(page 83 of 166)

August West 5

Tuesday

Late last week, we had a meeting at the boat to look at and discuss details of the dodger installation.  To prepare for that meeting, I set up a quick analog for the boom height, which was the critical factor in determining the dodger height.  After measuring to the gooseneck location on the mast, and allowing for the depth of the boom below its attachment point, I mocked up the setup with a 2×4 acting as the mast, and a string (which I led to the closest wall and leveled it) to represent the bottom of the boom in a horizontal position.

The net outcome of the meeting was that the owner decided against building the dodger.  The boom height was lower than any of us thought, and the dodger would have been quite small and confining.  This would have been workable if need be, but the owner had his own doubts about the project from the getgo:  while the dodger would be nice to have sometimes, the way he used the boat didn’t demand having one, and usually didn’t need it at all.  With all this, the deciding factor in abandoning the dodger project was the new rigid boom vang the owner had ordered and that we planned to install at the shop.  The new vang would extend far enough aft that it could have its own effect on the dodger design, and this ended up being the straw that broke the camel’s back.

With that behind us, and after a day finishing up some details on another project at the shop, I got back to things with the cockpit coamings.  I’d already stripped (but not sanded) the old coating from the insides of the coamings, and now I worked on the outside faces.  First, though, I decided to remove the old sheet winches, which were slated for replacement with new self-tailing ones during this project, and with the winches out of the way I’d have slightly better access for stripping and sanding the wood.  These were easy to remove, and I took a moment to test-fit one of the new winches, which were slightly larger in overall diameter but still just within the footprint of the existing bronze winch bases, though the drums slightly overhung the edges.   I’d discuss this with the owner before proceeding, but the new winches seemed workable without major changes.

With that, I got to work removing the old coating from the outside of the coamings on both sides.  As before, this took some time because of the thinness of the coating and the character/texture of the wood beneath, which was somewhat weathered with much of the wood’s softer grain being long gone with the passage of time, leaving behind the slightly uneven and hard surface we associate with aged, weathered teak.

Afterwards, I sanded the coamings clean and smooth in all areas, working through 80-120 grits to bring them to their final appearance.  These would be left bare to weather naturally from here on out, along with all the other woodwork on deck.  The nature of the existing woodgrain meant that some texture remained in the coamings, as they had long ago weathered past the point of glassiness, but the clean appearance would soon weather evenly to match the texture.

With the coamings stripped and sanded, I could reinstall the various bronze coaming cleats I’d removed at the onset of the job.  On the port side, there had been two of these cleats all along, though the after one had been installed without the little bronze backing plate like its brethren.  Now, I reinstalled this cleat with a new backing plate to match its counterpart.  On the starboard side, there’d been only a single cleat, and the owner asked me to install a second one to match the port, which I did now.   The new cleat to starboard would give the owner a good place to secure the roller furling line, which meant that I could remove the lame hoseclamped-on plastic cleat from the nearby stern pulpit, which had been the previous setup.

I recommended a spirited sail on a choppy day to splash the new bronze–and the bare teak–with salt water to begin and accelerate the aging process and desired patina.

After final preparations, I painted the underside of the sea hood, the first step towards preparing it for its final installation.

Total time billed on this job today:  6 hours (including Friday)

0600 Weather Observation:  28°, cloudy.  Forecast for the day:  Snow and rain showers, 35°

Scupper 260

Monday

At the owner’s request, I’d asked my intrepid canvas contractor to make up several covers for the winches, tiller, autopilot, and the windlass.  True to form, he exceeded expectations with some really nice work on these covers, delivering them all only a few days after he came by to measure and pattern.

The owner had also requested some simple friction-fit foam fillers to use for privacy in the small elliptical ports.  These weren’t fancy, but they did the job well.  There were enough of these for all the ports, plus an extra or two.

Meanwhile, I continued working with a local sign shop to finalize the lettering.  The owner’s choice of script for the new name meant that I felt it was worth various extra efforts to ensure that the name was the “right” size given all the considerations (transom size, individual letter size, overall appearance of the graphics), and properly matched the arc of the deck camber at the top of the transom.  To this end, the sign shop produced a cheap test version on throwaway vinyl that I picked up and tried out on the transom.  The owner liked the shape and size, so we went forward with the final version shortly thereafter.

