(page 144 of 165)

Patience 8

< Back to Patience

Wednesday

After a quick water wash, I lightly sanded the new patch over the knotmeter through-hull hole, sanding it flush on the outside as needed.  Then, I applied a coat of fairing filler over the area, leaving it to cure overnight.

With the epoxy coating on the bottom sides of the cabin sole panels now cured, I turned them over and sanded the top surfaces to smooth them as needed.  Then, after cleaning up and solvent-wash, I applied a coat of primer to the panels.

I installed the new bilge pump on its platform, and the float switch in the keel sump, then began some of the wiring, leading a new 2-conductor wire between the bilge and the compartment containing the pump, and making up the various connections in the bilge area between the switch, pump, and an existing wire leading to the battery compartment.   In this case, there was really no way to avoid having wires running through the bilge compartment, but I kept the wires as high as possible with wire clamps.  The old pump had been wired directly to the battery without a separate on/off switch, so I’d finish up power wiring and wiring to the new panel switch next time, along with the pump hose connections.

Total time billed on this job today:  4.5 hours

0600 Weather Observation:
58°, foggy.  Forecast for the day:  Becoming partly sunny, high 73°

 

Waanderlust 7

< Back to Waanderlust

Monday

Though the project was essentially complete, I’d continue minor work as new  hardware arrivals trickled in for the mast.  Today’s arrival was the VHF antenna, which I test-fit, then inverted in its bracket for storage and transport.

0600 Weather Observation:
42°, sunny.  Forecast for the day:  mainly sunny, some increasing clouds in the afternoon, high in the 70s

Patience 7

< Back to Patience

Tuesday

To prepare the old knotmeter through hull hole for patching, I ground the exterior to remove paint and taper back the laminate accordingly, as needed to install new flush fiberglass to cover the opening. This area of the hull was solid fiberglass with no core.  Inside, I sanded away the interior gelcoat/paint to bare fiberglass.  Then, I masked over the opening from inside, and filled the round hole with a thickened epoxy mixture.

A bit later, the epoxy plug had cured to the green stage, and I applied three layers of fiberglass in epoxy resin from the outside, and a layer on the inside to complete the structural patch.

To replace the ailing and ineffective self-contained bilge pump in the keel sump–which operation was hampered by the long hose run to the transom–the owner selected, at my suggestion, a remote-located diaphragm pump that would be more effective at dewatering and would avoid backflow issues into the tiny sump that we thought had kept the pump running too frequently during the previous season.  Because of where the existing discharge hose led (which I’d installed the year before), and also because it was a good location on its own, I chose to locate the new pump in a roomy storage space beneath the port settee.

After ensuring there was ample headroom for the pump, I prepared a basic cardboard template of the platform required, which would run between an internal structural member and the nearby hull for support.  I positioned and sized the platform to avoid the existing hoses and the hole through the structural stringer that led to the sump, and through which I’d run the suction hose.

From the template, I cut a platform from marine plywood, and after a test-fit and dry run with two fasteners on the inside, I epoxy-coated the bottom side and edges, then secured the platform in place with epoxy adhesive where it met the hull, and a pair of screws (and a little epoxy) at the inside.  Finally, with the platform in place, I epoxy-coated the top surface as well.

To give me a mounting location for the float switch that I’d install in the keel sump (thus avoiding fasteners directly into the bottom of the sump), I epoxied in a small fiberglass block, which I’d pre-drilled to accept the float switch later.

bilge6-52416

As it happened, there was a large hole in the starboard bulkhead just below the electrical service panel, where some old control panel had been installed, and this seemed a good location for the new bilge pump switch.  I cut a piece of teak plywood large enough to cover the old opening, and installed the new switch in the teak panel, which would cover the old hole and provide a convenient mounting spot for wiring and operation.

bilge7-52416

Down in the shop, I used the existing cabin sole pieces as exact patterns to cut new 12mm marine plywood to the correct sizes.  The largest piece, the aftermost one, had its bottom side routed out in way of the support cleats inside the boat, which I didn’t plan to emulate unless I absolutely had to.  At the moment, I could see no reason for lowering the apparent height of the aft piece.

