(page 147 of 166)

Waanderlust 2

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Tuesday

The owner shipped me the original bronze worm-drive centerboard winch, which mounted to the bulkhead above the galley on the port side.  While the exterior holes had been covered over by new paneling long before, the interior bolt holes and shaft hole were still in place to dictate the installation location.

Since part of the winch rested on the trim at the top edge of the bulkhead, I needed a block of corresponding thickness below to support the rest of the winch, so I cut an oversized blank from 3/4″ mahogany and, over two stages, scribed it to match the curvature of the trim, and narrowed the original blank to leave a consistent exposure on each side of the winch.  For now, I left the length long for later sizing and trimming.  I marked the location on the bulkhead with some pencil marks on tape.

Now I drilled through the cabin trunk from the inside, using the original winch shaft hole as a guide, penetrating the teak paneling on the exterior.  I also drilled the four bolt holes to secure the winch.  With the backing block held tightly in place in the right position, I marked the location of the large shaft hole from outside, so I could drill it in the backing block and then position the winch to mark and drill the final bolt holes as needed.

With the winch temporarily in place, I checked the fit of the handle, and marked the bottom of the mahogany backing block for its final dimension.  Back inside at the bench, I cut off the excess length from the block and shaped and sanded it to prepare for varnish, several sprayed coats of which I applied throughout the remainder of the day.

To help protect the inside of the shaft hole from moisture, I coated it with a thickened epoxy mixture.

cb13-51016

At the port after edge of the cabin trunk, over the past six years since the main exterior work had been completed (this project sat idle for many years between then and now), some cracking had formed where the plywood cabin trunk met the teak paneling at the cockpit bulkhead.  This was an area that had been worked on sometime before the boat ever came my way, and I’d not done any additional work here, other than the usual sanding and surface prep before priming and painting.  With extensive repair work going on elsewhere, the raised after portion of the coachroof was one of the areas that seemed sound and didn’t require resheathing, but in hindsight this seam should have been dealt with.  That said, it took six years to manifest itself in this cracking, so there you are.

This is how this area looked in May 2010, at the very beginning of the project.  Please feel free to review the original condition of this boat as well.

handrails-52010

Regardless of the reasons behind it, I didn’t want to leave it as is.  So I ground out and cleaned out the cracking as needed and filled the minor voids with a thickened epoxy mixture, which I left to cure in the hot sun.  I wasn’t going to fully cure the potential ills of this junction, but this repair would keep out water and hopefully prevent a recurrence.

I found that one of the breaker switches on the panel in the galley had been broken off, so I replaced the breaker with a new one, a quick process.  Meanwhile, I finalized prep work on a hull patch I’d made during the last work phase some months earlier, where I’d filled an old transducer hole in the bottom, and applied bottom paint over the epoxy repair.

bottom1-51016

 

 

Total time billed on this job today:  2.75 hours

0600 Weather Observation:  32°, clear.  Forecast for the day:  sunny, high in the mid-60s

Waanderlust 1

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Monday

Over the past week or two, I’d removed the winter cover and framework, and reinstalled the lifelines.  Now, with the boat open and available for work, I turned to some of the items on my very short list to finish up the project.  With minimal work at hand, I saw no reason to move Waanderlust indoors, and would complete the project outside.

waanderlust2-50916

First on my task list was to install a new composting toilet.  During the previous work phase on this project, I’d revamped the head compartment, creating a simple, clean, and open space for the new toilet.   The owner selected Nature’s Head, and in due course I ordered the unit and unpacked it at the shop.

head1-50916

Installation in this case was pleasingly straightforward.  The toilet was self-contained, perhaps the greatest advantage to composters, and there was ample room for it in the fairly large head compartment.  Even better, there was already a cowl vent and quasi-Dorade box overhead, making for a convenient location for the required venting system for the toilet.  To begin, I installed the supplied plastic hose connection flange over the opening in the overhead with screws and, to avoid any nuisance water that might enter the vent above, sealant.

head2-50916

Following the directions, I installed the toilet to the plywood floor with the supplied brackets, mounting it 1-1/2″ from the bulkhead (which allowed the lid to tip up and rest comfortably, and provided enough room to tip back the top part of the toilet for inspection and removal of the top for interior service).

There was a small 12V fan built into the side of the toilet, and to this housing I attached the supplied length of hose and ran it to the overhead vent.

