extensive work list, too many overlapping and required jobs and new installations hinged upon having the painting done before work could continue, and we didn’t have the luxury of an open-ended timeframe to let each thing flow more naturally together.

Down on a bench, I primed all sides of the various berth locker lids that I’d removed for the purpose.

Total time billed on this job today:  6 hours

0600 Weather Observation:  12°, clear.  Forecast for the day:   Partly sunny, 28°

Lyra 20

Wednesday

For the bilge and utility locker spaces, the owner requested a lighter version of the usual gray bilge paint, so I mixed up a 50/50 mix using a gallon each of white and gray to considerably lighten the color.  With the paint mixed, I got to work on beginning the interior paint, starting at the bow in the chainlocker.

Continuing aft, I painted the lockers beneath the V-berth, and around the water tank to the extent possible, before painting the first section of bilge on my way out.

Next, I painted the storage lockers on both sides of the head compartment, and the bilge there as well.

In the main cabin, I painted what I could reach through the various locker openings in the tops and sides of the settees, and the bilges.

Starting with the space beneath the cockpit on the centerline, as far aft as I could reach, I painted everything below cockpit level and through the engine room, including the forward face of the cockpit well.

To finish up for now, I painted the hull inside the port and starboard cockpit lockers, from just forward of the lazarette up to and including the aft-facing sides of the engine room bulkhead.  The lazarette still had some work to go, so I held off painting in there for now.

During the afternoon, I turned my attention to that very lazarette as I continued work on the storage arrangements for the small generator.  After various test-fits and puzzling things out, I started working on a support platform for the generator that could accommodate it without raising headroom too much.  Beginning with the cardboard template I’d made of the generator footprint, after some adjustments for hull shape I transitioned to a template made from some scrap 1/4″ plywood.  The new platform would require an angled installation, and the forward end would ultimately be supported against the back side of the cockpit well, but at the moment there was a fiberglass arrangement there in the way (though it did sort of help support my platform templates for now), and I couldn’t remove the fiberglass because I didn’t want to disturb the nearby fresh locker paint, so I worked around it.

Various reference marks I made on the hull and cockpit, along with side views courtesy of the camera held through the cockpit locker openings, helped me start to figure out how the platform would need to work.  In these photos, the template is still too low at the cockpit end, but once I could start doing dirty work in the space I could and would made adjustments there and add the requisite supports to hold the platform more where it needed to be to support the generator.  In this orientation, the handle at the top of the generator was just flush with the deck above, which meant that it would be clear beneath the new hatch once built.  Other details, like chocks, fiddles, and means of securing the generator, would easily work themselves out once the basic platform idea came together.

Eventually happy with my plywood template, I used it to cut a real floor from some marine plywood.  I beveled the aft edge severely to help it fit against the shape of the hull and counter at the aft end.  I had time to test-fit the platform, but I had one more thing I wanted to do before the end of the day, so that was all for the generator at the moment.

There was a series of holes in the transom leftover from a long-ago outboard bracket, and now I made preparations to fill them.  After reaming them out with a large countersink from outside, I cleaned everything up and masked inside and out before filling the holes with epoxy fairing compound.  I removed the exterior tape once the fill was in place.  With some delicate finish work once the epoxy cured, I’d be able to touch up the paint with something close to the paint that was on the hull.

With the remains of the fairing compound, I troweled over that little line in the middle of the aft cockpit patch.

Total time billed on this job today:  7 hours

0600 Weather Observation:  16°, clear.  Forecast for the day:   Sunny, 24°

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