Once I had the pieces trimmed to size as needed, and tapered to fit the hull (the small forward section only), I test-fit all three in the boat.  All fit well without a need for further trimming.

With the sole panels back on the bench, I prepared support cleats for the small access hatch over the bilge sump, and secured them in place with epoxy adhesive and temporary fasteners.  Then, I epoxy-coated the bottom sides and edges of the plywood panels.

Total time billed on this job today:  6.5 hours

0600 Weather Report:
58°, cloudy.  Forecast for the day:  clouds, maybe showers in the afternoon, low 60s

Precision 11

< Back to Precision 23

Monday

The final item outstanding from the original project list was new interior cushions, and these were now complete and looked terrific.  The color is sapphire blue.

< Back to Precision 23

Patience 6

< Back to Patience

Monday

I lightly sanded the first coat on the boottop stripes, then vacuumed, solvent-washed, and tacked off before applying a second coat of the bright red and light blue paints.

Meanwhile, I continued work on the new halyard stoppers on the cabin top.  The epoxy plugs had had the weekend to cure, and now I drilled for the new fixing bolts, and installed the new hardware in butyl sealant, which was a good choice in this instance since the hardware specifically admonished against using other common sealants.

There was a defunct knotmeter transducer in the boat, which the owner requested I removed and patch.

From inside, I removed the plug itself, then cut away the plastic housing and, from outside, removed the through hull flange.  Later, I’d prepare the hole and fill and patch to complete the job.

The original cabin sole, made from teak-veneer plywood, was in poor-ish condition, and the owner requested I replace it with new painted panels.  So I removed the old panels from the boat so I could pattern them and build the new pieces forthwith.

I also removed a stand-alone automatic bilge pump, which I’d soon be replacing with a remotely-located diaphragm pump.

By the end of the day, the new boottop paint had tacked up sufficiently to allow me to remove the masking tape.  Now I’d leave the fresh paint for a few days before I considered overmasking it to paint the white striped between.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:
42°, sunny.  Forecast for the day:  mainly sunny, some increasing clouds in the afternoon, high in the 70s

Waanderlust 6

< Back to Waanderlust

Friday

I finished up the mast electrical trim-out with the steaming light (actually called a masthead light), located on the front of the mast below the spreaders.  This light required a mounting bracket that I secured to the mast with screws.  As with the anchor light at the top of the mast, I replaced the stock incandescent bulb with an LED version.

Afterwards, I finished up the wiring at the masthead with a VHF connector (the antenna was due soon), and at the mast base by making up the ends of the two sets of wires (labeled and numbered according to their function for ease of connection to the terminal block belowdecks).

LED bulbs like this have distinct polarity, meaning the bulb only works when inserted correctly.  And indeed, inevitably, when I tested the two new fixtures with a battery, I found that in both cases I had to turn the bulbs over in order to get them to light.

This completed the mast work for now.  I had new halyard winches on the way, and would complete their installation upon arrival.

With good weather forecast all day, I finished up the little coachroof repair.  After masking off the surrounding areas to protect against overspray, and other final preparations, I spray-applied several coats of off-white LPU mixed with a flattening agent to match the remaining areas of the deck.

Total time billed on this job today:  2 hours

0600 Weather Observation:
48°, mostly clear.  Forecast for the day:  mainly sunny, 76°

Patience 5

< Back to Patience

Friday

After finishing up some work on another boat, and awaiting a shipment paint later in the day, I turned to the halyard stoppers located on the cabin trunk.  There were four of these, and they appeared original.  The owner requested replacement.

Removal was straightforward.  The barrel nuts on the interior had been painted over, but fortunately came off without issue, and soon the old hardware was removed.

The new stoppers were essentially identical to the old, with the same bolt pattern.  I extend my congratulations to Spinlock for not changing something just for the sake of change, even decades later.