The fan featured a one-prong power plug and harness, which allowed convenient disconnection for when the toilet required servicing or cleaning.  I ran the harness along the bulkhead and into an adjacent compartment, where I’d eventually connect it to a wire pair leading aft to the batteries.

This completed the installation work for the toilet itself.

Since the little fan needed to run all the time for proper usage, I chose to lead the wires directly to an “always hot” terminal bar that I’d installed previously for the electric bilge pump.  This terminal was powered whether or not the battery switch was turned on.  I ran in a wire pair along a pre-existing wire route through the engine room, galley, and behind the port berth, and made up the connections at each end as required, incorporating a fuse at the hot end.

To cover the interior opening of the second cowl vent through the overhead, located at the forward end of the main cabin, I installed a metal vent screen.

vent1-50916

In other news, my upholstery contractor had recently completed and installed new interior cushions for the boat, which looked terrific and really finished off the clean, bright interior.

Total time billed on this job today:  3.25 hours

0600 Weather Observation:
33°, clear.  Forecast for the day:  Mostly sunny, windy, high in the low 50s

Precision 10

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Friday

The steaming light (officially called a masthead light regardless of position) on the mast near the spreaders required new wiring, or at least new wiring seemed prudent since it would be simple to do and the old wiring’s condition was unknown.  I removed the light from the mast, noting the wire color conventions and placement of the terminals, then pulled in a new length of 14/2 wire, using the old wire to do the job.

Next, I made up the light end of the wires, installing new ring terminals to the light fixture and reinstalling the fixture to the front of the mast.   Then, I stripped the wire ends at the bottom and temporarily hooked them to a battery so I could check the light’s operation:  all good.

At the bottom end, I left enough wire slack and made up the end to the existing 2-prong plug, which mated with the one on deck.  I double-checked the wiring conventions in each case to ensure that the plug polarity would be correct.

Now I put the mast back on deck, supporting it on the pulpits as it’d been upon arrival, and strung new wire lifelines through the stanchions.  This completed my current task list, though the new cushions were still in production and would be ready in a couple weeks, probably.

Total time billed on this job today:   2.5 hours

0600 Weather Observation:
42°, cloudy.  Forecast for the day:  decreasing clouds (so they say), high in the  60s.  Dare we hope?  It’s been a dismal week.

Precision 9

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Thursday

It’d been a busy week filled with other (unrelated) complications that limited my time in the shop, but fortunately this project was winding down anyway, with only a few tasks remaining on the list before completion.

To begin, I painted the bottom with  black bottom paint, removing the masking tape afterwards.

With a raw and miserable, and wet-ish, day outside, later on I moved the mast indoors next to the boat so I could get started on the work required.  The two new halyards had arrived from the rigger, along with replacement lifelines, so I strung in the new halyards, using the messenger lines I’d installed when removing the old ones at the beginning of the project.

The old VHF cable to the masthead was shot, at least at the bottom end, so I prepared to run in a new one.  I tried using the old cable to pull through the new, but the way the exit hole at the top of the mast was, the cable didn’t pull in cleanly, and the old cable parted from the tape I’d used to secure the two together, so instead I had to use a wire snake pushed down the mast to string a messenger line, which line I then used to pull through the new cable from top to bottom.  Then, I made up the ends, completing that assembly.

All that remained was to rewire the masthead (by technical definition) located near the spreaders, but I’d do that next time.

Total time billed on this job today:  2.75 hours

0600 Weather Observation:
44°, clouds and drizzle.  Forecast for the day:  44°, clouds and drizzle.

lh7

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Wednesday

With the season around the corner, and the owner’s launch date a week or so hence, we made arrangements to get together and install the new sail track systems on both masts.  Earlier, we’d done all the required measuring, obtaining the internal track size specifications and overall lengths for the two tracks, and the owner had subsequently ordered them.  With the masts removed from their indoor storage shed by the boatyard, we could wrap up the installation.  I took few pictures, unfortunately, remembering only at the end when the tracks were complete.

