(page 82 of 165)

August West 4

Thursday

The sea hood required some light sanding, and then touchup with quick-drying filler to finalize the shape and contours of the after reinforcement.  Now the hood was ready for primer and paint.

I spent most of the day working on the teak project, starting with the handrails on the cabin top.  After paring away the excess bungs, I stripped and sanded these rails clean, to 120 grit.  At the same time, I removed the excess bungs from the companionway trim and sliding hatch.

Next, I stripped and cleaned up as well as possible the teak trim at the aft end of the cockpit, around the rudderpost and forward of the outboard well; Cape Dory did not choose the best wood for these pieces, which I suppose is fair enough, and they’d soon weather to a fine gray color in any event.  The clamping bracket for the outboard had once been finished as well, but as this was simply a short length of 2×6, I didn’t make any great attempts to sand it fully bright.

The owner and I had discussed the possibility of installing a vinyl “eyebrow” on the cabin trunk.  We’d seen some anecdotal photographic evidence of another Typhoon Sr. with a too-short and not-that-well-done eyebrow that looked unfinished, but still gave a hint of how a real eyebrow might enhance the boat’s appearance.  I had the thought of using vinyl tape to create the accent without having to go through the rigorous routine of trying to bend wood around the forward curvature, which was substantial on this boat, so with the owner due to be at the shop the next day for a meeting about the dodger, I took a few minutes to attempt a mockup using 1/2″ masking tape to test the concept.

While the first attempt needed some fine-tuning, particularly around the forward part of the trunk, and wasn’t necessarily quite right yet, it started to give a sense of things. With  he upcoming meeting,  I didn’t want to spend more time on it till we’d had a chance to decide whether it was worth pursuing.

During the afternoon, I worked to strip the old finish from the insides of the cockpit coamings on both sides.  This was surprisingly slow going, but in fact because there was so little finish actually on the wood, it took longer to scrape it away; heavier layers of coatings seem easier to heat and remove.  IN any event, by the end of the day I’d stripped all the finish from the inside faces of the coamings, leaving them ready for sanding to complete the work later.

Total time billed on this job today:  6 hours

0600 Weather Observation:  26°, mostly clear. Forecast for the day:  Mostly sunny, 42°

August West 3

Wednesday

After lightly sanding the new seahood fiberglass at its trailing edge, I test-fit the hood once more.  It fit well, and the curvature was what it needed to be to clear the sliding hatch.

I temporarily reinstalled the wooden hatch trims to ensure that the sea hood fit around them properly.  I found that these forced the sides of the sea hood out just a bit, flattening the curve and causing minor interference issues, so with the trims removed once more, I beveled the cuts to match the inside angles of the sides of the sea hood, and this cured the problem.  Satisfied now with the fit, I used a drill and a small bit to mark the deck at each of the screw holes in the sea hood mounting flange.

After removing the hood again, I applied a coat of fairing compound to the after reinforcement to fine-tune its shape and those of the fillets and surrounding area.

Back on the boat, I used a 1/2″ bit to drill out the top laminate and core from the new fastener locations for the sea hood.  The core was dry in all areas, but the spoils highlighted an interesting blue color to the laminate that I’d not seen before; this was present at all hole locations.  After cleaning up, I masked around the holes as needed and filled them with a thickened epoxy mixture, leaving this to cure while I worked on other things.

While I had the hatch off, it made sense to begin the wood stripping with the small trim pieces on the sliding hatch.  Once I’d sanded the wood clean, I installed bungs in the exposed screw holes on the top trim.

On deck, I decided to continue with the companionway hatch trim and work my way out from there, so to begin I removed the two vertical pieces of trim flanking the companionway–these had no bungs, and, as it turned out, not a stitch of sealant–and sanded them clean down on the bench.  Then, I reinstalled them with some butyl sealant behind, and later installed new bungs in the open screw holes.

Continuing, I turned to the trim just inside the companionway opening, which was partially finished (sides) and partially bare (forward). With heat and a scraper, I removed the heavy, dark finish from the sides, then sanded clean the bare wood.