After cleaning old sealant and debris from the deck, I used a 5/8″ bit to overbore the old bolt holes, removing the top skin and core at each location.  The core (plywood) was in good condition in all areas.  Drilling this deck, which was fabricated from Kevlar cloth, brought back lots of memories from my first boatbuilding job in 1990, at a well-known builder that was, at the time, experimenting with Kevlar and E-glass hybrids.  My enduring memory of Kevlar cloth was the fuzzy nature of the material whenever one cut the raw cloth, or sanded/cut the finished laminate, and the fuzzy bits that came up as I drilled into this deck now just reminded me of it all, oh so long ago.

Once I had the holes cleaned up, and masked over the bottom openings, I filled the holes with a thickened epoxy mixture, leaving it to cure before continuing.

My new paint for the boottop arrived just in time, and I looked forward to getting the first coat on.  The owner had a clear sense of the color scheme he wanted, but working with online color samples (notoriously inaccurate) we’d eventually decided to purchase two different shades of the blue he hoped for.  The first shade that arrived looked a close match to the samples, but might have been too light on the boat itself, so I’d ordered the next-darker shade, called Sky Blue.  When this arrived, I thought it looked like the right color for the main, wide stripe of the boottop.  The narrow upper stripe was to be bright red.

paint

After final preparations, and starting with the red on the uppermost stripe, I applied the first coat of paint to the boottop, finishing up with the sky blue on the lower stripe once the red was done.  To my eye this all looked pretty good.

Total time billed on this job today:  3.5 hours

0600 Weather Observation:
48°, mostly clear.  Forecast for the day:  mainly sunny, 76°

Waanderlust 5

< Back to Waanderlust

Thursday

In 2011, after reconfiguring the galley and engine room spaces in this boat (the original area had been completely rotted out), I installed a new Beta 25 diesel engine in this boat (during  Phase III of the project), but the engine had sat idle and untested until now.  With various factors and complications at hand, the owner had put the entire project on hold shortly after the engine installation, with work only resuming in fall 2015 and, of course, now.  The long delay had not been anticipated at the time.

So, five years later, I looked forward to finally test-firing this “new” engine.  I started by adding fuel (6 gallons to the new tank), coolant, and oil as needed, and checked the raw water pump impeller to inspect its condition.  I filled the fuel filter with clean diesel, and bled the engine at the secondary fuel filter until I got clear fuel from the bleed screw.  (14mm)  This is a really nice engine room, if I do say so.  Roomy and with outstanding access to the engine.  This made all the preparation and testing work a real pleasure.

With all initial preparations complete, I started the engine.  It started right away, and nearly kept running, but there was still air for it to work through its system.  The second time, the engine kept running, even as it worked through a few air-related fuel hiccups, as per usual.

After running the engine for a couple minutes, I shut down in order to check the fluid levels.  I added a bit of coolant and engine oil as needed to top up the levels once more.  Then, I proceeded through a longer engine test, which I recorded in the following videos.  I found that the new engine control was loose, and allowing the engine speed to change on its own, so after a while I stopped the engine again and adjusted the control as needed, after which I could actually leave things alone without holding the control lever or manipulating the lever on the engine itself.

The test was a  complete success, and after running the engine up to temperature and for about 20-30 minutes’ total time, I shut down, with the last major check mark off my work list.

After cleaning up and buttoning up the boat again, I turned to the new mast, which required a couple lights and a VHF antenna.  All the wiring was pre-installed by the mast builder, but it was up to me to source and install the fixtures.

The wiring at the masthead exited the spar (by necessity) just below the halyard sheaves, and to improve appearance and secure the wiring on its way to the ultimate masthead, I sheathed it in some flexible conduit and secured it to the spar in a couple places with rubber-lined clamps.

mast1-51916

During a brief rain delay, I unpackaged the new fixtures (the VHF antenna was backordered briefly) and changed out the incandescent light bulbs for some new LED bulbs that I purchased for the purpose.

After the rain shower ended, I got back to work on the anchor light at the masthead, which I installed on top of the masthead strap.  I repurposed one of the screws securing this strap, and used it to also secure the light fixture, and added a second screw (with spacers beneath each to allow room for wiring) to finalize the installation.  I made up the wire ends and secured the screw-on lens for the fixture.

