(page 121 of 165)

Jasmine 4

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Tuesday

With substantial deck work and eventual refinishing on the way, my first step was to remove deck hardware.  I began, as usual, at the stem and worked my way aft.  From inside the almost comfortably roomy chainlocker, I removed the nuts from the fasteners securing the manual anchor windlass above, along with those from the bow cleats.  Fortunately, these nuts came free without spinning the fasteners, even though the windlass bolts were a couple inches too long with lots of exposed thread.

Back on deck, I removed the windlass and cleats, along with the fasteners.    The chain stripper associated with the windlass was nearly completely rusted away.  The platform itself was in atrocious condition at the after end.

I removed the bow pulpit, which was bolted through the outward flange of the hull/deck joint and toerail, making the fasteners easy to access.  The central forward stanchion of the pulpit was secured into the bronze stem fitting at the end of the bow platform with a single bolt, and this was straightforward to remove.  I also removed the bow chocks, which I realized belatedly was unnecessary since they were on the rail and not in the way of deck work, along with an anchor hawse and some wooden blocking on the port side.

Removing the windlass highlighted the extremely poor condition of the wooden bow platform:  the after end was completely rotten and unsound, and compressed and flaked away easily under light (or no) pressure.  I’d been aware that the platform’s condition was sketchy, but hadn’t understood quite to what extent.  It was abysmal.  With the windlass and its bolts removed, I could have easily pulled away most of the after portion of the wood by hand had I so chosen, but I hoped to keep the platform as intact as possible to aid in templating a replacement later.

In order to remove the platform, I had to unhook the solid rod bobstay beneath, which opposed the rigging pressures from the headstay when attached to the bronze casting at the far end of the platform.  The top fitting was semi buried in a tight space between the two aluminum anchor rollers at the end, and I couldn’t easily access the cotter pin nor spin the clevis to aid in removal.  In hindsight I should have just unbolted the pair of anchor rollers to remove them and access the pin, but at the time I preferred the thought of doing this later at my leisure, wanting more to simply get the platform off the boat.  So I removed the pins from the lower end of the bobstay, freeing it from the stem and also freeing the platform for removal.  The downside to this was that the platform was end-heavy, with all the hardware at the outer end, and the long, heavy, unwieldy bobstay only made things worse.  In the end this complicated removal, but didn’t prevent it and didn’t create any undue problems.

From belowdecks, I attempted briefly to remove the nuts from the platform fasteners, but it was clear the fasteners were all spinning freely in the remnants of rotted wood above, so instead I decided to simply lift the platform off the fasteners–pretty simple given that the wood was so rotted.  Before removal, I took a few moments to make a quick template of the shape of the top of the platform, in case the platform disintegrated complely during removal.

It only took a little prying from beneath before I could lift the outer end of the platform and free it completely from the deck.  The platform was quite heavy with all the hardware at the end, and the nearly 4′ long rigid bobstay was a pain in the neck, but without real issue I got the platform safely onto the foredeck, where I could regroup before lifting it more effectively and getting it to the staging, then eventually to the shop floor.

There was a substantial block of epoxy surrounding one of the after fastener holes, indicating that someone had tried to effect a band-aid repair when the platform had begun to deteriorate; there was also a huge blob of sealant at the after port edge, at deck level, where someone had filled in rotting wood with whatever came close to hand.    In any event, I removed the detritus and later, after cleaning up the wood scraps and dust, I cut off the bolts above decks and pushed them through the holes.

Now, wanting the bobstay out of the way completely, I had to go ahead and remove the anchor rollers from the end of the platform so I could remove the cotter pin and hammer out the extremely tight clevis from the top fitting, finally freeing the bobstay.  I set this aside for later inspection, then completed the removal of the bronze stem casting, which would be reused later.  The aluminum anchor rollers were in poor condition and had exacerbated (along with the aluminum anchor windlass) the deterioration of the wooden platform.  In any event, the owner planned for a new, single roller in the new installation.

Continuing aft, I turned to the first set of lifeline stanchions, a mismatched pair with a non-angled base on the port side, causing the stanchion to lean outwards.  Belowdecks, I removed some trim panels from the forward cabin to gain access to the stanchion bolts, which I removed without incident.