To finish up the day’s work on this project, I installed new bungs in the handrails, and the starboard cockpit coaming.  I’d be able to sand these smooth at the same time I stripped and sanded these parts, saving some time later.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:  36°, partly clear. Forecast for the day:  Mostly sunny, 44°

August West 2

Tuesday

The work list for August West was eclectic and generally of the minor maintenance category, beginning with the exterior brightwork, including toerails, handrails, cockpit coamings, and various other trim bits.  The existing finish  was old varnish and/or Cetol in poor condition, and the owner wanted to strip it all back to bare teak and then let the wood weather naturally from there, which look and lack of maintenance was in keeping with his vision and use of the boat.

In the same general exterior appearance category, the owner requested that I repaint and change the color of the boottop and bottom, and also replace the cove stripe to match.

We also planned to enhance the sailing experience with new self-tailing winches for the genoa, a tiller extension, and a rigid boom vang, all of which I’d be installing soon.

The owner also wanted to install a new dodger, and to that end he had purchased an old fiberglass sea hood that came from a Cape Dory 25; the existing companionway had no sea hood, and while one wasn’t required, it did make sense to install one and provide a better landing point for the dodger.  We didn’t know if the old sea hood would be adaptable to this boat, but it seemed a worthy (small) investment to give it a try versus building something from scratch.

The old sea hood was structurally sound and in generally good condition, and I set it in place over the existing hatch to get a sense of its fit.  I knew it would be too long, since the CD Typhoon Sr. features a rather short companionway hatch, but shortening the hood would be straightforward.  In a perfect world, it would have fit cleanly and without need for other modification, but in reality, while the hood fit over the companionway well enough, it interfered with the wooden trim that acted as guides and hold-downs for the existing sliding hatch, as it wasn’t quite wide enough to clear the existing trims.

I considered and rejected various options for dealing with the fit, from doing nothing and giving up on the sea hood (not really a desirable option), to extending the wood trim (maybe), to making the sea hood taller on the sides (fussy and not really practicable nor attractive nor desirable), but in the end I decided it made sense to see about modifying (i.e. cutting narrower) the existing wood trim to accept the sea hood, which was a simple option since the sea hood almost fit as it was, and there was no need for the trim to be as wide as it was other than consistent appearance–and that wouldn’t be an issue since the modified trim would be inside the sea hood and not visible.  Plus, conveniently, all the bungs were missing from the wood trim (and the handrails and the companionway trim and the coamings), so removal of the trim ought to be a snap.

Happy with that idea, I made a few measurements and marks to denote the new length of the sea hood, since now it extended well past the companionway opening.  Down on the bench, I fine-tuned the cut line and made the cut with a jigsaw.

Back on deck, I test-fit the shortened hood.  I’d been conservative in my initial cut, and while with the hood propped up on the wooden trims it sat nice and high and allowed the companionway hatch and trim to slide beneath, I could see that once I lowered the hood to deck height (by removing/modifying the wooden trims), the companionway hatch trim would no longer clear the hood, so I decided to cut off another 1-1/2″ to better allow for that.

At the same time, I removed the teak trim on either side of the hatch; this was as easy as I’d anticipated, as there was little sealant and all the screws were exposed.  I’d worry about the trim modifications later, but for now, with the interference removed, the sea hood flange sat nearly on the deck, though the little raised molded flats on either side of the hatch–designed to accept the wooden trims–prevented the hood from fitting properly on the deck itself.  The raised flat was perhaps 1/4″ high, and I’d need to remove about the outer 1/4″ of its width, so the amount of material to remove was minimal.

I figured those raised areas were solid fiberglass and therefore felt that it would be a pretty easy modification to trim the outer portions flush with the deck, which would allow the hood flange to rest flat on the deck; it appeared that the existing camber of the hood was a close (and workable) match to the cabin top.  To prepare, I marked the deck at the outer edge of the sea hood flanges, indicating the drop-dead don’t-grind-beyond line, and made some marks to represent the inside of the sea hood, then drew reference lines where I needed to remove the material.  Then, with a grinder and an angle flap disc, I carefully removed the offending material from each side, after which the hood fit quite well, as I had hoped.

