(page 118 of 167)

Jasmine 47

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Thursday

After cleaning up from the latest snowfall, I got back to work with the hardware on the coachroof, starting with the plastic deck plates for the solar vents.  I’d already pre-filled and marked the fastener locations for these fittings, so installation was straightforward.

Next, I installed the forward hatch with its two after hinges.  There was no access to this area from beneath–it was in way of the mast beam and bulkhead–so I installed the hinges with screws alone.  This section of the deck was solid fiberglass now that I’d rebuilt the mast step area earlier.

I waited on the mast step for now, as I’d need to build it up taller than original.  One of the upcoming projects for the riggers was to shorten the mast by a couple inches to remove some corrosion at the base, and accordingly we planned to raise the step to make up the difference.  Meanwhile, I installed two little bronze eyelets that had come off the deck near the vent fittings; I’d prepared these holes during an earlier stage of deck preparation as well.

Other than the sea hood, this completed the hardware installation for the coachroof, so now I moved down to the port sidedeck and worked on the new waste fill deckplate and reinstalled the waste tank vent fitting in the cabin side.  The deck was solid fiberglass around the waste fitting, so all I had to do was drill, tap, and install.

On the foredeck, I installed the round anchor line hawse in its original position to port,  where I’d also filled the surrounding area with solid fiberglass and epoxy to prepare for a simple installation now.

To wrap up work on the foredeck, I reinstalled the two mooring cleats.  I reused the original aluminum backing plate belowdecks.  I also installed the bow chocks which were mounted on the raised overhanging bulwark/toerail and hadn’t really needed to be removed for the deck work, but at dismantling time I’d just been going through my habitual motions and only afterwards realized my mistake.

Back in the cockpit, I installed the hinges for the starboard cockpit locker.

To round out the day, I decided to unpack and inventory the Norvane windvane assembly and begin to acquaint myself with the installation, as I planned to move forward with this soon and wanted to see how this particular vane would hang from the boat.  Plus, I needed to determine what sorts of fasteners and drill bits I’d need for the installation.  I inventoried the included parts, noted any fasteners I’d need to order, and acquainted myself with the installation directions.

Total time billed on this job today:  6.75 hours

0600 Weather Observation:  12°, clear, 8″  snow and sleet overnight.  Forecast for the day:  Sunny, 25°

Jasmine 46

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Wednesday

Over a disjointed morning rife with various competing distractions, I managed to finish up the stanchion installations, starting with the port amidships stanchion, completing the installation I’d begun earlier now that the epoxy-filled hole for the gate brace had cured.

Later, after stepping out for a bit to attend to other business, I completed the installation of both gate braces at the aftermost stanchions.  The bolt locations for the brace bases fell outside of the cored area on each side of the deck, so all I had to do was mark, drill, tap, and install the bases accordingly.  First the port side…

…then the starboard.

In the afternoon, I decided to tackle the “easy” installation jobs in the cockpit, starting with the old engine instrument panel.  I applied butyl tape sealant to the back of the panel and installed it in its original opening.

Next, I reassembled the gearshift lever and bilge pump bellows that I’d removed before painting.

Then, I installed the circular access port in the cockpit sole.

I reinstalled the starboard cockpit locker lid hinges, using more of the butyl tape to seal these fasteners.

Finally, I installed the new cockpit seat drain fittings, heavily applying sealant around the flanges and necks of each fitting and tightening the nuts from belowdecks.

Total time billed on this job today:  4.75 hours

0600 Weather Observation:  8°, clear.  Forecast for the day:  Snow by noon, heavy snow in the afternoon, about 10″ expected

Jasmine 45

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Tuesday

I set up the stern pulpit again and dry fit it, securing it temporarily with screws in the outer (solid deck) holes so I could accurately mark and drill the remaining holes in the newly epoxy-filled holes in the other areas.  Once I’d drilled all the holes, I removed the pulpit once more and finished up the work on the new holes, tapping for 1/4″ machine screws and beveling the tops of the holes with a countersink.

With the area cleaned up, I applied sealant and installed the pulpit with machine screws, nuts, washers, and backing plates, reusing some more or less permanently-affixed fiberglass backing plates from the old installation that remained inside the steering room (two centermost stanchion locations).

I temporarily installed the bow pulpit, which was straightforward since its bolting locations were on the outboard side of the toerail flange.  The pulpit looked ridiculous hanging out in mid air beyond the stem, as I had not yet built the new bow platform, but for the moment the installation served its purpose and would allow lifeline measurement whenever the riggers wanted to do it.