I’d continue with the VHF antenna and the steaming light, along with the wiring at the mast base, next time.

Total time billed on this job today:  3.75 hours

0600 Weather Observation:
40°, mostly clear.  Forecast for the day:  sun and clouds, showers in the afternoon, 60s

Patience 4

< Back to Patience

Thursday

Starting from the existing top line, which I’d struck and masked earlier, I worked my way down the various boottop stripes, lowering my beams at each end the proper amount to strike each line in turn.  Once I’d made the tick marks for each stripe, I masked off the line accordingly.

The first new line, representing the bottom edge of the top stripe, was 3/4″ below the topmost line.

The next line, representing the bottom edge of a hull-color band, and the top edge of the lower, wider colored stripe, was a further 3/4″ down.

The final line, representing the bottom edge of the wider stripe, was 2-1/2″ below that, leaving a 1″ band of hull color above the bottom.

With all the masking completed, there was finally a reasonable visual sense of the new striping, and it looked great.

We were still finalizing the paint colors, and awaiting some of the product, so with another boat awaiting my attention I moved on to other things for now.

Total time billed on this job today:  4 hours

0600 Weather Observation:
40°, mostly clear.  Forecast for the day:  sun and clouds, showers in the afternoon, 60s

Salty 49

< Back to Salty

Wednesday

After one final, hopeful, yet unsuccessful attempt to somehow twist the new propeller onto the shaft in the tiny space before the rudder, I gave in and went up and removed the flexible coupling from the shaft.  This gave me additional space to slide the shaft forward, which allowed me to get the prop into position without removing the rudder.  Then, I slid the shaft  (with prop loosely in place) as far aft as possible so I could reconnect the couplings inside.

prop1-51816

Afterwards, with the couplings reinstalled and bolted tightly into place, I finished up the propeller installation by securing it in place with its nuts and cotter pin.  The propeller size is 11RH6.

Now, I prepared the engine for its initial firing by adding fluids as needed:  engine oil and coolant.  Fuel had partially filled the fuel filter by gravity from the tank since I’d made those connections, but I added more fuel to the filter to fill it to the top.  I installed the start battery, and prepared a temporary cooling water intake line with a length of hose and a bucket.

With everything in place, I bled the engine at the secondary fuel filter, using the engine’s built-in pump lever to prime the system till I got fuel (and air) out of the bleed screw at the top.  (14mm)  Once I saw relatively clear fuel, it was time to fire the engine.  I knew from past experience that these engines were almost completely self-bleeding, so there was no need to chase fuel through the rest of the system.

Once I started the engine, it took a few times to get it to run properly as it worked fuel and air through its system.  After two starting attempts–the engine started, but wouldn’t run for long–I rebled the fuel system at the secondary filter, and afterwards the engine stayed running once I’d started it.  Easy peasy.

After running the engine for a few minutes, I shut down so I could check the fluid levels again.  Both oil and coolant were fine and I didn’t need to add any.  With this check complete, I started the engine again for a longer run.  The three videos below show various stages of the process.

Sorry about the bad reflection on the battery monitor in the video above.  These photos show the battery charging amps at higher speed and again at idle speed.

With the successful test firing behind me, the job was complete, and I spent the last minutes of the day cleaning up a bit and putting the boat back together.  I installed the raw water strainer and its hoses, and buttoned up the engine compartment.

I left the engine raw water seacock closed, and since I wouldn’t be there at launching, to help future operators remember to open the seacock before starting the engine I hung the engine keys right on the seacock (located at the forward end of the engine room and accessed from the panel behind the companionway).

shutdown3-51816

I installed the engine hatch with four screws (out of a total of about 12) so it’d be secured during transport, but easy enough to remove at launching to check the stuffing box and engine.

Total time billed on this  job today:  5.25 hours

0600 Weather Observation:
40°, clear.  Forecast for the day:  mainly sunny, 60

Older posts Newer posts