(page 107 of 167)

Dharma Rose 2

Monday

Dharma Rose’s owner brought her to me to accomplish several larger jobs that he deemed crucial to his future sailing plans, including replacing the original engine with a new Beta 14, installing a new Monitor self-steering windvane, and some semi-structural work in the cabin to repurpose a built-in keel-mounted waste tank, along with sundry maintenance and upgrade items along the way.  The boat was in good original condition that generally belied her age.

The engine replacement was the #1 job on the list, so after removing a small amount of gear from the boat to clean out the cabin and storage areas, I removed the cockpit sole to gain access to the original Bukh 8HP diesel beneath.  I was impressed by the appearance of the engine and engine room, both of which were cleaner than usual, and the engine itself (and related components) were so free from corrosion that I guessed the boat must have had the luxury of a mainly fresh-water life.  Clearing the way for the work ahead, I immediately pulled out of the way a length of ventilation hose that ran through the space, pulling it aft into the lazarette for now.

I began outside to remove the propeller, which I like to do immediately since using a prop puller requires that the shaft be secured and there’s no better time to do it than at the onset of the engine removal.  There was a prop zinc secured over the prop nuts, a two-piece design that clamped together between the two nuts, and while I suspected there were little screws holding it together, their heads were filled with corrosion or debris, so I simply knocked off the zinc after chiseling a groove through it, exposing the nuts for removal.  I tied the rudder to one site to improve access, Neither nut was particularly tight, so they came off easily once the zinc was out of the way.

I used a small two-blade prop puller to remove the propeller next, which also went more easily than I’d anticipated:  just setting the body of the puller behind (forward of) the prop hub was enough to loosen its grip on the shaft, and I pulled it off easily.  The original propeller was two-bladed, size 12RH13. Afterwards, I made some measurements of the shaft clearance and aperture size for future reference in spec’ing new equipment later.

Now up in the boat, I began to disconnect the engine for removal.  I tried to work systematically from aft to forward and top to bottom, removing anything that connected the engine to the boat.  I started with the shaft coupling, which once more was pleasingly free from corrosion, and the four bolts released without a fight.

Next, I removed the exhaust hose from the elbow; since I planned to replace the hose, I cut it just below the nipple.  I also removed the small vent line, which ran up into the port cockpit locker where there was a vented loop (I hoped to reuse these components).  Meanwhile, still near the aft end of the engine, I removed the throttle and gear control cables and moved them out of the way. I disconnected the wiring harness leading to the engine panel down in the cabin, but found that the wires were pinched somewhere along their run, somewhere out of my immediate reach, so for now I left the panel and its wiring for later.

In this way, I moved my way along the engine, removing the four nuts securing the engine to the flexible engine mounts, fuel lines, electrical connections, and raw water hoses as needed till the engine was free all around.  Knowing I needed to reduce the width of the engine in order to fit it through the opening directly above, I removed the air filter and exhaust elbow, and while I knew I’d probably have to take something else off later, I held off more disassembly for now since I wanted to minimize how much I did before knowing it was necessary.

With the engine free, I hooked up my hoist and prepared to lift it out.  I soon found that anything that could get caught somewhere and hang up the engine definitely would get caught somewhere and hang up the engine, so it was with significant continued effort and various additional parts removals (including three of the four wide engine mounting flanges, the secondary fuel filter assembly, and more) that I finally somehow wedged the engine up through the tight opening and into clear air.  It was obvious that this engine had been installed in the hull before the deck was installed above since the physical dimensions simply didn’t work any other way.

I lowered the engine to the shop floor and a little rolling dolly so I could move it around easily.  Since the owner already had someone interested in buying the engine, I’d tried to be careful during its removal, and now I reassembled the various parts I’d removed in order to make it whole again.

Meanwhile, back in the engine room I bailed out the engine drip pan, which was full of water, and cleaned up the space a bit further, removing the fuel filter and pulling the fuel lines back into the fuel tank locker for the moment before calling it a day.  I’d continue work in the space next time.

Total time billed on this job today:  8 hours

0600 Weather Observation:  34°, cloudy. Forecast for the day:  Cloudy, showers to rain/snow/mix overnight

 

Scupper 64

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Friday

With 220 grit and a palm sander, I sanded the spots on the hull where I’d applied fine filler earlier, removing the excess material and smoothing the hull.

Next, I lightly sanded the new fiberglass on the top of the rudder, just removing rough edges and lightly fairing with the surrounding areas.

There’d be more work on the rudder ahead, but for the moment I wanted to partially raise it back up into the boat and remove the temporary blocking, as I needed to move the boat over closer to the wall in the shop to make room for other projects for the next couple months till I got back to work on Scupper in earnest  with Phase 2  later in the winter.  With my jack, I lifted the rudder back up, then used a line wrapped over the poop deck to hold the rudder in place for now, just so I could reposition the boat.