Happy with those modifications, next I temporarily reinstalled the wooden trim pieces and marked where I needed to cut them as well, before removing them again and taking the whole arrangement down to the bench for some final work.

To prepare the sea hood for final touches and refinishing, I first sanded off the old paint from the underside, sanding enough to ensure good bonding but not overly worrying about removing all the paint since this part of the hood would never be visible once installed.  On the top surfaces, I sanded away a layer of old paint and primer–both were in good condition and sound, but the color was an off-white that wouldn’t work as is–and sanded smooth the original gelcoat beneath.  At the trailing edge, I removed a strip of the gelcoat down to bare laminate to prepare the surface for some needed reinforcement, as the hood was a bit flimsy there.  I had hoped to build a small extension beneath the opening, as per the original, but the hood was now a close fit with the sliding hatch and there simply wasn’t room, so instead I planned to add a stiffener on the top edge.

For that, I cut a strip of 3/8″ prefab fiberglass to fit, and after final preparations glued it in place with epoxy adhesive and epoxy fillets.  To hold the shape of the hood, I temporarily screwed the flanges to the bench, and added some support beneath the center of the opening.  Once the epoxy securing the new brace cured, it would hold the curvature nicely.  At that time, I also planned to shape and blend the new reinforcement into the adjacent areas for a seamless and intentional appearance.

Finally, I made the cuts on the teak trims so they would clear the sea hood.  With these pieces conveniently on the bench, I took a moment to sand off the old finish as needed, back to clean wood.

Total time billed on this job today:  4.5  hours

0600 Weather Observation:  32°, mostly cloudy. Forecast for the day:  Mostly cloudy, 55°

Scupper 259

Tuesday

After a trip out into the world to drop off the transom template at the sign shop, I spent a little time aboard the boat to install new ring pulls on the table top storage bin.  The new pulls were slightly larger in overall diameter than the old, though the same as the pulls I’d installed in the cabin sole hatches, so I had to enlarge the recess by just a bit, which I did with a Forstner bit in a drill press.  Afterwards, installation was straightforward.

Somehow, the boat and table had made it 42 years without someone installing a way to secure the table leaves when lowered; the banging leaves drove me crazy in only a matter of seconds even with the boat on the hard.  To deal with this, I installed a pair of simple brass hooks to secure the leaves in place when lowered, tightly against the table frame at the aft end.

I sanded and prepped the companionway boards and tiller for their next coats of varnish, but was awaiting new varnish so I postponed the application till later.

Total time billed on this job today:   2.5 hours

0600 Weather Observation:  32°, mostly cloudy.   Forecast for the day:  Mostly cloudy, 55°

August West 1

Monday

First thing in the morning, while it was still calm, I removed the tarp from the boat, preparing her for moving indoors soon.  A few weeks earlier, during another warm spell, I’d taken the time to dig out the boat from snowbanks and move her to location near the shop; though we hadn’t had any more snow since then, and in fact the melt had continued, it had been nice knowing that the boat was nearby and ready for me whenever I was.

Much later in the day, after I’d wrapped up several hours of work on another project, which included getting the second shop bay ready to accept August West, I moved her indoors, where after removing some straps and tie-downs, my first order of business was to lift the mast off the deck to get it out of the way for the project.  For now, I rested the mast on some sawhorses in the shop; I had a little mast-related work on this project as well.

Total time billed on this job today:  1.75 hours

0600 Weather Observation:  32°, mostly cloudy.  Forecast for the day:  Partly sunny, 56°

Scupper 258

Monday

Over the weekend, I applied another coat of varnish to the tiller (4) and swashboards (2).  So to start the day, I lightly sanded these again, and applied the 5th and 3rd coats of varnish, respectively.

I decided to make a simple template of the transom so I could help the sign shop make the lettering to the correct arcs.  In this case, the owner’s choice of lettering featured an interconnected font, and I felt it was worth the extra effort to ensure that the vinyl was properly cut.  With a piece of leftover pattern plastic, I marked the key points on the transom, mainly the top edge (deck camber), the centerline, and the two corners where the deck met the hull.  With these marks made, then down on the bench I could lay out a horizontal line between the two transom corners and determine the height of the deck crown (9″ over a width of 74″).  I made plans to bring this template to the sign shop in the near future to finalize the graphics.