The two stanchions amidships featured built-in gate braces, and these required an additional screw.  When I laid out the port side during an earlier phase of the project, for a reason that now escaped me I’d chosen not to pre-mark the hole location for the brace, so on this side I installed the stanchion (more on this in a moment) and marked the hole location, which turned out to be in a cored area of the deck, so I bored out the hole with a 5/8″ bit and filled it with thickened epoxy to prepare the hole for next time.

On the starboard side, I did have a pre-marked, pre-filled fastener location, so I could permanently install the stanchion and its gate brace now.  I had gate braces for the aftermost stanchion pair as well, which formed the other end of the opening gate section, but these were separate pieces and I’d get to their installation shortly.

I had some trouble installing the stanchion tubes, which should have been a simple task, but in almost every case the fit was just a bit too tight–these stanchion bases originally came from another boat, obviously with different tubes, though the ostensible diameter was the same.  In any event, fitting the stanchions required some sanding and cleanup of the tubes and especially within the base sockets before I could install the stanchions properly.  This was an irritating frustration that required much more time than it should have, but eventually I prevailed, as indeed I must.

Total time billed on this job today:  6 hours

0600 Weather Observation:  12°, mainly clear/high clouds.  Forecast for the day:  Mainly sunny, around 30°

Jasmine 44

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Monday

Now that the paintwork was complete, my first priority going forward was to install the stanchions and pulpits so that the riggers could come and measure for the new lifelines.  So to this end, I spent some time accumulating and preparing installation tools, fasteners, and equipment–including lots of soft towels and sheets to protect the decks–and getting geared up for the new round of work.

During the recore and surface prep work, I’d laid out, epoxy-filled, and marked all the stanchion base locations, so now it was a generally simple matter to install these bases.  To begin, I made up six fiberglass backing plates to fit the bases, using some leftover laminate I had from something or other.

For each of the six bases, I followed the same steps outlined here.  Masking off the deck around the lightly-marked holes from earlier, I placed the bases over the holes and drilled the pilot holes required for 5/16″ machine screws.  With the base still in place, I used a sharp knife to cut the masking tape around the base, after which I could remove the portion beneath the base and finish preparing the fastener holes with a 5/16 tap (threading the holes for the machine screws) and countersink to bevel the very top of each hole for additional sealant retention.

After cleaning up the spoils, I applied sealant–a light polyurethane–to the holes and deck, leaving an abundant bead.   I installed the base tightly with its four fasteners, then proceeded belowdecks to install the backing plate, washers, and nuts.

Back on deck afterwards, I cleaned up the excess sealant and removed the tape, completing the installation.

I repeated this process for each the remaining five bases, working my way forward on the port side, then back aft along the starboard.

This took most of the day, but by mid-afternoon all six bases were complete and I turned to the stern pulpit.  In this area, I’d not pre-prepared any of the fastener locations during the recore, so I’d need to lay out and overbore for epoxy any  fastener holes that fell within the cored area of the poop deck.  I began by applying masking tape over the entire area in question, since I wasn’t sure where the pulpit bases would exactly land, and in any event pulpit bases tend to be brutal to deck paint if precautions aren’t taken first.    Adjusting things hither and yon, I eventually ended up with the pulpit where I wanted it.

Because the outboard edges of the deck were filled with solid epoxy or were otherwise solid, un-cored fiberglass, I could drill and tap one hole at each base location (the forward starboard base on this pulpit had been replaced sometime previously with a different, separate 4-hole base style; the remaining three bases were welded rounds with three holes apiece) and install a temporary screw to hold the pulpit in its proper position and allow me to mark the remaining holes, and trace out the base profiles on the masking tape.

Removing the pulpit again, I removed the circles of masking tape I’d marked, and drilled out all the remaining holes with a 5/8″ bit, passing through the top skin and removing the core, but leaving the bottom skin intact.

After cleaning up, I filled the new holes with a strengthened and thickened epoxy mixture, leaving this overnight to cure so I could continue installation in the morning.

Total time billed on this job today:  7.25 hours

0600 Weather Observation:  38°, clouds and fog.  Forecast for the day:  Showers, clearing, temperature dropping through the afternoon

Handy Cat 4

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The switch, or controller, that I removed from the original electric motor housing was all that was needed to control the motor (located in the propeller hub) itself.  My goal in this installation was to create a simple and portable means of transporting and connecting the controller switch and 12-volt battery to the wiring from the rudder, so that I could quickly install and remove the controls whenever I used the boat, and keep the battery charged up ashore in the meantime.

