(page 165 of 165)

Nomad 2

< Back to Nomad

Sunday, May 17, 2015

My first opportunity to get back aboard came a few days later.  First, I went through the boat and removed all the loose gear, headed either to the dumpster or into the shop for storage.

My goal for the day was to try and run the engine.  Though I’d already decided in my mind to replace it–it just seemed like a new engine would be the better and more enjoyable choice going forward–I wanted to see it run, for my own sake and so that I could document it when I wanted to sell the old engine later.

Not knowing the state of the gas tank on board, I used a portable can and hose to set up a temporary fuel line, set up a hose and cuffs over the lower unit, and got to work starting the motor.  I think it had been some time since the engine was last used–years–but it started pretty easily and ran well enough, all things considered.  It pumped water well and seemed like it was basically in fine working order.  The steering didn’t work, so I couldn’t straighten the engine.

run1-51715

 

Higher Speed-ish

No video player visible above?  Click here to go to the video.

Idle Speed-ish

No video player visible above?  Click here to go to the video.

Nomad 1

< Back to Nomad

Various circumstances led indirectly to my acquisition of a 1990 Nimble Nomad.  A friend who often trolled Craig’s List found the listing and sent it to me, totally out of the blue.  I wasn’t familiar with Nomads, and my first gut reaction was that the boat was so ugly it was cute.  This particular example was priced at the very low end, and was advertised as needing work:  it had an original 1990 outboard (reportedly running),and very faded original gelcoat on the hull.  It was an interesting design, but I doubt this would have progressed at all had not the boat been located right in town–what were the chances?  Given the proximity, I thought I would have a look.  Some online research on “The Google” revealed a virtual cult status for this boat, with surprising values and asking prices.  This boat was well below the average range of prices I could find online.

The pictures below are from my first viewing. As expected, the boat needed a cosmetic facelift on the outside.  Inside, she was OK–just OK, but there was plenty of opportunity for improvement.  I was impressed, however, with the boat’s spacious layout, and the forward cockpit was a really neat idea that opened up the whole boat and made the small size, with its walkthrough design, amazingly unclaustrophobic.  She was small, trailerable, and simple.  I liked the boat, but left petty much deciding that just because I liked it didn’t mean I had to own it.  Honestly, I didn’t really want another project for a while.

After a night’s reflection and discussion, during which time my wife fell in love with the boat, with some reluctance I decided to make an offer on the boat–lower than the asking price, and without contingency.  I thought given the design’s cult status that the seller wouldn’t take my offer, and I was ready to (expecting to) walk away.  To my amazement (and disconcert), he accepted my offer, so just like that, I had another project.  I was sort of angry at myself.  But my wife loved the boat, and I thought that I could make the boat pretty nice without spending a fortune–or without spending a huge amount of time.  There’d be no set timeframe for the work, and if it killed me I’d keep the scope as minimal as possible–a hard thing to do when I liked to make boats just so, but it simply had to be the new way forward at this point in time.

We completed the sale and brought the boat home the few miles the next day.

Box of Rain 1

November, 2011

Box of Rain, a 1984 O’Day 30′ sloop, came to the shop in late 2011 with a short list of maintenance and improvements required by hew new owner.

One of the tasks at hand was to address two areas on the encapsulated keel where moisture was seeping from within.  So before winter set in, I ground out these two areas to allow any remaining moisture to drain and evaporate during the cold, dry winter.

March, 2012

During a week of summer-like warmth in March, I took the opportunity to complete the keel repair.  There’d been no additional discharge for some time, so I cleaned up the previously-ground areas and filled them with multiple layers of new fiberglass and epoxy resin till they were flush with the adjacent areas.  This required from 4 to 8 layers.

Afterwards, I sanded, filled, and faired the two patches smooth with the surrounding keel.

Friday, April 6, 2012 (1 hour)

During the winter, we’d removed the overhead hatch in the main cabin, which needed a new lens and which had been leaking into the cabin.  With the hatch back on hand with its new lens by early April, I prepared for its installation by reaming out the exposed (well, semi-coated with whatever material O’Day had used on the inside of the cabin liner) core from around the edges of the hatch opening, and installed thickened epoxy in the gap to seal the area.

Wednesday, April 11, 2012 (3.25 hours)

I installed the hatch in a heavy bed of sealant with new screws, cleaning up the squeezeout on the exterior, but leaving the bead that formed on the inside of the hatch flange to cure before removing it.