Along with the new track on the mizzen mast, the owner wanted to lower the gooseneck (and therefore the boom) for easier access from the cockpit.  The boom height had been surprisingly (and, frankly, inconveniently/dangerously) high from a practical standpoint, making furling and covering the sail a real hassle, and with ample headroom beneath, there was no reason other than aesthetics (the mizzen boom height, as original, was sort of tied in with the main boom height so they looked visually level) not to lower the boom.  Since the old mizzen sail was a rag in poor condition, and lacking battens, the owner wanted a new sail made anyway, so it was the perfect opportunity to move the boom height.

I started by removing the mizzen gooseneck, as its existing position was in the way of the track.  Then, I had to use a Dremel tool to open up the mast slot a couple feet above the gooseneck, where the track would actually be installed; the existing slot was too short by half, and was open only on one side of the slot.  I’d opened up part of a slot on the mainmast much earlier, in order to fit one of the old sail slides at the time, so I was already familiar with the process.  Fortunately, the cutting went well and quickly, and we were soon able to install the track in accordance with the instructions.  The installation went swimmingly, and afterwards, I reinstalled the gooseneck a foot or so lower, at a location we’d determined previously.  We’d carefully measured the track so the track as provided was the exactly correct length.

Moving on to the mainmast, I also had to open up the second side of the existing track slot, as this one was open only on one side as well.  With that complete, we installed the track, which went just as well as the smaller one on the mizzen mast.  I didn’t have to remove the gooseneck in this case.  Overall, the installation on both masts, including setup and opening the mast slots as needed, went much more quickly than I’d ever hoped, taking only about two hours.

I wrapped up my end of this project with a couple odds and ends, including restringing the top line of the main’s lazy jack system, which I’d rigged incorrectly the year before, and installing some new registration numbers on the bow for the owner.

Total time billed on this job today:  2.5 hours

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0600 Weather Observation:
45°, cloudy.  Forecast for  the days:  clouds, maybe a shower, high in the low 50s or upper 40s

Precision 8

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Tuesday

As the work list wound down, I turned to one of the last jobs:  replacing the boottop.  The original, made from vinyl tape, was in poor condition.

With a heat gun, I removed the old striping tape.  This took a long time since the old tape was so scarred and damaged, and it wasn’t possible to release and pull large sections, so it required plenty of scraping with a putty knife.  This also left behind quite a bit of adhesive.

I used solvent and elbow grease to remove the old adhesive left behind.

Afterwards, I applied a new stripe from 2″ vinyl striping tape, like the original.

With other commitments, I’d had a late start and there was only a bit of time left in the day, so I used it to prepare the bottom for painting, first masking off the waterline as needed.

The trailer had keel guides, which blocked most of the keel, so I removed them for painting access.  I’d await the painting till next time.

 

Total time billed on this job today:  4.5 hours

0600 Weather Observation:
44°, cloudy.  Forecast for the day:  Mostly cloudy, high in the 50s

Precision 7

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Monday

Back at work after a long weekend, I found various new supplies on hand that I’d ordered earlier, so I got started with what I thought would be the simplest task:  installing the new 6″ light fixture in the forward cabin, which I’d ordered after finding that the original was rusted and inoperable.  Double-checking, I powered up the boat’s circuits and used a meter again on the exposed wires, getting the appropriate reading, so I connected the wires from the light fixture, only to find that it didn’t work.  It took a few moments for me to realize that (silly me) I’d assumed that the red wire coming off the light was positive, and the black negative.  As it happened, the wiring convention on this fixture was backwards, which a simple glance at the way the wires ran through the switch would have revealed, but one becomes quite conditioned to normal wire colors and their supposed meanings.

With the wiring reversed, the light operated, and I secured it to the overhead with screws, as per the original.  This fixture also hid the wiring passing through the deck to the mast lighting.

Next, I turned to the scuppers.  All parts were now on hand, so I completed the installation by installing the screened cockpit fittings along with elbows and hose adapters so I could lead hoses the short distance to the transom outlets.  I debated crossing the hoses  but found that I could get short lengths on to keep the drainage as short and direct as possible.  Before final installation, I cut off excess thread length from the cockpit fittings to keep the elbows as close to the cockpit as possible.  I installed the cockpit fittings in beds of sealant in their newly-built recesses.

Afterwards, I installed the plastic access hatch with machine screws and sealant.

Before it slipped my mind, I went ahead and installed the knotmeter impeller in its new through hull–the impeller was removable from inside for cleaning, ostensibly.  I’d left this out during initial through hull installation and until the sealant had had adequate cure time.