With the final version of the name on hand in the owner’s choice of gold leaf with dark blue outlines, I finished up the installation a couple days later.

With the accessory installation brackets for the tillerpilot on hand, I could finish up its installation now.  The way the geometry of this boat worked out, the standard tillerpilot required  an under-tiller mount, plus a pushrod extension, plus a cantilever bracket for mounting the outboard side of the tillerpilot to the side of the cockpit coaming.   I put the starboard cockpit cushion in place temporarily so I could ensure the tillerpilot cleared the cushion when installed, which the rise of the tiller dictated anyway.  I installed the 4″ pushrod extension to the end of the tiller, then extended the pushrod about halfway through its stroke for the initial setup.

With the tiller temporarily in place, and measuring the required 18″ distance forward from the center of the rudderpost, I made a mark on the tiller where the pin for the tiller end of the unit needed to go, and taped the new bracket in place beneath in the proper position–both for testing and minor adjustment and because I wasn’t ready to permanently install the bracket, since the tiller needed a few more coats of varnish.  I put the starboard cockpit cushion temporarily in place to ensure that I mounted the tillerpilot above the cushion, which the shape of the tiller dictated anyway.  I installed the 4″ pushrod extension to the end of the tiller pilot, then spent quite a bit of time fussing with the overall setup to determine the final mounting location for the coaming-mount bracket, which, because of the fore and aft angle of the coaming, required an angled spacer block behind.

At length, after one failed version of the angled block and various trials, I determined the final mounting location and dry-fit the bracket so I could permanently mount it.  This location was clear above the cockpit cushion, in line with the pin on the tiller itself, and met all the other installation criteria.  The tube containing the various cantilever mounting pin locations was removable from the base, leaving a relatively clean installation when the tillerpilot was not in use; the cockpit locker lid just cleared the assembly when installed, which was fortunate but happenstance since the geometry of the cockpit and tiller arrangement dictated its position.

With the bracket permanently installed with sealant, bolts, and a backing plate, I fitted the tillerpilot and double-checked its position.  With the tiller centered, the tillerpilot (i.e. the pushrod) was at 90 degrees to the tiller, as required.  I’d await an electrical test till I could mount the tiller bracket to the tiller once the varnish work was complete.

With these final installations complete, my work list came virtually to its end, other than some final loading onto the boat and ongoing varnish work.  To wrap things up, during the afternoon I picked up the boat’s new sails from the sailmaker.  I’ll wrap up any lingering work or details in a final post as progress dictates.

Total time billed on this job today:  7 hours (Over a couple days)

0600 Weather Observation:  15°, mostly clear. Forecast for the day:  Sunny, 36°

August West 4

Thursday

The sea hood required some light sanding, and then touchup with quick-drying filler to finalize the shape and contours of the after reinforcement.  Now the hood was ready for primer and paint.

I spent most of the day working on the teak project, starting with the handrails on the cabin top.  After paring away the excess bungs, I stripped and sanded these rails clean, to 120 grit.  At the same time, I removed the excess bungs from the companionway trim and sliding hatch.

Next, I stripped and cleaned up as well as possible the teak trim at the aft end of the cockpit, around the rudderpost and forward of the outboard well; Cape Dory did not choose the best wood for these pieces, which I suppose is fair enough, and they’d soon weather to a fine gray color in any event.  The clamping bracket for the outboard had once been finished as well, but as this was simply a short length of 2×6, I didn’t make any great attempts to sand it fully bright.

The owner and I had discussed the possibility of installing a vinyl “eyebrow” on the cabin trunk.  We’d seen some anecdotal photographic evidence of another Typhoon Sr. with a too-short and not-that-well-done eyebrow that looked unfinished, but still gave a hint of how a real eyebrow might enhance the boat’s appearance.  I had the thought of using vinyl tape to create the accent without having to go through the rigorous routine of trying to bend wood around the forward curvature, which was substantial on this boat, so with the owner due to be at the shop the next day for a meeting about the dodger, I took a few minutes to attempt a mockup using 1/2″ masking tape to test the concept.