I reinstalled the reinforced starboard cockpit lid, one of a few small and otherwise insignificant tasks I expunged from my short list this day.

I spent most of the rest of the day’s time getting the boat ready for “being complete”, picking up where I left off.  I’d gotten the interior mostly in order and put together last time, but had run out of time before I could clean up the decks.  Now, I removed most of the protective plastic I’d had in place since shortly after the paint was complete, leaving only the cockpit for now.  It was nice to see the decks fully exposed again and with the deck hardware in place.  This meant that afterwards, I could dismantle the staging to make more room around the boat, and to prepare her for a yard move later; for now, I planned to leave her in the main work bay, as current weather aside (it had been mostly warmer than usual and no snowstorms for some time), it was still winter, and I didn’t want to expose the boat to the elements just yet if I didn’t have to.

That meant that I would be working in my other bay for the upcoming projects, and to prepare that space for the other boats, I was ready to move Scupper’s mast out, which had been in the bay since mid-winter at the beginning of the mast-painting project.  Now, all spar-related work was done, and to prepare the mast for moving outdoors as well as for transportation whenever that happened, I wrapped the mast and furlers in plastic sleeves, securing the plastic and rigging within well and often with tape and small stuff as needed protect the mast (and boom).  Afterwards, I moved the spars outdoors where they’d await the boat’s departure.

Total time billed on this job today:  5.5 hours

0600 Weather Observation:  32°, mostly cloudy.  Forecast for the day:  Partly sunny, 60°

Scupper 257

Friday

The paint work on the liner cover plates was complete, so to begin the day I installed the various pieces throughout the boat.

Afterwards, I cleaned up the whole interior so I could get to work on installing the upholstered backrests/locker doors in the main cabin, and installing the other interior cushions to complete the work in the cabin.  The backrests went on quickly with four bolts each, since they’d already been fitted once before, so it was simply a matter of the final installation this time around.

Before completing the cushions, I reassembled the cabin table down in the shop, as it was still in pieces from the refinishing efforts earlier, then installed the table on the cabin sole, securing it to its original brackets that allowed quick removal of the table to access the bilge beneath as needed.  Because one of the brackets landed on the new, larger bilge hatch I’d built, I secured the bilge hatch with a pair of screws to ensure that everything was as stable as possible.  The old pull rings for the table top storage compartment were in overly-weathered condition, so I chose not to re-use them and ordered replacements that I’d install once on hand.

The table installation brought to light an unwelcome surprise:  the companionway ladder/head door didn’t clear the back of the table by about 1/4″.  This might be because the new ladder assembly was slightly larger and different in shape than the original, or perhaps the table was in a slightly different position than its original, but whatever the cause, it required me to cut away and shape the offending corner of the door/ladder so it would clear the table and operate properly.  With the table out of the boat for so long, and basically no experience in the cabin with the table in place (I’d removed it forthwith at the beginning of the project because it was so much in the way), it hadn’t even occurred to me that clearance would be an issue.  Education never ends, nor do the continuing surprises that small boats hold in store for the unwitting.

Fortunately, it was just a small modification, after which the door operated as needed, but I’d have to touch up the finish at the newly-changed corner.

With the table in place, the protective floor covering and masking tape out of the way, and the whole cabin vacuumed and cleaned up, I could now put the cushions in place to bring the whole cabin together for the first time.

This all took surprisingly long, but the project list was nearly fully expunged by this point.  I had a short list of small jobs to complete over the next week or two, but expected this to be my last day working full-time on Scupper.  After unloading most of my tools and other supplies from the boat–they’d been briefly repurposed to the cockpit from the cabin, but now it was time to clean house–I finished up by painting the new reinforcement on the locker lid, so that would be ready for reinstallation next time, along with a few other minor tasks before the boat was truly completed.