Afterwards, I moved her over closer to the wall, opening some space to one side of the shop and near the door that I could use for some other projects on the docket.  It wasn’t a big move, but enough for what I needed, and I wouldn’t need full access to Scupper’s hull for the next round of work in any event.

Total time billed on this job today:  1.75 hours

0600 Weather Observation:  25°, clear.  Forecast for the day:  Increasing clouds in the afternoon, rain overnight, 45°

Scupper 63

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Thursday

I began with a light sanding of the most recent round of fiberglass work on the rudder, including the upper portion of the leading edge and the top edge of the blade, bringing the fill work down to the final contours at the top.

Some slight depressions remained on top, and around the rudder post, so I installed some thickened epoxy over these areas to do the final smoothing.

Afterwards, and while the new epoxy was still uncured, I wet out and installed two layers of 1708 fiberglass over the top of the rudder, wrapping around the rudder post and overlapping slightly the new glass on the leading edge.

Total time billed on this job today:  2.25 hours

0600 Weather Observation:  55°, cloudy.  Forecast for the day:  Mainly cloudy, increasing sun, low 60s

Scupper 62

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Tuesday

I continued work on the first stage of the rudder repair, starting with a light sanding of the new fiberglass and related work that had cured overnight.

I used my plywood template to check the contours of the leading edge of the rudder over the new repair.  As I’d hoped, the two new layers of fiberglass brought things back to where they needed to be, without making the shape too large.

With the lower section glassed, I used my jack and blocking to raise and support the rudder at a greater height so I could access the top portion of the leading edge.

After final preparations, I installed the corresponding two layers of fiberglass over the top, with the top layer overlapping the bottom section by three inches as planned.

At the top of the rudder, I used a thick mixture of strengthened epoxy to build up the forward section near the rudderpost, bringing it back close to the original shape,. working only by eye at this stage.   This application would later serve as the basis for the final shaping once cured.

Moving on, I turned to the topsides, beginning with vacuuming and a solvent wash to remove residual dust from an earlier round of sanding following the high-build primer.  Afterwards, I went closely over the hull with a strong light, looking for small flaws and pinholes that required filling, just as I’d done on deck before.  I marked these with simple pencil marks as I found them, since it was very hard to see them otherwise.  This would make filler application easier.

Mixing up a batch of epoxy fine filler compound, I troweled it into the various spots as needed, including filling the remnants of the recessed scribe line from the top of the original boottop.

Total time billed on this job today:  4 hours

0600 Weather Observation:  64°, mostly cloudy.  Forecast for the day:  Cloudy, maybe a stray shower as what’s left of Florence passes to the south, 77°

Scupper 61

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Monday

I’d originally planned on removing the rudder at some point when I lifted and moved the boat, since there was not enough clearance to the shop floor with the boat in the shop to allow a complete removal of the shaft.  However, for the moment I planned to keep the boat where she was, and after some consideration I decided I could attack the rudder repair now without completely removing it–barring unforeseen circumstances, of course.

The main problem with the rudder was at the top edge, where the blade had hit the hull over the years since there had been no rudder stops installed in the steering system to prevent such an occurrence.  This had crushed the fiberglass and crumbled the interior structure of the rudder (basically a mix of solid putty).

(Photos from earlier in the project)

There was also a crack along the seam at the centerline on the leading edge of the blade–a common issue with rudders on many boats–plus additional damage to the bottom edge of the blade, which would also require some rebuilding work. (Photos from earlier in the project)

A bit earlier in the project, I’d prepared for the rudder’s removal by releasing the interior stuffing box nut and partially removing the bolts securing the bronze shoe on which the rudder shaft rested.

I set up a jack beneath the rudder to help me lift it off the pintle on the bronze shoe, and also to help me control the rudder’s descent.  There was little clearance to lift the rudder given its relatively tight fit against the shape of the hull, but it was enough to ease the pressure on the shoe and allow me to remove the bolts, after which the shoe dropped to the ground of its own accord; there was only a little bit of silicone sealant behind it.  Then, with relative ease, I could lower the rudder the rest of the way to the floor (after dropping it partially and removing the jack and blocking).

With the rudder down, I could access the top part of the blade–the most-damaged area–and also the leading edge, at least roughly half at a time.  I hoped the scope of repair would fit within the limitations of the access, which indeed it appeared it would.  The bottom of the blade I could deal with later, once I’d dealt with the top and leading edge.

Clearance between the rudder and the skeg and hull was tight, and there was no room to add extra material to the rudder in the course of repair, particularly at the leading edge, which had virtually no clearance between it and the skeg.  So to reinforce the cracked, curved edge, I’d need first to remove sufficient material to accommodate the thickness of new reinforcement.  To ensure that I maintained the existing shape and contours, I began by making a simple template–first from cardboard, then eventually from 1/4″ plywood–of the leading edge.  This would guide me as I ground off material and built up the new.

I also made a quick cardboard template of the shape of the top of the rudder, using the relatively-intact starboard side as my guide.  The template would help me keep the rebuilt top in the correct shape, though this wouldn’t be much of a challenge since the top of the blade was basically a straight line from the rudder shaft aft to where it curved down to meet the trailing edge.

