(page 147 of 165)

Precision 6

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Thursday

After some other business away from the shop, I got to work again on the scuppers.  The epoxy had cured overnight, leaving my new recesses ready to go.  The screened fitting fit flush and finely.

I was awaiting delivery of the second fitting–I only had one on hand–as well as some elbows I needed below the deck, so for the moment I held off on installation.  I did install the two exit through hulls in the transom, completing that side of the new drainage system.

Next, I continued work on the electrical system.  I hooked up a battery so I could start to check the various circuits for operation.  Most of the lights on the boat–two of three cabin lights, plus the bow and stern lights–operated when tested, but the forward cabin light turned out to be rusted within and was missing its switch, and therefore inoperable.  I removed the damaged fixture and ordered a replacement light.

The owner reported that the VHF was inoperable, and after some troubleshooting and testing I traced the electrical problem to a bad fuse holder near the radio, which I replaced.  This process also highlighted some issues with the existing fuse holder block on the port side of the boat, which serviced the VHF as well as the depthsounder and knotmeter (old as well as the new), and I couldn’t determine the issue, so I simply replaced the fuse holder/terminal block with a new one that I had on hand, and redid the short wire runs for the depthsounder and knotmeter, running them through an existing switch so they could be turned off as needed.  At the same time, I secured a 12-volt outlet to a nearby structural member, and cleaned up the wiring pending final installation of the instruments a little later.  Everything tested operational once I’d made these changes.

To ensure that I could complete the new instruments’ installation soon, I continued work on the exterior cover panel where they’d be mounted.  I lightly sanded the primer that I applied earlier, then during the day spray-applied several coats of off-white LPU to generally match, or at least be consistent with, the existing deck surfaces.

panel1-42816

The wiring to the single mast light led through the deck forward of the mast step, and was hidden beneath the forward cabin light fixture (the one that didn’t work and I’d removed).  I couldn’t get power to the plug above deck, so I looked into the issue further and eventually removed the existing wiring through the deck, cutting off several old extensions and rewires from the past till I had the basic wires remaining.  Digging into the old wire harness leading to the mast light plug, I found that red connected to green, and black to white, so now I knew which wires were which inside the boat and could make up a connection to a new wire pair, which I led above deck through the existing cable clam and reconnected to the old 2-way plug for ease of mast stepping and unstepping.  With the meter, these wires tested operational.  Later, I’d redo the mast side of the lighting circuit as required, but this completed the boat side troubleshooting and testing, and repairs as needed.

Total time billed on this job today:  4.25

0600 Weather Observation:
Clear, 22°.  Forecast for the day:  Sunny, 50s

Salty 46

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Wednesday

In the near future, I wanted the chance to test-run the new engine, and this need, along with other obligations requiring the inside of the shop, meant that, now that all the work was otherwise complete (excepting the new propeller shaft and engine startup), it was time to move Salty outdoors for storage and the duration of the final stages of the project.  The boat wouldn’t be leaving here for a couple months, so to ensure access to other boats in storage I set her down in an out-of-the way location, but readily accessible to the shop for the final work as needed.  I offset the jackstands so I could easily paint the last patches of the bottom.

Total time billed on this job today:  1 hour

0600 Weather Observation:
Clear, foggy, frosty, 22°.  Forecast for the day:  sunny, 50

Precision 5

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Wednesday

To access the aftermost part of the boat and the cockpit scuppers, the best way in seemed to be through the aft bulkhead in the cockpit, which would give access to the transom as well as the cockpit sole fittings.  There was an existing access port there, but it was far too small for real access.  To begin, I marked the bulkhead using the cardboard template of the cutout that I made earlier.   With a 4″ hole saw, I made the 2″ radius cuts at the corners, then connected them with a saw to create the opening.  The new opening gave quite good access to the required areas.  Note that the original access port was not quite centered.

Next, I removed the old pipe and fittings.  The cockpit side was already loose and took only a push from the top; the gobs of sealant securing the pipes to and through the transom were quite resilient, but eventually I got them loose and the pipes removed.