There was an old, broken, and sun-damaged solar vent fitting on the foredeck, and the owner requested that I simply replace it with a clear plastic deck plate.  After removing the old fitting and sealant, I prepared the inside of the hole with epoxy, then installed the new deck plate with plenty of new sealant.

One of the main upgrades requested by the owner was to replace all the existing through hull fittings, which were the usual production-boat style comprising bronze (brass, in one case) ball valves screwed tenuously to the top two threads of bronze through hull fittings, and coated in rust and corrosion.

The first one I removed, the head intake, gave me false hope for the others:  I was able to easily unscrew the valve body, and then the through hull nut, from the inside, and the fitting was gone in just a couple minutes.  Alas, none of the others would be so forthcoming, forcing me to cut them all from the inside–a simple task complicated by the access in several places, but I prevailed, and with only a few scars managed to remove all fittings in an hour and a half or so.

Monday, April 16, 2012 (4.5 hours)

With a sander, I cleaned up the insides of all the existing through hull openings, removing debris and old paint to prepare the inside of the hull for either patching (for two of the openings) or new fiberglass backing blocks for the through hulls.  The owner requested that I move the engine intake, which had been located inconveniently behind the engine, to the locker beneath the galley sink where it’d be easily accessible.  This required that I cut out some of the fiberglass liner in the locker, which I did with grinder and a cutoff wheel.

While I was making a mess, I prepared a section of the bilge for new fiberglass.  Earlier, the owner had chipped away some damaged fiberglass in this area, exposing sandy concrete filler in the encapsulated keel.  Picking up where he left off, to prepare for an eventual overlay of new material, I ground the edges of the area to remove gelcoat and debris.  Later, I coated the exposed concrete with epoxy resin to hopefully begin to seal and stabilize the surface for future steps; it was like painting a sandbox, but ultimately did what I needed it to do.

For the four new through hulls, I prepared backing blocks of 3/4″ prefabricated fiberglass.

th11-41612

After cleaning the inside of the hull and the insides of the existing holes, I installed the backing blocks in a bed of epoxy adhesive.  For the two small through hulls that would no longer be used, I masked over the holes from outside and filled the holes with the thickened epoxy, the first step in patching.

The starboard topsides featured an abraded area where the boat had come against a dock or other obstruction, and we planned to patch and blend in some gelcoat to match as closely as possible the original.  To begin the process, I applied some filler to take care of porosity in the exposed laminate, and also some minor scratches around the main damage.  This photo shows the area in question before completing any work.

topsides-41612

Tuesday, April 17, 2012 (4.75 hours)

After lightly sanding the filler over the topsides patch, and otherwise preparing the area, I applied a light coat of color-matched gelcoat, obtained to match the original color of the boat.  The match was very good considering the age of the original gelcoat.  I applied a spray coat of PVA as an oxygen barrier (not shown here), then left the patch to cure before continuing.

I lightly sanded and cleaned up the seacock backing blocks as needed to remove any excess epoxy, then prepared the outsides of all the openings by removing the bottom paint around each fitting.  For the two abandoned through hull holes that I’d filled yesterday, I ground out a dished area several inches across to accept new fiberglass, which I installed afterwards, with layers on both the outside and inside of the old holes.

Continuing work on the bilge area, I began to fill the void left by the removal of some of the old concrete.  For this filler, which was intended only to bring the area flush with the surrounding fiberglass, I used polyester resin mixed with choppings to form a solid mass, and installed the material in several lifts of about 1 qt. total mixed volume over the course of the day, slowly bringing the void up to the level of the surrounding areas; the incremental approach prevented excess heat buildup.  By the end of the day, there was room for probably one more application, which I’d do on the ‘morrow.

Throughout the remainder of the day’s work, I prepared the four new seacocks and through hulls for installation, beginning by preassembling the valves, flange adapter bases, and pipe-hose connectors.

th6-41712

The two 1-1/2″ fittings would require that the through hulls be cut a bit shorter to accommodate the overall thickness of the hull and backing block, so with the fittings pushed through from the outside I made some reference marks for later cutting.  The 3/4″ fittings did not require shortening.

This complete, I dry-installed the various fittings and drilled for the flange mounting bolts, a relatively simple theoretical process that took much longer thanks to difficult access in some areas, but by the end of the day I had all the bolt holes prepared, and would be ready to install the fittings permanently after only a few minor additional steps.

Wednesday, April 18, 2012 (7.5 hours)

To get started, I washed and sanded the fiberglass patches over the two unused through hulls, and, on the exterior, applied a coat of fairing compound.