To this end, I hoped that a small 12-volt battery (such as the small case size often seen in lawn tractors) would provide sufficient amp-hourage for my limited motor use.  Obviously a smaller battery would limit the length of time I could run the motor, but I thought my needs were minimal enough that the desire for easy portability would take precedence.  The instructions that came with the motor recommended a minimum 105 amp-hour battery, which made sense for all that, but I thought/hoped I wouldn’t need such capacity since I only planned to run the motor for perhaps (thinking generously) 10 minutes total per trip.

With this in mind, I found a plastic toolbox (ostensibly “waterproof” with a gasketed cover, though this wasn’t a criterion for me in this case, nor had I any illusions about the sanctity of the lid seal) that was large enough to hold a standard lawn tractor battery, and I planned this box to form the basis of my controller installation.  For illustration, I used a tractor battery I had on hand.  Truth be told, I’d purchased the box thinking it would also be large enough to hold a group 24 size battery if needed, as the listed dimensions suggested this, but of course the inside of the box was somewhat smaller and too tight in height and width for a regular battery.

These little batteries weren’t, in the main, rated by amp hourage, as they weren’t deep cycle and, as small engine starting batteries, were rated only in cold cranking amps.  Some online research revealed low amp-hour ratings (in the 18-20 amp-hour range) for these batteries from other sources, but after additional searching I located a deep cycle version rated at 45 amp-hours  in a similar case size that would still fit in my controller box.  My plan, once I purchased the exact battery, was to build some internal bracing to hold the battery in place at one end of the box, leaving the other end open for the wiring and controller.

Satisfied that the box idea would work for now–only time in actual use would determine whether the small battery was enough for what I needed–I prepared to install the controller switch in the end wall of the box.  I drilled a hole that fit the diameter of the housing around the control shaft, and cut by hand a small slot at the top to match the molded keyway on the switch housing.  This allowed me to insert the switch from inside the box, with the control shaft outside.  To hold the switch in place, in addition to the friction-fit cutout and keyway, I applied some epoxy after I scuffed up the plastic on the box.  I hoped this would be sufficient for the basically light-duty use the switch would experience.  I braced this in place while the epoxy cured.

Outside the box, I used one of the plastic pieces that originally came with the motor, and which slipped right over the metal control shaft.  This piece originally allowed connection of the tiller-type control handle, but I didn’t plan to use that.  Instead, I found and ordered a knob for outside that would fit over the roughly 1/2″ diameter of the shaft cover.  As of this writing I awaited delivery of the knob.

To cover the wiring connections and back side of the control switch, I purchased a plastic storage tray that I could hang over the switch, covering it completely from inside while allowing wiring to pass below the cover.  As a simple means of installation, I epoxied in a wooden cleat above the switch, which, once cured, would allow the cover to hang over the switch for protection.  I’d use a single screw to secure the cover to the cleat.

For ease of connection and disconnection and transport of the battery/controller box, I ordered a plug and receptacle for the wiring between the box and the rudder.  Once the matched set–though sold separately–arrived, I set to work to install the receptacle and wire it to the controller switch.  The plug and receptacle were large and fairly serious duty, perhaps more than the job called for, but this was one of the only 4-wire setups I’d found; I had four wires to connect.  In any event, it looked like it would more than hold up to the continuous connection and disconnection that I had in mind, so good enough.

I cut a hole in my portable control box, then installed short lengths of wire–in the same colors as the motor’s original wiring–to the four terminals, choosing them arbitrarily since it didn’t matter.  Then, with the receptacle installed in the box (I used small machine screws and nuts to help hold the receptacle against the pulling motion of plug disconnection), I connected the four short wires to their respective terminals on the control switch.

I finished up the box-end wiring with a 50-amp circuit breaker that I installed in the battery positive line.  I protected the exposed terminals with some heat shrink tubing, just to prevent the unlikely event of a short across these terminals in the generally unprotected environment within the box.  Then, I installed my simple wiring cover over the works of the switches.

To finish up the control box, I installed a large knob on the outside of the controller.  This fit over the plastic piece leftover from the original motor configuration, and I secured it with an included setscrew.  Later, once I tested operation, I’d make some tick marks on the knob and on the box to indicate the motor speed and direction.