While the first attempt needed some fine-tuning, particularly around the forward part of the trunk, and wasn’t necessarily quite right yet, it started to give a sense of things. With  he upcoming meeting,  I didn’t want to spend more time on it till we’d had a chance to decide whether it was worth pursuing.

During the afternoon, I worked to strip the old finish from the insides of the cockpit coamings on both sides.  This was surprisingly slow going, but in fact because there was so little finish actually on the wood, it took longer to scrape it away; heavier layers of coatings seem easier to heat and remove.  IN any event, by the end of the day I’d stripped all the finish from the inside faces of the coamings, leaving them ready for sanding to complete the work later.

Total time billed on this job today:  6 hours

0600 Weather Observation:  26°, mostly clear. Forecast for the day:  Mostly sunny, 42°

August West 3

Wednesday

After lightly sanding the new seahood fiberglass at its trailing edge, I test-fit the hood once more.  It fit well, and the curvature was what it needed to be to clear the sliding hatch.

I temporarily reinstalled the wooden hatch trims to ensure that the sea hood fit around them properly.  I found that these forced the sides of the sea hood out just a bit, flattening the curve and causing minor interference issues, so with the trims removed once more, I beveled the cuts to match the inside angles of the sides of the sea hood, and this cured the problem.  Satisfied now with the fit, I used a drill and a small bit to mark the deck at each of the screw holes in the sea hood mounting flange.

After removing the hood again, I applied a coat of fairing compound to the after reinforcement to fine-tune its shape and those of the fillets and surrounding area.

Back on the boat, I used a 1/2″ bit to drill out the top laminate and core from the new fastener locations for the sea hood.  The core was dry in all areas, but the spoils highlighted an interesting blue color to the laminate that I’d not seen before; this was present at all hole locations.  After cleaning up, I masked around the holes as needed and filled them with a thickened epoxy mixture, leaving this to cure while I worked on other things.

While I had the hatch off, it made sense to begin the wood stripping with the small trim pieces on the sliding hatch.  Once I’d sanded the wood clean, I installed bungs in the exposed screw holes on the top trim.

On deck, I decided to continue with the companionway hatch trim and work my way out from there, so to begin I removed the two vertical pieces of trim flanking the companionway–these had no bungs, and, as it turned out, not a stitch of sealant–and sanded them clean down on the bench.  Then, I reinstalled them with some butyl sealant behind, and later installed new bungs in the open screw holes.

Continuing, I turned to the trim just inside the companionway opening, which was partially finished (sides) and partially bare (forward). With heat and a scraper, I removed the heavy, dark finish from the sides, then sanded clean the bare wood.

To finish up the day’s work on this project, I installed new bungs in the handrails, and the starboard cockpit coaming.  I’d be able to sand these smooth at the same time I stripped and sanded these parts, saving some time later.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:  36°, partly clear. Forecast for the day:  Mostly sunny, 44°

August West 2

Tuesday

The work list for August West was eclectic and generally of the minor maintenance category, beginning with the exterior brightwork, including toerails, handrails, cockpit coamings, and various other trim bits.  The existing finish  was old varnish and/or Cetol in poor condition, and the owner wanted to strip it all back to bare teak and then let the wood weather naturally from there, which look and lack of maintenance was in keeping with his vision and use of the boat.

In the same general exterior appearance category, the owner requested that I repaint and change the color of the boottop and bottom, and also replace the cove stripe to match.

We also planned to enhance the sailing experience with new self-tailing winches for the genoa, a tiller extension, and a rigid boom vang, all of which I’d be installing soon.

The owner also wanted to install a new dodger, and to that end he had purchased an old fiberglass sea hood that came from a Cape Dory 25; the existing companionway had no sea hood, and while one wasn’t required, it did make sense to install one and provide a better landing point for the dodger.  We didn’t know if the old sea hood would be adaptable to this boat, but it seemed a worthy (small) investment to give it a try versus building something from scratch.