Next, I made final preparations for installing the four new through hull fittings and seacocks.  The bolt holes required countersinks on the outside so the fasteners could sit flush, so I finished up that work and gathered tools and materials.  Then, I installed the four fittings with polyurethane sealant and bronze fasteners.

There was room for one more application of resin mixed with choppings in the bilge, which brought the voids flush.  Later, when the final layer had cured, I sanded the rough surface and applied a final bit of polyester resin thickened with cabosil to smooth the surface a bit more.  Once that had cured, and after a final light sanding (one endearing quality–perhaps the only–of polyester is that it cures quickly vs. epoxy), I applied two layers of heavy fiberglass with epoxy resin over the entire areas.

On the starboard topsides, I wet-sanded and buffed the new gelcoat, completing the small repair.

With the new through hulls in place, I installed new hoses for the head discharge and galley sink, and resecured the existing head intake hose.  The new engine intake required a new hose and sea strainer; I had the sea strainer on hand, but didn’t have the correct hose in stock, so I ordered what I needed for later installation.  Meanwhile, I made some measurements and notes about a couple remaining small interior projects that I’d wrap up in the near future.

Thursday, April 19, 2012 (3.5 hours)

After a water wash and quick sanding, the bilge work was complete.  I also sanded the two through hull patches, where I’d applied fairing compound earlier, and with that complete I coated the patches with plain epoxy resin to seal the fairing compound (no pictures, sorry).

I spent most of the afternoon working on a punch list to finish up most of the jobs required.  To begin, I installed a new bronze raw water strainer in the locker beneath the galley sink, near the newly located engine intake.  Then, I ran new hoses to the engine itself.  Because the raw water pump on the engine required a 5/8″ hose, while the rest of the system was 3/4″, I had to adapt the hose down with some bronze fittings.

I ordered a new electric bilge pump to replace the non-functioning one in place; to prepare for its arrival next week, I ran new lengths of bilge hose into the sump, as well as a new length of hose for the manual pump.  I’d complete the bilge pump installation once the new pump arrived.

A couple small jobs remained.  One, mounting new hardware for the removable, convertible table in the dinette, required a round wooden base to cover some old holes in the cabin sole, so from a piece of scrap mahogany I cut and shaped the required disc and started the finishing process so I could install it soon.

tablebase-41912

In place of a since-removed gimballed stove, the owner requested a simple shelf in the stove area, which he could use for storage or for a portable stove.  I began shelf construction by cutting a piece of 1/2″ plywood to fit the opening, planning to cover the top with white Formica, with teak trim to match the interior.  I’d wrap up this project next time.

Friday, April 20, 2012 (3.5 hours)

The owner was on hand for much of the morning, during which time we went over some things and completed two small projects from the remaining list:  rebed the traveler, which had been leaking into the quarterberth; and replacing the diesel fuel deck fill.

Afterwards, I wrapped up preliminary work on the basic shelf for the galley area, which would fill in the old stove area and provide a place for a new portable stove and/or stowage.  I cut a shelf from 1/2″ plywood, then scribed the outboard end to fit the hull before installing white Formica over the exposed surface.  I milled a teak fiddle for the exposed edge, then installed the shelf with hardwood cleats beneath.  Nothing fancy, but effective.  I oiled the teak trim to match the existing woodwork.

shelf-42012

The table base was ready for final installation.  I drilled and tapped bolt holes into the cabin sole for machine screws, and  slightly oversize pilotholes through the wooden base, then installed the base with stainless steel screws; the underside of the sole was inaccessible for bolting.  I secured the matching top socket to the table with screws, and the reinstallation of the table was complete.

table-42012

Other than final installation of a new electric bilge pump, which was on order and due Monday, my work list was complete for now.

 

Blue Teal 1

A local boatowner contracted me to do a few small-ish jobs on his Alberg 30 that he hadn’t had time to get to over the winter.    After some pre-project meetings to talk about the proposed scope of the job, as well as his desires and intentions, I eventually picked the boat up in late May and brought her to the shop.

blueteal1

The most significant item on the agenda was to install the basics of a new electrical system–essentially the main battery cables and associated main feeds to the new panels that the owner had selected.  His chosen location for the panels was in the port bulkhead at the forward end of the saloon, mainly for ease of access to the panel backs and for the dryness of the location.