Total time billed on this job today:  7 hours

0600 Weather Observation:  22°, cloudy. Forecast for the day:  Mostly cloudy, snow showers, 40°

Scupper 256

Thursday

After a light sanding, I applied another coat of semi-gloss white enamel to the liner cover plates, and another coat of varnish to the tiller.

I finished up the toilet installation by connecting the fresh water intake line behind the toilet, and installing the other end of the discharge line to the fitting on the holding tank.  Then I ran the toilet wiring (for the intake and discharge pumps) into the engine room, where I secured it and made the connections as needed to the toilet control box.  I applied the little cover plates over the toilet bowl fasteners, and finished up work in the head by installing the panel to cover the holding tank, and cleaning up the space.

Unclamping the screen frame, I lightly sanded the new assembly as needed and test-fit it in the opening.  The screening would come later, but for now I went ahead with a sealer coat of varnish–and on the solid swashboard as well, as I didn’t want to leave the plywood unprotected, and since the companionway was small and vertical, a varnish finish on these pieces would last a long time, and provide an accent to the exterior of the boat.

After a lunch engagement, I got back in time to finish up a couple more items, in and around cleaning up the boat as I continued the transition from project to completed vessel.  The owner’s new tiller pilot arrived, and although the mounting brackets I needed were not yet on hand, I could go ahead and install the power supply, choosing a spot in the cockpit coaming just aft of the tiller pilot’s expected mounting location.  I’d planned ahead and already had a 14 gauge wire pair led to the area from the panel, so final connection was straightforward.

Finally, after a light sanding, I applied two-part epoxy primer to the fresh fiberglass reinforcement beneath the starboard cockpit seat, which would allow me to apply the final gray paint next time, one of just a few minor tasks remaining on my list.

Total time billed on this job today:  6 hours

0600 Weather Observation:  3o°, clear. Forecast for the day:  Sunny, 45°

Scupper 255

Wednesday

I got started with some quick sanding and another coat of paint and varnish on the liner cover plates and tiller, respectively.

The tail end of any project tends to be filled with myriad undefined chores, and I knocked several off my actual and stream-of-consciousness lists throughout the morning in and around a couple of the more concrete jobs still underway, including working with the owner and my local sign shop to begin and finalize the lettering for the transom, a process still underway as of this writing.

About the last “major” item on my work list, as-yet untouched, was to build new swashboards for the companionway.  The boat had arrived at the shop with several different versions, all of which were in disrepair and unsuitable going forward, even if still essentially functional.  I planned to build a new teak plywood version, plus a teak screen unit.

To begin, I tested the fit of one of the original boards to determine its suitability for a pattern.  This old plywood board was ugly, but it worked well enough and I could use it to help pattern the new ones.  From a partial sheet of teak plywood I had on hand, I cut out a replacement, matching the size and shape of the original.

This was straightforward, but in the process it led to an unexpected job.  Throughout the project, I’d basically never stepped on the starboard cockpit locker lid; I’d removed these lids early on in the first phase of the project, and they’d been set aside in the shop for most of the time since, as I used temporary plywood covers over the locker openings throughout construction.  Even after I finally reinstalled the locker lids several weeks earlier, I never had much cause to walk on the starboard one since my path on and off the boat, and in and out of the cabin, kept me well clear.  The port locker lid, onto which I stepped every time I got on or off the boat, had never shown any signs of weakness.

This all leads up to the fact that during my companionway work, I stepped on the lid and was most unhappy to feel softness underfoot–the first time I’d noticed this or even had any inkling, as somehow this had escaped my notice for the past two years.   I did my best to pretend I hadn’t felt it, and willed it to deal with itself, but ultimately, of course, I knew it was something I had to deal with.

So I removed the lid from the cockpit, unscrewing the hinge, and down on the bench I did some exploratory probing with a drill bit from the underside.  As expected, the lid featured a cored construction, but unexpectedly the core in all my test holes was clean and bright.  I had expected it to be wet and damaged.  After various additional testing and consideration, I decided that the lid was simply weak and not well-enough supported, and that it wasn’t a core problem after all.

