(page 159 of 167)

Nomad 14

< Back to Nomad

Thursday

With the required or at least prudent full-day waiting period before I could mask over the brand-new hull paint, there was little I could do beyond cleaning up the spray equipment, prepping boottop paint for the work ahead, and removing the masking tape I’d applied where the boottop would be.

I looked forward to having this image-changing part of the project behind me, and to getting back on board for the first time since I got ahead of myself and masked her up a few months earlier.

Total time billed on this job today:  .5 hours

0600 Weather Report:
25°, cloudy.  Forecast for the day:  Possible wintery showers, then mainly sunny, high in the upper 30s

Nomad 13

< Back to Nomad

Wednesday

After final preparations, I applied three coats of Alexseal wine red gloss topcoat (also called claret by other coatings manufacturers) to the hull.  The flash, and the harsh lighting in the shop, make the paint appear a little lighter than it actually is.

The job went swimmingly till the very end, as I was refilling my spray cup after doing the third coat on the first side of the boat, as is my habit, but this time somehow I managed to fumble the paint pot, spilling a good amount all over my paint prep table, spray gun, and the floor.  It looked like I’d just slaughtered a pig, though it was less dramatic after I’d cleaned up a bit.  The stain would remain for all my days as a reminder.

hullpaint11-123015

Total time billed on this job today:  3 hours

0600 Weather Report:
15°, cloudy.  About 3-4″ snow total yesterday, plus mixed sleet/freezing rain.  Forecast for the day:  clouds and showers (all types), highs in the 20s

Nomad 12

< Back to Nomad

Tuesday

I spent the first part of the day sanding the new primer with 320 grit, by hand and machine as required.   Once the sanding was complete, I blew down, vacuumed, and solvent-washed the hull before cleaning up the rest of the shop by broom and water hose.

With her slab sides and sharpie-like hull sections, this boat had no challenging hull curvature to complicate the boottop layout, so to mask off for the eventual boot top I simply applied 2″ masking tape just above the line I’d masked earlier for the bottom.

I wrapped up the day with final hull preparations–another solvent wash, this time with the proprietary solvent from the coatings manufacturer–and paint and spray equipment preparations.

Total time billed on this job today:  4.75 hours

0600 Weather Report:
Snow, about an inch on the ground, 17°.  Forecast for the day:  Snow, 4-7″ predicted, possibly mixing with or changing partially to freezing rain at some point.  Highs in the 20s.

Nomad 11

< Back to Nomad

Monday

After final preparations, I spray-applied four coats of gray Alexseal epoxy finish primer on the hull.

Typically, I liked to use high-build primer first on the boats I worked on, and for a time I waffled on whether to use it here or not.  Most of the boats that passed through the shop benefited from this additional work, as with various repair work and aged, often checked and damaged, gelcoat, the heavier layer of primer not only helped ameliorate these surface conditions, but also gave me additional opportunity to fine-tune the surfaces before final primer coats.  I considered it part of the fairing and surfacing work, rather than part of the painting work.

With this original hull in such good condition overall, with minimal sanding and virtually no repair work or fairing required (other than the transom repair),  the finish primer was the coating that was most important to the eventual character of the gloss topcoats.  But I still wavered on the high-build, and  in fact I eventually decided to use it here simply as a matter of course, even though I’d originally determined not to.   Then, late on a Sunday afternoon during final preparations, I discovered to my dismay that I didn’t have enough of the reducer for the high-build primer on hand to do the job, which meant that I’d have to postpone my planned schedule in order to get it–a two-day delay.   With my feeling that it wasn’t an important step for this boat anyway, this discovery cemented the decision to simply go with finish primer as the first and only step before topcoats.

Total time billed on this job today:  4 hours

0600 Weather  Report:
16°, clear.  Forecast for the day:  Sunny, windy, 25°

Nomad 10

< Back to Nomad

Sunday

A few final details remained before I could apply the hull primer, so I finished up the prep work with some additional masking to cover the trailer and along the waterline, where I installed masking paper to protect the bottom and portions of the trailer from overspray.  Afterwards, I solvent-washed the hull and set up paint and spray equipment to be ready for the work ahead.

Total time billed on this job today:  2.25 hours

0600 Weather Report:
Rain, snow, sleet, 32°.  Forecast for the day:  on and off rain and mixed precipitation, highs in the low 30s

Danusia 7

< Back to Danusia

Wednesday

With new saw blades on hand, I felt I needed to conquer the windlass before Christmas break, as I hated to leave things unresolved.  I wanted that windlass out.  At this point, I almost didn’t care how it got out–as long as it did.  I couldn’t stand seeing it there, sneering at me and pretending it was just so superior.