The bulkhead had a slight concave curve to its shape at the top of the new opening, and it was too severe to bend the new hatch into position.  The bottom edge, and the vertical sides, were flat enough for a successful fit, but I needed to build a filler piece for the top to properly support the hatch and fill the gap.  From teak stock, I scribed and cut  a curved piece to fit; I’d await final installation of the hatch till I was done with all the scupper work, since the raw opening was quite a bit larger than the hatch itself.

To rebuild the scuppers, I planned on new fittings at transom and cockpit sole, connected with hose to create a more flexible situation than the original pipe.  For the cockpit, I selected Marelon fittings with a built-in screen.  To provide complete drainage, I had to recess the mushroom fittings so they were flush with or beneath the sole surface.  Since the laminate was no thicker than the thickness of the mushroom heads, I’d need to basically build a new supporting surface beneath the sole for the fittings.  The original holes were the right size for the threads, but too small for the heads.  So to open up the holes, I hot-glued some plywood beneath the openings, to give the hole saw pilot bit a guide, then used a larger hole saw to increase the diameter of the openings.

This allowed the mushroom head to fit flush through the sole.

scuppers11-42716

To support the fitting below the sole, I used some circular cutouts from 1/4″ fiberglass, into which I drilled holes the right size for the fittings’ threaded necks.  After cleaning up and sanding as flush as possible the bearing surfaces below the openings, I epoxied these discs in place, aligning the holes in the center.  This effectively provided a “molded” flat-bottomed recess in the sole that would fit the scupper fittings cleanly.  I made the epoxy mixture thick enough that it held the discs in place on its own, but to be sure that I continued to thwart gravity long enough for the epoxy to cure, I added some tape as a backup.

I also sealed the plywood edges of the transom cutouts with the thickened epoxy.  Now I’d wait for all the epoxy to cure before I continued with work on the scuppers.

scuppers15-42716

To cover the large holes left over from the old round instruments, I built a simple exterior panel from 1/8″ fiberglass laminate, which I cut to the angles required to tie in with the shape of the companionway and cabin top.  After marking its position as needed, I drilled 2-1/8″ holes to accommodate the new instruments, then applied a few coats of epoxy primer during the remainder of the afternoon.

For the inside cover panel, I cut teak plywood to fit as needed, which blended well with the existing plywood cover on the bulkhead.

covers4-42716

With the new instruments and transducers now on hand, I went ahead with the installation of the transducers (depth and speed), using the original holes in the boat, which I’d already prepared for the installation.

Then, I led the cables aft, following the same route and using the same support hardware as the original cables that I’d just removed.  I’d make the final connections to the new instruments later, once the cover panels were done and ready for installation.

I finished up the minor keel work with a quick wash and sand of the filler I’d applied earlier.

I’d moved some other boats around, which gave me the opportunity to reposition this boat alone in the center of the shop for better access for the remainder of the project.

shop1-42716

Total time billed on this job today:  6.25 hours

0600 Weather Observation:
Clear, foggy, frosty, 22°.  Forecast for the day:  sunny, 50

Precision 4

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Tuesday

Starting out, I pared and smoothed away the excess bungs from the new companionway rails.

The owner reported that the depthsounder was non-functional, and replacment was on the work list.  To begin, I removed the existing through-hull transducer, then the transducer wiring leading aft to the display unit mounted in the cockpit bulkhead.  I removed the obsolete 4″ round display and all related components.  4″ round displays were no longer available on the market, so the replacement would be something else, and would require a cover plate over the larger hole left over from the old unit.

Later in the day, while on phone conference with the owner about the new depthsounder choices, he made the decision to also replace the old knotmeter, so with that decision made I went ahead and removed the old display, wiring, and transducer as required.  The owner selected a matching set of new instruments, which I ordered at once.

There were various minor wiring issues that became apparent as I looked over the boat’s electrical system, which was generally in good (original) condition, but there were a few improvements that I thought I could make right off the bat, starting with replacing the terminal ends on the two sets of wires that would connect to the battery, located in a large compartment below the cockpit.  I also replaced a black (or maybe dark purple) wire that fed the positive supply to an auxiliary fuse panel on the port side with a red wire to eliminate confusion, and, further along these lines, secured together two white (negative, in this boat’s protocol) wires with a section of black heat-shrink to make it apparent which wires were which going forward.  For now, the remaining wiring looked OK, but I’d test out various lighting fixtures and installations in the near future, now that I had the basic supply side in better shape.