Templates complete, I ground the leading edge of the rudder as needed to remove paint and gelcoat, and also deep enough to accommodate several layers of fiberglass that I planned in order to better reinforce the cracked edge.  I ground a bit into the crack running along the edge (the crack was simply where the two halves of the rudder came together but had been inadequately reinforced).  At the top of the rudder, I ground into the damaged areas enough to remove all loose fiberglass and the damaged filler in between, and also sufficiently down onto the blade to allow room for new fiberglass that I’d wrap over the top during the rebuilding process.  The round areas lining the edges of the rudder are filled areas covering the heads and bases of bolts that someone had installed long before in an attempt to reinforce the rudder.  I saw no reason to remove them, as they’d end up fully encapsulated within the rebuilt blade.

Holding my leading edge template against the rudder according to some reference marks I’d made before grinding, I could see that I’d removed enough material to allow for the rebuilding.

I also sanded the skeg around the edges of the rudder shoe recess, to clean and prepare this area for eventual reinstallation.

Despite these shortfalls, the blade itself, over most of its area, seemed sound enough, and short of starting from scratch I felt that the repair scope was such that I could–and would–proceed with the repair in place, despite the fact that ideally it would have been nice to fully remove the rudder.  But I didn’t see the need to spend the time and effort to lift and move the boat in order to drop—and then later reinstall–the rudder given what I’d found so far.  I had full access to the top and (later) bottom of the blade, and I could address the leading edge reinforcement in two overlapping sections, since the skeg interfered with part of the rudder even with it dropped as far as possible.  But raising the rudder part way after fiberglassing the lower part would allow me the access to the upper section as needed.

Now that I’d cleaned out loose and broken material within the top of the rudder and exposed solid material all around, it was time to build up–in several separate applications to avoid undue heat during curing–the interior of the rudder, now with a solid epoxy mixture of structural components like chopped strand and high-density filler.  After two applications during the afternoon, I reached the top of the existing sides of the blade.  Additional material to bring the rudder back to its final shape would have to wait till these first stages cured overnight.

Meanwhile, I got to work on the lower section of the leading edge, beginning with some strengthened epoxy filler in the groove I’d ground out over the crack, then following with two layers of biaxial tabbing set in epoxy.  I left room on the second layer so that the second layer from the top section could later overlap and conjoin the two sections accordingly.

While I had the rudder dropped, I removed the packing nut from inside so I could replace the packing before reinstallation.    The old packing (5 rings, though the fifth disintegrated to dust upon removal) was well-worn and overdue for replacement.  I’d cleanup the bronze nut and corresponding threads on the rudder tube before installing new packing and reinstalling it once the rudder was done.

Total time billed on this job today:  5.75 hours

0600 Weather Observation:  64°, foggy.  Forecast for the day:  Fog, then eventual clearing, around 80°

Dory 16

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Thursday

To complete the refinishing part of the project, after the hull paint had cured a couple days I continued with some green bottom paint–chosen  because I had it on hand, not necessarily because it matched the color of the interior trim (though it did closely match, as it happened).

To round out the interior, I painted the flat surfaces of the deck with a cream-colored nonskid paint.  Originally I’d planned to cut this in closely to the sides and other framing members, but in practice I quickly discovered that the thick brush I had was not adaptable to this sort of detail, nor was the roughness of the bottom planking and other surfaces.  Instead, I ultimately chose to paint up to about 1/2″ of the structure all around, leaving a band of the overlapping green paint in all areas.  There was no way I was going to mask around all the members for this project; frankly, it wasn’t worth the time.  While my freehand lines were imperfect, so too was the whole boat, and the net effect was what I wanted.

Overall, I thought the boat looked good, and a whole lot nicer than the original boat.  I was pleased with the transformation, and thought it represented a reasonable blend of practicality and good looks.

Total time on this job today:  1.5 hours

Dory 15

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Tuesday

Second coat, same as the first.

Total time on this job today:  .5 hours

Dory 14

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Sunday

Now that the two coats of green paint for the interior and trim were dry, I could continue with the hull paint.  There was no need to mask, since the overhanging gunwale gave me a good place to cut in by hand, and the waterline was already ready.  For the hull, I chose a paint called Shaw’s Yellow, and in little time applied the first coat with roller and brush.

Total time on this job today:  .75 hours

Dory 13

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Saturday

I applied a second coat of the green interior and trim paint right over the first.

Total time on this job today:  1 hour

Dory 12

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Thursday

With the primer cured, I continued with the first coat of paint on the interior surfaces and gunwale trim.  For this, I chose a light green color.  When I chose the color, I’d been going for that sort of very light, Bahamian teal green sometimes seen on old wooden Maine lobster boats or Novis, but the actual color was somewhat different than I’d expected–but I liked it anyway.  I overlapped the color from the various framing members onto the floor of the dory to ease cutting in later.

Total time on this job today:  1.5 hours

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