The old sea hood was structurally sound and in generally good condition, and I set it in place over the existing hatch to get a sense of its fit.  I knew it would be too long, since the CD Typhoon Sr. features a rather short companionway hatch, but shortening the hood would be straightforward.  In a perfect world, it would have fit cleanly and without need for other modification, but in reality, while the hood fit over the companionway well enough, it interfered with the wooden trim that acted as guides and hold-downs for the existing sliding hatch, as it wasn’t quite wide enough to clear the existing trims.

I considered and rejected various options for dealing with the fit, from doing nothing and giving up on the sea hood (not really a desirable option), to extending the wood trim (maybe), to making the sea hood taller on the sides (fussy and not really practicable nor attractive nor desirable), but in the end I decided it made sense to see about modifying (i.e. cutting narrower) the existing wood trim to accept the sea hood, which was a simple option since the sea hood almost fit as it was, and there was no need for the trim to be as wide as it was other than consistent appearance–and that wouldn’t be an issue since the modified trim would be inside the sea hood and not visible.  Plus, conveniently, all the bungs were missing from the wood trim (and the handrails and the companionway trim and the coamings), so removal of the trim ought to be a snap.

Happy with that idea, I made a few measurements and marks to denote the new length of the sea hood, since now it extended well past the companionway opening.  Down on the bench, I fine-tuned the cut line and made the cut with a jigsaw.

Back on deck, I test-fit the shortened hood.  I’d been conservative in my initial cut, and while with the hood propped up on the wooden trims it sat nice and high and allowed the companionway hatch and trim to slide beneath, I could see that once I lowered the hood to deck height (by removing/modifying the wooden trims), the companionway hatch trim would no longer clear the hood, so I decided to cut off another 1-1/2″ to better allow for that.

At the same time, I removed the teak trim on either side of the hatch; this was as easy as I’d anticipated, as there was little sealant and all the screws were exposed.  I’d worry about the trim modifications later, but for now, with the interference removed, the sea hood flange sat nearly on the deck, though the little raised molded flats on either side of the hatch–designed to accept the wooden trims–prevented the hood from fitting properly on the deck itself.  The raised flat was perhaps 1/4″ high, and I’d need to remove about the outer 1/4″ of its width, so the amount of material to remove was minimal.

I figured those raised areas were solid fiberglass and therefore felt that it would be a pretty easy modification to trim the outer portions flush with the deck, which would allow the hood flange to rest flat on the deck; it appeared that the existing camber of the hood was a close (and workable) match to the cabin top.  To prepare, I marked the deck at the outer edge of the sea hood flanges, indicating the drop-dead don’t-grind-beyond line, and made some marks to represent the inside of the sea hood, then drew reference lines where I needed to remove the material.  Then, with a grinder and an angle flap disc, I carefully removed the offending material from each side, after which the hood fit quite well, as I had hoped.

Happy with those modifications, next I temporarily reinstalled the wooden trim pieces and marked where I needed to cut them as well, before removing them again and taking the whole arrangement down to the bench for some final work.

To prepare the sea hood for final touches and refinishing, I first sanded off the old paint from the underside, sanding enough to ensure good bonding but not overly worrying about removing all the paint since this part of the hood would never be visible once installed.  On the top surfaces, I sanded away a layer of old paint and primer–both were in good condition and sound, but the color was an off-white that wouldn’t work as is–and sanded smooth the original gelcoat beneath.  At the trailing edge, I removed a strip of the gelcoat down to bare laminate to prepare the surface for some needed reinforcement, as the hood was a bit flimsy there.  I had hoped to build a small extension beneath the opening, as per the original, but the hood was now a close fit with the sliding hatch and there simply wasn’t room, so instead I planned to add a stiffener on the top edge.

For that, I cut a strip of 3/8″ prefab fiberglass to fit, and after final preparations glued it in place with epoxy adhesive and epoxy fillets.  To hold the shape of the hood, I temporarily screwed the flanges to the bench, and added some support beneath the center of the opening.  Once the epoxy securing the new brace cured, it would hold the curvature nicely.  At that time, I also planned to shape and blend the new reinforcement into the adjacent areas for a seamless and intentional appearance.

Finally, I made the cuts on the teak trims so they would clear the sea hood.  With these pieces conveniently on the bench, I took a moment to sand off the old finish as needed, back to clean wood.