I cut the holes, installed the panels, and ran #2AWG battery cable to a 300A positive distribution buss, from which I ran individual supply cables to each of the two panels, and to a negative distribution buss for the eventual negative wires of the electrical system (not part of this job scope).  Originally, I installed a three-switch battery parallel panel on this bulkhead as well, but after another discussion with the owner, we determined that this location would be awkward for a number of reasons, mainly associated with the lengths of the cable runs required and the difficulty in hiding them properly along the way.

After some additional discussion, I re-installed the battery parallel panel at the aft end of the port settee back, within easy reach for service and close by the engine compartment and battery storage areas beneath the sole to minimize cable runs.  Nearby, I installed other components of the basic system: a 300A main negative distribution buss; a Blue Seas Automatic Charging Relay (ACR), for automatic battery charging and isolation of two banks; and a main 100A fuse block for the service panel feed.  Crucial to all element locations was ease of access for service and maintenance down the road.

I completed the necessary cable runs according to a basic schematic that I planned out using the various components’ instructions and schematics as a guide.  The job required 25′ of yellow #2AWG cable and 75′ of red #2AWG cable.  I ran the wires through some of the hidden lockers, secured them with rubber-lined clamps and wire ties, and protected them where they passed through bulkhead with short lengths of hose that I glued in place in the openings.

Next on the project list was to relocate and reinstall an existing electric diaphragm bilge pump.  I mounted the pump in the locker beneath the starboard-side galley sink (removed by the owner and in storage), and wired it along with the existing float switch in the bilge.  Then I connected it to an existing length of hose from the old installation, extending the hose as needed with a bronze adapter assembly.

electbilgepump-61908

I also installed a Henderson MK IV manual bilge pump in the cockpit, with bulkhead access plate.  Plumbed into an existing through hull fitting in the starboard topsides, I added a Marelon inline shutoff valve that the owner requested.

manualbilgepump-61908

The diesel fuel filter had been located in an awkward position beneath the fuel tank in the starboard cockpit locker, so at the owner’s request I relocated it to a space in the engine room for easy access and servicing.  this required a new length of supply hose, but the other components were pre-existing.

fuelfilter-61508

The owner indicated that his diesel fuel vent line allowed fuel to exit the boat under static conditions.  Looking at the setup, I surmised that because the tubing was level with the tank along its entire run, it must have been  allowing the fuel to run out by gravity alone.  To correct this issue, I replumbed the vent with new hose and fittings, and ran the hose upwards as high as possible immediately after the tank to provide a head that I hoped would eliminate the leakage.

fuelvent-61508

One project that became accelerated to my list, when it had not originally been on the list, was to replace the forward hatch; the owner had planned to replace it himself later, but during the transport to the shop the unsecured hatch flew open and broke, essentially ruining the existing hatch.  The owner decided to have me replace it with his new Lewmar ocean series hatch while the boat was here.

The old trapezoidal flange had to go, so I used a Sawz-all to cut it away; the flange was solid glass, or solid resin with chopped strand at least.  I left a section of the old flange at the aft end because I realized that the new hatch was just a bit narrower than the old opening at this end, and to have cut away the entire flange would have required rebuilding part of the opening before the hatch could be installed.  Instead, I cut and ground the after corners flush with the adjacent decks, avoiding the need for any significant work to fill in the hole.

I built a mahogany frame to support the new hatch, and scribed frame to match the contours of the deck.  After sanding, shaping, and 6 coats of varnish, I installed the frame and hatch in a single operation using 4200 sealant and #10 through bolts with fender washers through the entire assembly, per the owner’s request.

Under previous ownership, the boat had had a hot water heater installed, along with a bewildering assortment of hoses and extra heat exchangers in the space aft of the engine room. The current owner wanted all this removed; he’d already removed the water heater previously.  I removed the excess hose, replumbed the system through the heat exchanger, and moved the heat exchanger several inches higher on the bulkhead so that there’d be better clearance for servicing the pencil zincs, which the owner reported he’d have to cut shorter in order to fit.  I also replaced a jury-rigged and obsolete coolant recovery tank with a new, smaller plastic one plumbed off the heat exchanger cap in the engine room, as per normal.

The top photos show the old setup; the lower photo shows the new setup.

Finally, I installed a 1-1/2″ stainless steel through hull fitting upside down through the deck through which to pass the mast wiring; I chose the SS version because the mushroom flange was small and rounded, for a clean interior appearance; similarly, the nut on the opposite side was smaller than typically seen in bronze fittings, for a cleaner appearance in this application.

With the jobs on the project list complete, the owner made plans to launch the boat shortly thereafter.

Total billed time on this job, including trucking time:  40.25 hours

Newer posts