The forward cabin had a set of deadlights facing forward, along with a pair of aluminum opening ports.  From inside, I removed cap nuts from the fasteners, then carefully removed the screws from the outside.  I always keep track of screw locations when removing ports and deadlights on boats like this, as I’ve found that the fasteners are often different lengths depending on position.  Once I’d removed the screws, I carefully pried off the opening port trim rings, which were well-sealed with what was likely the original bedding compound, a soft, oily, flexible material roughly comparable to a mix between window glazing compound, plumbers putty, and butyl.  Effective and good stuff,  the likes of which I’ve not seen in modern products.

With the trim rings off (the trim rings were inside on the deadlights, which had the glass set in the outer frame), I removed the ports and deadlights from the forward cabin.  I’d clean off the excess sealant later.

To round out the day, I removed two hatch hinge bases from the forward side of the forward hatch.

Total time billed on this job today:  7.25 hours

0600 Weather Observation:  30°, mostly cloudy.  Forecast for the day:  Increasing clouds, showers, then rain into and through the overnight, temperatures rising into the 50s

Jasmine 3

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Monday

Earlier, I’d moved Jasmine from my secondary work bay and into the main shop, where I planned to complete the bulk of the project.

To begin, I set up staging around the boat at deck height to allow good access to all deck areas.

Ready to get to work in earnest on this project, I spent a little time first thing perusing various notes and emails to refresh myself on the scope of the project and various jobs ahead.  The main focus of the job in the coming weeks would be the deck, which featured several areas with known or suspect core issues and all the usual shortfalls of boats of this age.  In addition, my work list included a revamped electrical system, chainplate work, particularly on the mizzen mast, and some other related projects, plus installing a Norvane wind vane.   In addition, I’d be subcontracting a fair bit of rigging work to ensure the masts and their standing and running rigging were in good shape.  The net result of the project was to ensure a sound and safe vessel by taking care of these known and suspected issues.

Before beginning any real work, I thoroughly documented the existing condition of the decks and hardware for future reference.  These photos represent the overall condition of things, but I had many others on hand to show specifics on installations and initial condition.

I’d soon begin work on hardware removal, but first I had to clean out the cabin, which contained various boat parts, some sails, and miscellaneous equipment.

I needed clear access to all areas of the boat in order to effect the work ahead, and didn’t want anything unnecessary left behind to minimize worries about project dust and the like, so over the course of the afternoon, I removed and stored these items elsewhere in the shop to make room, leaving the way clear to begin the deck work next time.

Total time billed on this job today:  5 hours

0600 Weather Observation:  20°, clear.  Forecast for the day:  Sunny, 40s

Steadfast 29

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Monday

A few small jobs remained for me to take care of, starting with the reinstallation of the pilothouse door and its trim.  This was a straightforward process; I used new fasteners to secure the wooden trim back in place.  I also put back the newly-painted lazarette hatch.

The owner requested that I repaint the insides of the running light boards on the pilothouse; the existing paint was weathered and worn.  I removed the running lights from their brackets and the covers from the sockets, leaving the wiring in place, and prepared the black-painted boards with sandpaper and masking tape as needed so I could apply fresh black paint.

Late in the day, the first coat of paint had cured to the point that I could apply a second coat over the top.

The owner requested that I replicate and install  some logo stickers that had once been in place on the pilothouse, the ghost of which was still visible on one side.  I happened to have a plastic placard with the logo and text from a previous Fisher 30 project, so I dropped this off earlier with my local vinyl shop for reproduction in new vinyl, which I installed now.

I also took a moment to paint the patches where the jackstands had been originally; when I moved the boat, I’d staggered the stands to expose the unpainted patches for access.

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Total time billed on this job today:  1.5 hours

0600 Weather Observation:  20°, clear.  Forecast for the day:  Sunny, 40s

Steadfast 28

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Friday

My work on the brightwork was complete, and I spent the first part of the day removing all the masking tape.  I reinstalled the cockpit seats, and also some metal half-oval that I’d removed from one of the caprails.

The pilothouse door (exterior side) required another coat of the green paint, so after a light sanding and final preparations, I applied more.  For the lazarette hatch, to match the original finish, I mixed some rubberized nonskid particles into the paint and applied a nonskid coat to the top surface.

Earlier, I’d ordered and picked up new vinyl for the name and hailport according to the owner’s wishes (the font is Brittanic Bold), and now I applied these to the stern, using reference measurements I’d noted when I removed the original name at the beginning of the project.