I’d been fully prepared to recore the lid, though the process could have risked damage to the finished surface of the lid, but since the core was sound, and I didn’t relish removing sound core from the top skin if it wasn’t truly necessary, I decided instead to install a stiffener/reinforcement.  I sanded away the paint from a section of the middle of the lid (all on the underside), and cut a piece of prefab fiberglass as a stiffener, which I secured in place with thickened epoxy adhesive and a large fillet all around.  In the process I also epoxy-filled my test holes, which in this case would double as additional reinforcement and a sort of “key” into the existing structure beneath the new reinforcement.

After letting the epoxy cure for a few hours while I continued work on other things (to which I’ll return shortly here), I applied a small touch-up layer of thickened epoxy to the fillets, smoothing minor imperfections from the first round, then installed two layers of 1708 fiberglass over the top of the whole arrangement to complete the reinforcement.  I’d certainly not planned to be doing this at this stage of the project, but I was glad I’d noticed the problem when I did in any event.

Meanwhile, I continued work on the pair of new companionway boards.  With the basic plywood one cut to shape, my next step was to cut a little slot for the companionway hasp, but as with everything that required an additional step first.  There’d been no hardware installed on the companionway when the boat arrived here, but there was a recess in the wooden part of the slide that fit a standard hasp tang perfectly–except that it didn’t allow the tang to rotate out of the way when the hatch was open.  So I made a little teak spacer to fill the space, and glued it in place before installing the little tang through the new spacer.  Then, with the hatch shut, I used the tang to mark its own slot on the back side of the new hatch board, and cut out the slot as needed.

To begin the solid teak-framed screen unit, I cut several pieces of 4/4 teak to the widths I wanted (3″ for the bottom rail, 2″ for the stiles, and a wider piece for the top rail that I’d later cut into the curve required), then resawed and planed them down to a finished thickness of just under 5/8″, which fit in the slots of the companionway.  Using my new plywood swashboard as a template, I laid out and cut the frame pieces for the screen, then, on a flat surface covered with plastic, clamped and glued the frame pieces together with thickened epoxy adhesive.

By now, it was mid-afternoon, and I’d just received the shipment containing the elbow fitting I needed for the head, so with a short stretch of time before I had to leave for the day, I thought I’d get that in place if I could.  Barbed plastic plumbing fittings tend to be annoyingly oversized–this one was spec’d out at 1.61″ OD, nominally 1.5″ pipe size, but 1-1/2″ reinforced marine hose simply does not stretch enough to fit over something oversized–a fact with which I was well familiar, so my first step was to sand away the offending barbs as needed so the fitting would fit inside the hose, removing just what I needed to from both sides of the barb before pre-installing the short length of hose I needed to attach to the discharge fitting on the toilet.  Then, up in the boat, I installed the new elbow and connected it to the discharge hose I’d installed earlier, bolting the toilet into its brackets in the process.  It was a relief to have that done, and now all that remained to complete the head installation was to connect the intake hose, and finalize the wiring from the toilet to the control box.

Total time billed on this job today:  7 hours

0600 Weather Observation:  39°, cloudy, rain shower.  Forecast for the day:  Mostly cloudy with gradual clearing, windy, 46°

Scupper 254

Tuesday

I continued work on the fiberglass liner cover plates as needed, which in this case meant lightly sanding and cleaning up the two newly-glued pieces from last time, and finalizing the sanded finish on the remaining sections as needed.  After test-fitting the newly-extended section for the port side, I applied a coat of primer to all pieces.  At the same time, I lightly sanded the tiller and applied a second coat of varnish.

I spent some time on a more involved test of the electric motor and controller, eventually figuring out how to shift from forward to reverse (it wasn’t immediately clear that the key switch was the “gear shift”, and that turning it one way or the other selected the direction of the motor).  I had to switch a pair of wires on the back of the key switch, as indicated in the instructions, in order for the key switch to work logically, with forward being forward and aft being reverse.  With the boat on the hard, I had to severely limit how much I operated the shaft for now, lest I cause damage to the Cutless bearing, but in any event the propulsion system worked as it was supposed to in both directions.

Satisfied with the engine controls and that the wiring as as it should be, I permanently installed the control panel with butyl tape sealant and six screws.