Meanwhile, over several different days, I applied two additional coats of semi-gloss white enamel to the rudder, completing the paint work.   Once that was sufficiently cured, I masked off and painted the lower portion of the rudder with new bottom paint.  All that remained for this project was to finish up the rudder-end wiring, including running the new flexible conduit (aka hose) and installing the plug at the end; I planned to complete this soon, and effect a bench test of the whole system shortly thereafter.

Total time on this job today:  2.75 hours (spread over several days)

Jasmine 43

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Friday

Now that the nonskid painting was complete, I removed all the masking tape, and temporarily replaced some of the hatches I’d removed earlier.

Before continuing with deck work, I wanted to give the fresh paint additional cure time, so I spent a little time working on specifying and preparing orders for some of the items–mainly electrical–that I’d eventually need in the weeks to come, but otherwise meaningful progress on the project would wait till after the weekend.

Total time billed on this job today:  1 hour

0600 Weather Observation:  32°, light snow.  Forecast for the day:  Light snow, another inch or two, then ending in the morning and becoming colder.

Jasmine 42

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Thursday

To begin, I applied the second coat of nonskid paint to the deck areas.

Afterwards, looking to keep busy with the project, I continued work on the deck hardware, cleaning up the various bits and pieces I’d removed from the boat and preparing them for reinstallation, along with inventorying and ordering–as necessary–replacement fasteners and other installation supplies.

Total time billed on this job today:  4 hours

0600 Weather Observation:  25°, clouds, an inch of snow overnight.  Forecast for the day:  Cloudy, light snow on and off, 34°

Jasmine 41

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Wednesday

During the morning, I masked off the fresh white paint to isolate the field areas, following the paint lines I’d laid out previously; then, after final preparations, I applied the first of two coats of white nonskid paint.

Although I’d removed the old lenses, gaskets, and sealant earlier, the deadlight frames required some general cleanup to prepare the bonding surfaces and improve the appearance.  Now, as needed, I cleaned out the grooves and scraped/sanded clean the various bonding surfaces (for the lenses and on the back side, where the frames would rest against the cabin trunk), and removed any final bits of old sealant (silicone) from the exterior of the frames, along with some light buffing with fine sandpaper.  The corresponding inside trim rings were generally in good condition, but all benefited from some minor cleanup and light buffing.

The four opening ports from the forward cabins, also aluminum, were covered with lots of sticky butyl-type sealant from their removal.  For each set, I removed all the old sealant from the surfaces to prepare them for new sealant and reinstallation, and otherwise generally cleaned up the frames and trim rings with fine sandpaper and soft wire brushing to improve appearance.  Later, I removed the old screen frames to make installation of the ports easier when the time came.

Total time billed on this job today:  6.75 hours

0600 Weather Observation:  8°, clear.  Forecast for the day:  Sunny, increasing clouds, 23°

Jasmine 40

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Tuesday

I spent the good part of the day removing all the masking tape from the deck and other parts, and generally cleaning up and getting the shop back to normal after a few weeks of painting.  I’d presently continue with the nonskid portion of the deck paint, but needed to give the fresh gloss a days’ cure time before masking for the next step.

With that work complete, I spent some time working on the remaining three deadlight frames, removing the old lenses and cleaning up the worst of the old sealant from the frames.  I’d disassembled one of the frames a few weeks earlier, and now that I knew how the arrangement worked the process went a little more quickly.

The aluminum frames would require some additional cleanup to remove all traces of the old sealant and clean out the grooves in which the old rubber gaskets had sat, but that chore was for another time.  In the meantime, I ordered the new lens material so I’d have it on hand shortly to make replacement lenses.

Total time billed on this job today:  6.25 hours

0600 Weather Observation:  20°, cloudy.  Forecast for the day:  Clouds, some light snow, 20s

Jasmine 39

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Monday

After final preparations, I applied three coats of Alexseal snow white gloss topcoat to the deck areas, working again in two separate phases:  first the remote areas of the coachroof (around the companionway and forward hatch) and the cockpit well; then, three coats on the remaining areas, including the cabin trunk, channels, coamings, and bulwarks, along with the loose hatches on the shop floor.

Total time billed on this job today:  5.75 hours

0600 Weather Observation:  26°, mostly clear.  Forecast for the day:  Sunny, high around 30° but then falling in the afternoon

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