Other than a few final details, this completed the work I’d been hired to do.  The owner had made arrangements with me to store the boat indoors during the winter, but I couldn’t keep her in my main work bay, so I spent the afternoon shuffling boats (I had first to move out a boat in the other bay to make room)  so I could move Steadfast into the other bay for comfy storage.  This gave a good opportunity to have a look at the refinished topsides from a distance, though the winter light was low  and hidden in a cloud bank, so failed to give a true sense of the vibrancy of the jade green hull.

Total time billed on this job today:  4.25 hours

0600 Weather Observation:  Clouds and a shower, 40°.  Forecast for the day:  Clearing, high near 50

Steadfast 27

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Thursday

I applied the third and last coat of finish to the brightwork during the morning.

Afterwards, I turned once again to the pilothouse door and lazarette hatch.  The hatch required a second coat of paint on all areas, and I turned the door over so I could paint the second (outside) side.

Total time billed on this job today:  3 hours

0600 Weather Observation:  20°, clear.  Forecast for the day:  sunny, increasing clouds in the afternoon, upper 30s

Steadfast 26

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Wednesday

During the morning, I applied the second coat of Cetol to the exterior woodwork.  Later, I spent some additional time running errands related to the project.

Total time billed on this job today:  4 hours

0600 Weather Observation:  40°, clear.  Forecast for the day:  Partly sunny, 50°

Steadfast 25

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Tuesday

I got right to work on the first coat of finish for the exterior woodwork.  The owner chose Cetol Lite for the finish, the same product that had been used previously.  On the various bits and pieces on the pilothouse and coachroof, I applied a maintenance coat over the existing finish, as I’d not stripped these areas.

For the caprails, I applied the first of three coats of the new finish, working my way around the boat up one side and down the other.

I continued with the bulwarks and rubrails on both sides, along with some loose parts including the cockpit seats and some trim from the pilothouse door.

The pilothouse door and a small lazarette hatch cover had been painted green in the past, matching the hull color.  The finish was weathered and worn, but generally sound on both parts, so preparation was a straightforward matter of light sanding and cleanup.  Afterwards, I painted the lazarette and the inside/back side of the pilothouse door with one-part green paint that matched the new hull color.

Total time billed on this job today:  5 hours

0600 Weather Observation:  12°, clear.  Forecast for the day:  sunny, 30s

Steadfast 24

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Monday

The owner requested that I remove and send to him the four round deadlights from the forward hull so he could have them rechromed, all the better to complement the freshly repainted hull.  So now that I had all the masking removed and once more had access inside the boat, I removed the frames and their backing rings.  The deadlights were secured through the hull with machine screws and nuts inside.  In some cases, I could remove the nuts without the fasteners spinning, but in other locations I had to secure the nuts inside with locking pliers and remove the screws from outside.

Once I’d removed all the fasteners, I carefully pried loose the external frames and glass to avoid any damage to the hull paint.  I packaged the frames up and shipped them to the owner, as he had a local shop ready to do the refinishing.

Next, I moved on to masking for the brightwork, starting at the top of the boat with the pilothouse roof, and working my way around the deck areas, masking around handrail supports, existing hardware, and against the decks as needed to prepare the woodwork for maintenance coats of finish (on the pilothouse and coachroof), and all-new finish on the caprails.  I removed the wooden cockpit seating areas so I could refinish them down on the bench.

With the decks masked, I continued on the hull, masking off the lower edge of the caprails bow and stern and around the bulwarks and rubrails to prepare for their new finish.  Afterwards, I wiped down all the woodwork with paint thinner to clean it one last time, so the wood would be ready for new finish next time.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:  29°, clear.  Forecast for the day:  Sunny, 40°

Steadfast 23

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Sunday

Over the long weekend, I unmasked the rest of the boat, including the bulwarks and deck areas.

Later, I masked off and painted the bottom with red antifouling paint to complete the  hull paint work.

Total time billed on this job today:  3.25 hours

0600 Weather Observation:  20°, clear.  Forecast for the day:  sunny, 40

Steadfast 22

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Thursday

With only a short time available before departing for Thanksgiving festivities, I still wanted to remove the masking to expose the fresh boottop, and during an early morning session I did just that, along with the plastic covering the topsides.  I’d take care of the remaining plastic and masking in the near future, after which I’d be ready to continue work on the brightwork.

Total time billed on this job today:  1 hour

0600 Weather Observation:  27°, clear.  Forecast for the day:  sunny with a chance of turkey, 37°

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