The new outboard motor bracket pad had arrived, and I installed it.

bracket1-50216

My new cover plate for the instrument installation was complete, the new paint having had several days’ cure time, so I installed it over the old openings with screws and sealant, centering the new instrument holes over the old ones for access within.

instruments3-50216

Now I installed the two new instruments, securing them with the supplied clamps from behind, and made up the final wiring connections–power and transducer cables in each case.  I found I could run these wires through a space between the fiberglass bulkhead and the wooden interior of the bulkhead for a clean appearance.

During an earlier wiring session, I’d run wire blanks from the nearby fuse panel for these instruments, and now I made up the final connections and secured the excess transducer cables out of the way beneath the cockpit.  The instruments tested operational.

To complete the installation, I installed a teak cover over the interior side of the instruments.  I had to build the original plywood cover out slightly to clear the wiring leads at the back of the instruments, but otherwise it was a clean interior appearance with no exposed instrument wires.

To access the underside of the galley sink and its supply faucet, I had to cut an access hole from the cabin, which I did now that I had the new access port on hand.

sink4-50216

 

The supply fitting on the portable water tank was broken, and lacked a dip tube/hose to actually draw water from the tank, so I replaced the fitting with a new one that I luckily happened to have on hand, and fitted in a flexible dip tube to the bottom of the tank.  Then, I led a new supply hose between the tank and the sink faucet, and, to wrap up the work, installed the new plastic inspection port in the opening beneath the sink.

Total time billed on this job today:  5.75 hours

0600 Weather Observation:
41°, clouds and showers.  Forecast for the day:  showers and rain, 40s

Precision 6

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Thursday

After some other business away from the shop, I got to work again on the scuppers.  The epoxy had cured overnight, leaving my new recesses ready to go.  The screened fitting fit flush and finely.

I was awaiting delivery of the second fitting–I only had one on hand–as well as some elbows I needed below the deck, so for the moment I held off on installation.  I did install the two exit through hulls in the transom, completing that side of the new drainage system.

Next, I continued work on the electrical system.  I hooked up a battery so I could start to check the various circuits for operation.  Most of the lights on the boat–two of three cabin lights, plus the bow and stern lights–operated when tested, but the forward cabin light turned out to be rusted within and was missing its switch, and therefore inoperable.  I removed the damaged fixture and ordered a replacement light.

The owner reported that the VHF was inoperable, and after some troubleshooting and testing I traced the electrical problem to a bad fuse holder near the radio, which I replaced.  This process also highlighted some issues with the existing fuse holder block on the port side of the boat, which serviced the VHF as well as the depthsounder and knotmeter (old as well as the new), and I couldn’t determine the issue, so I simply replaced the fuse holder/terminal block with a new one that I had on hand, and redid the short wire runs for the depthsounder and knotmeter, running them through an existing switch so they could be turned off as needed.  At the same time, I secured a 12-volt outlet to a nearby structural member, and cleaned up the wiring pending final installation of the instruments a little later.  Everything tested operational once I’d made these changes.

To ensure that I could complete the new instruments’ installation soon, I continued work on the exterior cover panel where they’d be mounted.  I lightly sanded the primer that I applied earlier, then during the day spray-applied several coats of off-white LPU to generally match, or at least be consistent with, the existing deck surfaces.

panel1-42816

The wiring to the single mast light led through the deck forward of the mast step, and was hidden beneath the forward cabin light fixture (the one that didn’t work and I’d removed).  I couldn’t get power to the plug above deck, so I looked into the issue further and eventually removed the existing wiring through the deck, cutting off several old extensions and rewires from the past till I had the basic wires remaining.  Digging into the old wire harness leading to the mast light plug, I found that red connected to green, and black to white, so now I knew which wires were which inside the boat and could make up a connection to a new wire pair, which I led above deck through the existing cable clam and reconnected to the old 2-way plug for ease of mast stepping and unstepping.  With the meter, these wires tested operational.  Later, I’d redo the mast side of the lighting circuit as required, but this completed the boat side troubleshooting and testing, and repairs as needed.