Before moving on to energize and test the charger for the engine battery bank, I took a few moments to finalize the wiring at the port outboard batteries, cleaning up and securing the charger and temperature sensor wires and securing the battery box top; I’d not been able to properly finish this when I made the final connections the other day.

After plugging in the shore power, flipping the proper switches, and resetting the GFI outlet in the engine room (these seem to come pre-tripped when new), the battery charger powered up, and all lights that should have been lit were lit, and things that shouldn’t have lit up didn’t (i.e. error lights or codes).  Once I’d confirmed proper operation, I left both this charger and its counterpart for the house battery bank energized for the rest of the day as a chaperoned test to ensure nothing untoward happened.

With the propulsion system and battery bank checked out and complete, the last major job aboard was to complete the installation of the head.  I’d already done everything I could to prepare, so all that was left (one of those funny phrases in boat restoration…) was to install the throne itself, including water supply and discharge hoses and four wires.

With the character and dimensions of the head platform and head compartment itself, I eventually settled on what I thought was a good position for the toilet bowl.  I had to factor in arm and leg room, the shape of the nearby hull, space to allow the lid to open more than 90 degrees, and also leave room for the hoses to exit the back of the toilet.  While the toilet was designed to have its hoses and wiring exit straight down from the back of the china bowl, and the bowl backed up close to a bulkhead, in this case there was no access, nor room, for this sort of arrangement, and I’d always known I’d have to run the hoses in a different way.  My final location struck the required compromise between all the factors, and I marked the outline of the bowl right on the protective paper I’d had in the head during the project.

The bowl was to be secured to three hidden brackets that fit inside, with bolts that passed through holes in the bottom of the unit.  As needed, I marked these locations to help align the three brackets, which came pre-stuck to a piece of cardboard that I supposed was to hold the brackets in the proper position and alignment, which could have been helpful if indeed the brackets were properly aligned and positioned on the cardboard, which they were not. So I removed the brackets from the cardboard (whatever they used to stick them on was extremely adhesive) and installed them according to my layout marks and in accordance with the instructions, securing them to the platform with the included screws and washers.  Then, having previously noted the approximate locations where I wanted the hoses to run, I drilled two holes through the small bulkhead behind the platform and into the holding tank space, and with some effort eventually led in the heavy discharge hose, leaving both ends detached for now pending final head installation.  The fresh water intake line I had led into the compartment some time before, and now had only to lead it out through its own new hole towards the toilet.

I had hoped and planned to complete the installation now, but I ran into difficulty with the discharge hose connection.  As I noted before, the design intended this hose to lead straight down, and the discharge attachment arrangement inside the toilet bowl didn’t easily accommodate deviation from this engineered solution.  There was flexibility in the discharge connection, but I found that with the hose attached and a fairly aggressive bend to lead out to the bulkhead, the rubber thingie inside the toilet tended to kink.  At length, after trying various things, I came to the conclusion that I needed an elbow fitting in there in order to make the bend while keeping the discharge assembly happy, and since I didn’t have one on hand I’d have to postpone final installation till a little later.  Fortunately, there was (or, I should say, appeared to be) ample vertical clearance to accommodate an elbow, so I hoped that it would work out well once I had it on hand.  I would have preferred to avoid the extra fitting, but so it goes with anything on a small sailboat (or, I imagined, any boat).

During this process, I’d found that it looked like it would be beneficial if I pre-installed the rubber bracket included with the discharge assembly, and which was designed to be secured from above by one of the bolts holding on the toilet seat, so I took care of that now to ease angst later on.

Having taken the head as far as I could for the moment, I finished up the day by installing the new aluminum bracket I’d purchased for the masthead, and completing the Windex installation.  I secured the bracket to an existing hole in the masthead unit, along with an additional screw to keep it from twisting, and bolted the Windex mount to its after end, giving the vane ample clearance with the lights forward.  I removed the vane for safekeeping.

Total time billed on this job today:  8 hours

0600 Weather Observation:  34°, partly cloudy.  Forecast for the day:  Mostly sunny, 51°

Older posts Newer posts