The existing VHF antenna cable, which led to deck through the mast step base, was in poor condition where visible, with numerous cuts through the insulation, so I replaced the entire length back to the VHF with a new cable.

The galley sink featured a simple tankage and supply system consisting of a plastic jug in the cockpit locker.  There was no connection visible between the tank and the hand faucet, and the owner had mentioned that the old hose was clogged with debris and mold.  Although there was a round access hole located just behind the mobile tank–which allowed me to h old in a camera for the photo of the underside of the sink–the locker wasn’t large enough for me to climb into, and I made plans to install a new access port from the cabin so I could change the hose and (if necessary) the faucet to restore the sink to working order.

With new bolts on hand, I reinstalled the chainplates in heavy beds of sealant, forcing the sealant into the gaps around the chainplate as much as I could.  I left the excess sealant to cure before attempting to remove it.

With a new plastic access hatch now on hand–black to match the other access ports on the boat–I prepared a cardboard template of the cutout, and would use this next time to open the aft end of the cockpit for access to the scuppers.

The leading edge of the keel had some minor impact damage, so to repair it I sanded away paint and loose material, then filled it with an epoxy fairing mixture.

Meanwhile, I sanded away the paint from around the two through hull openings just forward, to prepare the hull for proper bonding of the new fittings when the time came for installation.

Total time billed on this job today:  7.25 hours

0600 Weather Observation:
Clouds, 36°.  Forecast for the day:  cloudy, snow, high around 40

Precision 3

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Monday

The sliding companionway hatch rode inside and beneath slim pieces of teak trim, which, over time, had become brittle and weathered, and were broken and cracked in places, limiting proper function as well as appearance.  Replacement was warranted.

To remove the old trim for reproduction, I drilled out the bungs to expose the screw heads, then removed the trim easily from there.

From some teak stock on hand, I milled new trim pieces, more or less duplicating through various saw operations the profile and details of the original trim, which was a sort of inverted, angled L shape.  However, hoping to provide a little more strength over the long term, I made the top portion of the profile–the section that overhung the companionway hatch to hold it in place–a bit thicker than original.  Afterwards, I cut the trim to the required length, pre-milled counterbores and screw holes for the fasteners, and sanded the pieces smooth, easing the edges as I went.

I intentionally changed the location of the screw holes to provide fresh material for the threads to grip, so I began the installation with a dry fit, in which I predrilled and secured all the fixing screws as needed.

Next, I cleaned up the bonding surface, masked off the exposed edge of the teak trim, and installed the rails permanently with sealant and screws.  After removing the excess squeezeout, I removed the masking tape, leaving the clean, bare teak.  I bunged the screw holes, completing the job for now.

The owner had asked me to look at the original plywood outboard motor mount and see about somehow refinishing it.  This would be possible, though it would never be beautiful, but as I looked at the piece I noticed plenty of splintering, compression, and missing chunks, and on impulse I decided it’d be better, less expensive, and ultimately more attractive and useful  to purchase a replacement pad, which were now available in maintenance-free plastic.  After confirming the bolt pattern was compatible, I ordered a new pad, and removed the old one to prepare for the new one’s arrival.

Meanwhile, I spent some time coming up with a new scupper plan, and ordering various materials for the job.  I planned to remove the existing PVC pipe and elbows at both ends, and replace with new fittings and hose once I’d opened up access at the aft end of the cockpit.  I ordered the new access port as well, and would begin this job later, once the pieces were on hand.

The owner reported a problem with chronic chainplate leakage, and indeed evidence of this was cl ear, with water staining on the bulkheads around the chainplates.  Similar issues with this sort of  through-deck design were common, as everything about the design and the forces involved made sealing a tenuous situation at best, but the leaks were probably more noticeable here because of the highly visible location well inboard and exposed on the bulkhead.

In any event, to address the issue now I removed the chainplates entirely, starting with the deck covers and then the stainless steel plates themselves, which were secured with four bolts through the bulkhead and a heavier support beam across the cabin.  The various components were in good condition, and I cleaned them up to prepare for reinstallation, removing old sealant and staining.  Though the fixing bolts were in sound condition, I decided to order new ones as a matter of course.