Total time billed on this job today:  4.5  hours

0600 Weather Observation:  32°, mostly cloudy. Forecast for the day:  Mostly cloudy, 55°

Scupper 259

Tuesday

After a trip out into the world to drop off the transom template at the sign shop, I spent a little time aboard the boat to install new ring pulls on the table top storage bin.  The new pulls were slightly larger in overall diameter than the old, though the same as the pulls I’d installed in the cabin sole hatches, so I had to enlarge the recess by just a bit, which I did with a Forstner bit in a drill press.  Afterwards, installation was straightforward.

Somehow, the boat and table had made it 42 years without someone installing a way to secure the table leaves when lowered; the banging leaves drove me crazy in only a matter of seconds even with the boat on the hard.  To deal with this, I installed a pair of simple brass hooks to secure the leaves in place when lowered, tightly against the table frame at the aft end.

I sanded and prepped the companionway boards and tiller for their next coats of varnish, but was awaiting new varnish so I postponed the application till later.

Total time billed on this job today:   2.5 hours

0600 Weather Observation:  32°, mostly cloudy.   Forecast for the day:  Mostly cloudy, 55°

August West 1

Monday

First thing in the morning, while it was still calm, I removed the tarp from the boat, preparing her for moving indoors soon.  A few weeks earlier, during another warm spell, I’d taken the time to dig out the boat from snowbanks and move her to location near the shop; though we hadn’t had any more snow since then, and in fact the melt had continued, it had been nice knowing that the boat was nearby and ready for me whenever I was.

Much later in the day, after I’d wrapped up several hours of work on another project, which included getting the second shop bay ready to accept August West, I moved her indoors, where after removing some straps and tie-downs, my first order of business was to lift the mast off the deck to get it out of the way for the project.  For now, I rested the mast on some sawhorses in the shop; I had a little mast-related work on this project as well.

Total time billed on this job today:  1.75 hours

0600 Weather Observation:  32°, mostly cloudy.  Forecast for the day:  Partly sunny, 56°

Scupper 258

Monday

Over the weekend, I applied another coat of varnish to the tiller (4) and swashboards (2).  So to start the day, I lightly sanded these again, and applied the 5th and 3rd coats of varnish, respectively.

I decided to make a simple template of the transom so I could help the sign shop make the lettering to the correct arcs.  In this case, the owner’s choice of lettering featured an interconnected font, and I felt it was worth the extra effort to ensure that the vinyl was properly cut.  With a piece of leftover pattern plastic, I marked the key points on the transom, mainly the top edge (deck camber), the centerline, and the two corners where the deck met the hull.  With these marks made, then down on the bench I could lay out a horizontal line between the two transom corners and determine the height of the deck crown (9″ over a width of 74″).  I made plans to bring this template to the sign shop in the near future to finalize the graphics.

I reinstalled the reinforced starboard cockpit lid, one of a few small and otherwise insignificant tasks I expunged from my short list this day.

I spent most of the rest of the day’s time getting the boat ready for “being complete”, picking up where I left off.  I’d gotten the interior mostly in order and put together last time, but had run out of time before I could clean up the decks.  Now, I removed most of the protective plastic I’d had in place since shortly after the paint was complete, leaving only the cockpit for now.  It was nice to see the decks fully exposed again and with the deck hardware in place.  This meant that afterwards, I could dismantle the staging to make more room around the boat, and to prepare her for a yard move later; for now, I planned to leave her in the main work bay, as current weather aside (it had been mostly warmer than usual and no snowstorms for some time), it was still winter, and I didn’t want to expose the boat to the elements just yet if I didn’t have to.

That meant that I would be working in my other bay for the upcoming projects, and to prepare that space for the other boats, I was ready to move Scupper’s mast out, which had been in the bay since mid-winter at the beginning of the mast-painting project.  Now, all spar-related work was done, and to prepare the mast for moving outdoors as well as for transportation whenever that happened, I wrapped the mast and furlers in plastic sleeves, securing the plastic and rigging within well and often with tape and small stuff as needed protect the mast (and boom).  Afterwards, I moved the spars outdoors where they’d await the boat’s departure.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:  32°, mostly cloudy.  Forecast for the day:  Partly sunny, 60°

Scupper 257

Friday

The paint work on the liner cover plates was complete, so to begin the day I installed the various pieces throughout the boat.