First, I tried–in a laughingly brief way–to use a length of pipe to bang on the steel part of the shaft housing surrounding the bronze turning shaft.  This was so utterly ineffective (exacerbated by that cove shape the housing had ended up), and I quickly turned to the saw, fitting it beneath the bronze deck plate where I’d already reamed out the sealant earlier.  This was really the only practical access to cut the windlass into pieces, as space belowdecks was simply too tight and basically inaccessible where the shaft was.  If this didn’t work from on deck, I wasn’t sure what I’d do.

windlassout1-122315

I found it worked for me to stand on the staging next to the boat and hold the saw along the aft side of the shaft–this gave me the best leverage.  It took about 30 minutes and two saw blades to make it through.  At first it was impossible to tell whether I was making progress or not, as I couldn’t really see into the narrow slot, and certainly the cutting progress was not something one could measure by eye or feel.  I think the first blade must have dulled quickly on old sealant or wood, as once I’d changed to the new blade after a time the progress seemed quicker.  In any event, eventually I completed the cut, freeing the deck plate.  Success!  Or so I thought.

I’d kind of expected that once I’d made the cut, I’d hear the windlass drop out below.  Planning ahead for this, I’d lined the chainlocker with an old cushion and towel to soften the blow, but the shaft and housing held tightly in the wooden deck riser with no sign of movement whatever.  After checking things out below, I returned to the foredeck and, using a small hand-held sledge, I pounded the top of the shaft, both with my length of pipe (limited or no success at first), and then without,  It took surprisingly brutal effort to budge the thing at all, and at first all I heard was more chunks of thick, flaky rust crumbling off the windlass, but after a number of severe hits I saw progress, as the shaft started plunging through the wood.  Finally, at length, the windlass gearbox and motor came free and fell the short distance onto the pillows.

Even though I’d removed–by corrosive attrition and as a byproduct only–probably 10 pounds of rust (a full 5 quart bucketful) from the windlass housing during the removal process, what remained of the windlass and motor was extremely heavy.  I was so glad to get it out of there and down to the bench with all its component pieces (except the capstan drum, which I forgot to include in my still life photos below),  What a piece of junk this thing turned out to be.  What all this plain steel was doing in a windlass was beyond me.  A real shame, as I know the working components were all bronze and stoutly built.  To shroud such fine mechanicals in this steel case was obviously a poor choice.

With the windlass finally out of the way, I cleaned up the deck and chainlocker as needed, including removing the semi-circular deck riser adjacent to the bowsprit, as the removal had damaged this easily-replaceable piece.  The good news in all of this was that the deck in this area was core-free, just a solid 1/2″ or so laminate.  Briefly inspecting things from beneath, it seemed this might have been a planned omission at the time of construction specifically to allow for a windlass installation on this side.  But at least the large through-deck hole had not allowed any damage to the decks, which couldn’t be said for the windlass itself.

During some work in the port cockpit locker a little earlier, I’d noticed the other ends of the large windlass cables hanging out of the wire chase on that side.  Besides being too short to reach a battery, the cable ends weren’t looking too great, and one of the cables had a cut in the insulation that would obviate the last foot or so of that cable.  So whatever happened from here in terms of windlass replacement, there’d unfortunately be more wiring work to complete.

 

Total time billed on this job today:  1.5 hours

0600 Weather  Report:
Fog, clouds, 35°.  Forecast for the day:  clouds, rain coming overnight, high in the low 40s

Nomad 9

< Back to Nomad

Tuesday

Once more, I sanded the transom repair as needed, eventually ending with hand and machine sanding with 120 grit to tie this area in with the rest of the hull.  I touched up a few other areas by hand as well, completing the basic hull prep.

transom1-122215

Afterwards, I cleaned up the shop, blowing off the walls and other surfaces, vacuuming, sweeping, and washing the floor.  Just a little final prepwork lay between me and high-build primer.

transom2-122215

Total time billed on this job today:  1 hour

0600 Weather Report:
25°, cloudy.  Forecast for the day:  clouds, rain late in the day.  High 44°

Danusia 6

< Back to Danusia

Tuesday

I continued work on the decks, this time mainly on the starboard side, where I cleaned up and polished the cabin trunk and borders on the sidedeck.

With the main deck areas complete, I moved up to the coachroof and portions of the cockpit, and took care of various borders and smaller areas around the hatches and elsewhere, which, as with other deck areas, started out with various levels of dirt, oxidation, and other staining.

For now, I left the main part of the cockpit well untouched, but cleaned up all the areas bordering brightwork so I could get moving on that project soon.

I used some rags to soak up any remnants of liquid from the bilge, and sanded away the paint from the new garboard drain area to prepare in advance for its installation later.

garboard1-122215

I’d hoped to finish up work on the windlass removal, hoping my saw blades would arrive in the early afternoon, but the usual increased package demand and traffic from the last-minute holiday rush caused my normal delivery to be much later than usual (not unexpectedly), too late for me to move forward with that project.