Afterwards, I cleaned up the chainplate slots through the deck, reaming out old sealant and other material to open them up as much as possible and provide a good sealing surface for reinstallation.  Then, I sealed the insides of the openings through the deck with a thickened epoxy mixture; while there wasn’t an obvious issue with deck core moisture in these slots that required repair, it was sound practice to seal the openings now, while I had the chance.

Total time billed on this job today:  6.5 hours

0600 Weather Observation:
21°, clear.  Forecast for the day:  sunny, high in the 50s

Salty 45

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Friday

A supply snafu had delayed delivery of the 1″ hose I needed for the engine siphon break system, but now it was on hand, and I gladly finished up the installation.  I located the siphon break fitting in the port cockpit locker, secured to a wood block on the hull, as high up as practicable and just aft and outboard of the battery box.  I connected the vent/overflow hose, which led aft to the gooseneck at the transom, to the nipple on the top

I also cleaned and polished the cockpit well, completing the deck work.

At this point, the project was complete except for installing the new prop shaft, and finalizing the engine alignment, along with the engine start-up and test run.  I anticipated the shaft would be on its way within the next week or so, at which time I’d finish the final tasks.

Total time billed on this job today:  2 hours

0600 Weather Observation:
32°, clouds.  Forecast for the day:  clouds and sun, 60s

Precision 2

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Thursday

Getting ready to begin the project in earnest, I spent a short time aboard, documenting the initial condition of the boat and looking over the jobs list so I could begin to order any materials and parts required.

The biggest job, as it were, was the cockpit scuppers.  The original scuppers used rigid plastic fittings and pipe to connect the cockpit well with the transom outlets, and these fittings had cracked over time, with several apparent attempts to stem the problem with sealant or other repairs apparent.  The main issue with this situation was that access was essentially impossible for anyone other than a highly-skilled two year-old, as the molded interior structure and cockpit well prohibited direct access to the space from inside the boat–despite what looks like wide open access from the photos.

The answer to the access problem seemed to be to install a larger access hatch in the vertical section of the cockpit well, replacing the small round one.  So creating this access would be the first part of the job, and afterwards hopefully the access would be sufficient to replace the fittings with a new system.

scuppers8-42116

The interior cushions were badly worn and in poor condition, and I’d subcontracted their replacement to my trusted upholsterer.  This job was already underway, and I removed the cushions from the boat to make more room for the other parts of the project.

The work list contained myriad and sundry smaller jobs, from rebedding the leaky chainplates to replacing the depthsounder to repairing some teak trim, among other things.  I’d cover them all in more detail as the job got underway.

The hull would require some basic restorative work, including replacing the scuffed vinyl-tape bootstripe and painting the bottom.

Total time billed on this job today:  .5 hours

0600 Weather Observation:
25°, clear.  Forecast for the day:  sunny, 70s

Aquasport 5

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Thursday

Earlier, I’d finished up the fiberglass backing plate for the outboard bracket–sanding, primer, topcoat (the same gray I used on the boottop).  Now, with the transom prepared and the backing block ready, I completed the bracket installation, securing it with four bolts, backing plates, and large washers.

< Back to Aquasport

Total time billed on this job today:  1 hour

0600 Weather Observation:
25°, clear.  Forecast for the day:  sunny, 70s

Danusia 46

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Thursday

Taking advantage of a beautiful day, I finished up a couple final chores for Danusia, starting with new bottom paint.

When I’d reloaded the anchor chain into the new windlass at the end of the original project earlier in the winter, I’d recommended installing some sort of protective plate over the bow platform between the roller and the windlass, as I feared the chain, when wiggling and wobbling its way up or down, might harm the surface.  It would also protect the platform from the anchor shank at rest.  At the time, the boat was being moved outdoors and covered, so although I acquired the bronze plate shortly thereafter, I waited till the boat was uncovered to finalize the installation.

I’d ordered a 1/8″ x 3″ x 18″ bronze plate, which I’d determined was a good size for the area in question, and now I held the plate in position so I could mark an angled cut required on one side to match the angle of the teak platform.  Down on the bench, I cut off the excess and finished off the cut appropriately.  I prepared several countersunk holes for screws.