Afterwards, I cleaned up the whole interior so I could get to work on installing the upholstered backrests/locker doors in the main cabin, and installing the other interior cushions to complete the work in the cabin.  The backrests went on quickly with four bolts each, since they’d already been fitted once before, so it was simply a matter of the final installation this time around.

Before completing the cushions, I reassembled the cabin table down in the shop, as it was still in pieces from the refinishing efforts earlier, then installed the table on the cabin sole, securing it to its original brackets that allowed quick removal of the table to access the bilge beneath as needed.  Because one of the brackets landed on the new, larger bilge hatch I’d built, I secured the bilge hatch with a pair of screws to ensure that everything was as stable as possible.  The old pull rings for the table top storage compartment were in overly-weathered condition, so I chose not to re-use them and ordered replacements that I’d install once on hand.

The table installation brought to light an unwelcome surprise:  the companionway ladder/head door didn’t clear the back of the table by about 1/4″.  This might be because the new ladder assembly was slightly larger and different in shape than the original, or perhaps the table was in a slightly different position than its original, but whatever the cause, it required me to cut away and shape the offending corner of the door/ladder so it would clear the table and operate properly.  With the table out of the boat for so long, and basically no experience in the cabin with the table in place (I’d removed it forthwith at the beginning of the project because it was so much in the way), it hadn’t even occurred to me that clearance would be an issue.  Education never ends, nor do the continuing surprises that small boats hold in store for the unwitting.

Fortunately, it was just a small modification, after which the door operated as needed, but I’d have to touch up the finish at the newly-changed corner.

With the table in place, the protective floor covering and masking tape out of the way, and the whole cabin vacuumed and cleaned up, I could now put the cushions in place to bring the whole cabin together for the first time.

This all took surprisingly long, but the project list was nearly fully expunged by this point.  I had a short list of small jobs to complete over the next week or two, but expected this to be my last day working full-time on Scupper.  After unloading most of my tools and other supplies from the boat–they’d been briefly repurposed to the cockpit from the cabin, but now it was time to clean house–I finished up by painting the new reinforcement on the locker lid, so that would be ready for reinstallation next time, along with a few other minor tasks before the boat was truly completed.

Total time billed on this job today:  7 hours

0600 Weather Observation:  22°, cloudy. Forecast for the day:  Mostly cloudy, snow showers, 40°

Scupper 256

Thursday

After a light sanding, I applied another coat of semi-gloss white enamel to the liner cover plates, and another coat of varnish to the tiller.

I finished up the toilet installation by connecting the fresh water intake line behind the toilet, and installing the other end of the discharge line to the fitting on the holding tank.  Then I ran the toilet wiring (for the intake and discharge pumps) into the engine room, where I secured it and made the connections as needed to the toilet control box.  I applied the little cover plates over the toilet bowl fasteners, and finished up work in the head by installing the panel to cover the holding tank, and cleaning up the space.

Unclamping the screen frame, I lightly sanded the new assembly as needed and test-fit it in the opening.  The screening would come later, but for now I went ahead with a sealer coat of varnish–and on the solid swashboard as well, as I didn’t want to leave the plywood unprotected, and since the companionway was small and vertical, a varnish finish on these pieces would last a long time, and provide an accent to the exterior of the boat.

After a lunch engagement, I got back in time to finish up a couple more items, in and around cleaning up the boat as I continued the transition from project to completed vessel.  The owner’s new tiller pilot arrived, and although the mounting brackets I needed were not yet on hand, I could go ahead and install the power supply, choosing a spot in the cockpit coaming just aft of the tiller pilot’s expected mounting location.  I’d planned ahead and already had a 14 gauge wire pair led to the area from the panel, so final connection was straightforward.

Finally, after a light sanding, I applied two-part epoxy primer to the fresh fiberglass reinforcement beneath the starboard cockpit seat, which would allow me to apply the final gray paint next time, one of just a few minor tasks remaining on my list.

Total time billed on this job today:  6 hours

0600 Weather Observation:  3o°, clear. Forecast for the day:  Sunny, 45°

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