Total time billed on this job today:  3.75 hours

0600 Weather Report:
25°, cloudy.  Forecast for the day:  clouds, rain late in the day.  High 44°

Nomad 8

< Back to Nomad

Monday

After the usual water-wash, I sanded as needed the spots on the hull and, especially, the transom repair to smooth the epoxy fairing compound and, where required, to prepare for a second coat.  After cleaning up, I applied more fairing compound to portions of the transom to take care of low spots and some fine-tuning.

Total time billed on this job today:  .75 hours

0600 Weather Report:
30°, mostly clear.  Forecast for the day:  clouds and sun, breezy, around 40

Danusia 5

< Back to Danusia

Monday

Over the weekend, I continued treating the windlass shaft housing with penetrating oil.  Whatever the next attempt at removal entailed, it’d require additional force and additional materials, especially as the likelihood grew that I’d end up cutting the shaft to release the above- and below-decks components from each other so I could finally effect a total removal, which was required no matter what.   So while I awaited saw blades, I took a break from the windlass to focus on some of the other jobs on the boat.

I started with the external strainer over the engine intake, down in the keel near the turn of the bilge.   The owner was rightfully wary of this external “scoop” strainer, and with a good internal sea strainer he requested I remove the strainer to leave the through hull unprotected, which gibed with my own opinion.  During a meeting at the boat a few days earlier, we’d determined that the strainer was not an integral part of the through hull the way they sometimes are, so removal looked straightforward.

And so it turned out to be.  After removing layers of paint and barrier coat from the fitting and exposing the fixing screws, I could remove the strainer easily, after which I cleaned the hull of old sealant, slightly feathered in the edges of the surrounding bottom paint and barrier coat, and prepared the four screw holes for repair by milling small countersinks at each location.  Afterwards, I applied some epoxy fill material.

While in this neck of the woods, I scoped out the bilge to determine where to mount a new garboard drain.  From inside the boat, through a small access hatch directly above the deepest portion of the bilge sump, I looked for obstructions and reference points I could use from outside, and measured down from the bolts securing a grounding plate that happened to be located right above the best location for the new drain.  This made it pretty easy to recreate the location from outside, after which I drilled a 1/2″ test hole to drain the remaining liquid from the bilge (mostly antifreeze) and ensure that the location was where I wanted it.

Then, I could drill the 1-1/2″ hole (with key slot at the top) required for the new bronze drain fitting, which I didn’t yet have on hand but would order and install soon.

The largest single job on the work list for Danusia was the exterior brightwork, which required stripping and refinishing.  The existing Cetol finish was tired overall and failing completely in many areas, and the owner wished to upgrade to varnish.  With significant woodwork on deck, this would effect a dramatic improvement to the overall appearance of the boat.  These photos show the general condition of some of the brightwork at the start of the job.

Before beginning down that road, however, I thought it’d be best to first work on the cleanup and polishing of the gelcoat on deck, another job on the project list. By doing this first, I could avoid worrying about damaging new varnish work with abrasive polishes, and any residue I might get on the woodwork now would be removed during the stripping and sanding process ahead.  The gelcoat, which appeared to be original (though the nonskid had been redone at some point), was in generally good condition for its age, approximately 30 years, and I thought it would clean up fairly well all things considered.  At the moment, it was dirty and oxidized.

Starting randomly on the port side, I prepared to clean up and polish the gelcoat on the cabin trunk and deck areas.  I soon found that the lifelines were inconveniently in the way, and since removing the stanchions was something that was going to happen at some point anyway to allow me to add or redo stanchion tube fasteners and set screws (and also to make way for a new winter cover), I went ahead and did it now, first on the port side and later to starboard.  While the stanchion bases included one screw opening for a fixing screw into the stanchion, which secured the stanchions well, many of them were wobbly in the bases, a condition the owner didn’t care for, and adding set screws would tighten them and prevent this from happening.  I was prepared to drill and tap the bases for new set screws, but as I began the removal I noticed that all the bases already had a place for a set screw, though in most cases there was no fastener in place.

This was good news since it would save the challenge of creating these holes from scratch later.  So without further delay, I removed the stanchions and lifelines, and got back to work on the gelcoat polishing on the port side, and eventually moved around the transom towards the starboard, where I’d continue next time.  The old gelcoat looked much better afterwards, clean and with some shine and much improved, though the gelcoat was growing thin and showing its overall age and would never look brand new again.

Total time billed on this job today:  5.75 hours

0600 Weather Report:
30°, mostly clear.  Forecast for the day:  clouds and sun, breezy, around 40

 

Older posts Newer posts