Installation was straightforward.  I started with the plate just aft of two slots in the platform and aligned it as needed, then secured it with bronze screws.

< Back to Danusia

Total time billed on this job today:  2 hours

0600 Weather Observation:
25°, clear.  Forecast for the day:  sunny, 70s

Salty 44

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Wednesday

After some morning errands away from the shop, I turned to the mast wiring.  While I had the masthead casting off, I checked over the masthead sheaves, which all looked in good condition as far as I could tell, but it looked like there might be one damaged or partially missing, as evidenced by the plastic hub on the aftermost pin (first photo).  That pin just slipped into cast slots from above, and was contained by the masthead casting when it was normally in place.

To extend the RTE wiring harness, a 5-conductor cable, I ended up using the same 14/5 cable that I’d run through the boat for this purpose earlier, which meant that wiring connection at the terminal block in the boat would be straightforward same color to same color.  This cable was heavier and larger than I wanted, but options were few and far between, at least with any products I’d trust and that were available in less than 1000′ parcels.  As least I knew it was quality wire.  Somewhere there must be a source for tinned 5-conductor cable in smaller gauge sizes and nominal overall diameters, but I couldn’t find it and after a time further looking was only wasteful.

In the event, I connected the new wire to the existing harness, noting again the color conversions between the two, and for added longevity and strength within the mast, I added a sheath of heat shrink over the entire splice.

I chose to use the existing wires (which had powered a tricolor masthead unit) to pull the new cable down from the top.  So I heavily taped the new harness to the old to help it on its way through whatever course it took down the top part of the mast.  In addition to the 14/5 cable, I also secured a new VHF cable to pull through the mast and replace the existing.

The wires from the masthead ended up in a length of plastic conduit within the mast when they reached the steaming light location at the spreaders, along with the three-wire harness from this light.  The conduit slipped over an extruded lip on the inside of the mast, and therefore was removable as a whole.  At the steaming light, I secured a length of messenger line to the existing wires before starting to pull out the entire harness.

mast5-42016

From there, it was relatively simple to pull out the conduit and old wires from the bottom.  The new harness fed in fairly easily from the top once I got it going, which suggested it had an unimpeded path through the spar.

I left some slack in the masthead wires just below the top of the mast to allow the masthead casting to be removed for sheave access in the future, then resecured the masthead–with RTE and VHF extension attached–back in place before making up the end of the VHF cable as required.  After photos, I removed the VHF antenna for safekeeping, but the RTE was now a permanent fixture by virtue of its hardwired and sealed construction.

Since it was straightforward to slip on the wire conduit afterwards, I went ahead and ran in the 14/3 wire for the steaming/deck light combo at the spreaders, and made up the wiring at the new LED fixture before installing the fixture with machine screws.  I left some wire slack bundled behind the fixture.

The masthead cable was too large to fit within the internal mast conduit along with the steaming light harness, so to secure it as much as possible I came up with a plan to secure it to the outside of the conduit with cable ties.  With the conduit out of the mast, at intervals I drilled holes at the outer edge to accept wire ties, and as I fed the conduit back into the mast and over the steaming light cable, I secured the thick masthead cable loosely in the wire ties–loose because they had to allow the conduit to slide up, while still securing the exterior cable tightly enough.  This actually worked better than I’d hoped.

I chose a location on the forward side of the mast for the wire outlet, which would eventually connect (via flexible conduit aka hose) with the deck fitting on the boat.  I drilled a hole for the wires to pass through and installed a rail mount base on the outside, which diameter matched that of the deck fitting (and hose).  Then I led through the wires.

After reinstalling the mast base casting, I measured generously for the final wire lengths, which had to pass through a length of hose/conduit, then through a path in the boat to the terminal blocks for final connection.  Since the terminal blocks were hidden from normal view, and because I wouldn’t be there to make up the wire lengths when the boat was rigged, I left what I thought (and hoped) was more than ample wire length to make up the connections without being ridiculously long.  The wires could always be shortened later if necessary, but at least they were ready to be connected as is.  I labeled the wires as necessary to match up with their respective connections in the boat.

Total time billed on this job today:  5.25 hours

0600 Weather Observation:
35°, clear.  Forecast for the day:  sunny, 50s

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