Total time billed on this job today:  4.25

0600 Weather Observation:
Clear, 22°.  Forecast for the day:  Sunny, 50s

Salty 46

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Wednesday

In the near future, I wanted the chance to test-run the new engine, and this need, along with other obligations requiring the inside of the shop, meant that, now that all the work was otherwise complete (excepting the new propeller shaft and engine startup), it was time to move Salty outdoors for storage and the duration of the final stages of the project.  The boat wouldn’t be leaving here for a couple months, so to ensure access to other boats in storage I set her down in an out-of-the way location, but readily accessible to the shop for the final work as needed.  I offset the jackstands so I could easily paint the last patches of the bottom.

Total time billed on this job today:  1 hour

0600 Weather Observation:
Clear, foggy, frosty, 22°.  Forecast for the day:  sunny, 50

Precision 5

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Wednesday

To access the aftermost part of the boat and the cockpit scuppers, the best way in seemed to be through the aft bulkhead in the cockpit, which would give access to the transom as well as the cockpit sole fittings.  There was an existing access port there, but it was far too small for real access.  To begin, I marked the bulkhead using the cardboard template of the cutout that I made earlier.   With a 4″ hole saw, I made the 2″ radius cuts at the corners, then connected them with a saw to create the opening.  The new opening gave quite good access to the required areas.  Note that the original access port was not quite centered.

Next, I removed the old pipe and fittings.  The cockpit side was already loose and took only a push from the top; the gobs of sealant securing the pipes to and through the transom were quite resilient, but eventually I got them loose and the pipes removed.

The bulkhead had a slight concave curve to its shape at the top of the new opening, and it was too severe to bend the new hatch into position.  The bottom edge, and the vertical sides, were flat enough for a successful fit, but I needed to build a filler piece for the top to properly support the hatch and fill the gap.  From teak stock, I scribed and cut  a curved piece to fit; I’d await final installation of the hatch till I was done with all the scupper work, since the raw opening was quite a bit larger than the hatch itself.

To rebuild the scuppers, I planned on new fittings at transom and cockpit sole, connected with hose to create a more flexible situation than the original pipe.  For the cockpit, I selected Marelon fittings with a built-in screen.  To provide complete drainage, I had to recess the mushroom fittings so they were flush with or beneath the sole surface.  Since the laminate was no thicker than the thickness of the mushroom heads, I’d need to basically build a new supporting surface beneath the sole for the fittings.  The original holes were the right size for the threads, but too small for the heads.  So to open up the holes, I hot-glued some plywood beneath the openings, to give the hole saw pilot bit a guide, then used a larger hole saw to increase the diameter of the openings.

This allowed the mushroom head to fit flush through the sole.

scuppers11-42716

To support the fitting below the sole, I used some circular cutouts from 1/4″ fiberglass, into which I drilled holes the right size for the fittings’ threaded necks.  After cleaning up and sanding as flush as possible the bearing surfaces below the openings, I epoxied these discs in place, aligning the holes in the center.  This effectively provided a “molded” flat-bottomed recess in the sole that would fit the scupper fittings cleanly.  I made the epoxy mixture thick enough that it held the discs in place on its own, but to be sure that I continued to thwart gravity long enough for the epoxy to cure, I added some tape as a backup.

I also sealed the plywood edges of the transom cutouts with the thickened epoxy.  Now I’d wait for all the epoxy to cure before I continued with work on the scuppers.

scuppers15-42716

To cover the large holes left over from the old round instruments, I built a simple exterior panel from 1/8″ fiberglass laminate, which I cut to the angles required to tie in with the shape of the companionway and cabin top.  After marking its position as needed, I drilled 2-1/8″ holes to accommodate the new instruments, then applied a few coats of epoxy primer during the remainder of the afternoon.

For the inside cover panel, I cut teak plywood to fit as needed, which blended well with the existing plywood cover on the bulkhead.

covers4-42716

With the new instruments and transducers now on hand, I went ahead with the installation of the transducers (depth and speed), using the original holes in the boat, which I’d already prepared for the installation.

Then, I led the cables aft, following the same route and using the same support hardware as the original cables that I’d just removed.  I’d make the final connections to the new instruments later, once the cover panels were done and ready for installation.

I finished up the minor keel work with a quick wash and sand of the filler I’d applied earlier.

I’d moved some other boats around, which gave me the opportunity to reposition this boat alone in the center of the shop for better access for the remainder of the project.

shop1-42716

Total time billed on this job today:  6.25 hours

0600 Weather Observation:
Clear, foggy, frosty, 22°.  Forecast for the day:  sunny, 50

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